ML20209F079: Difference between revisions

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=Text=
=Text=
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Cp&L
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Caroliria Power & Light Company                       .g
Caroliria Power & Light Company
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June 27,1985                               m en Dr. 3. Nelson Grace                                                               NRC-375 United States Nuclear Regulatory Commission Region 11 101 Marietta Street, Northwest (Suite 2900)
P. O. Box 101, New Hill, NC 27562 June 27,1985 m
en Dr. 3. Nelson Grace NRC-375 United States Nuclear Regulatory Commission Region 11 101 Marietta Street, Northwest (Suite 2900)
Atlanta, Georgia 30323 CAROLINA POWER & LIGHT COMPANY SHEARON HARR5 NUCLEAR POWER PLANT 1986 - 900,000 KW - UNIT 1 COMPONENT COOLING WATER SYSTEM BUTTERFLY VALVE OPERATORS, ITEM 181
Atlanta, Georgia 30323 CAROLINA POWER & LIGHT COMPANY SHEARON HARR5 NUCLEAR POWER PLANT 1986 - 900,000 KW - UNIT 1 COMPONENT COOLING WATER SYSTEM BUTTERFLY VALVE OPERATORS, ITEM 181


==Dear Dr. Grace:==
==Dear Dr. Grace:==
Attached is our final report on the subject item, which was deemed reportable per the provisions of 10CFR50.55(e) and 10CFR, Part 21 on October 31, 1984. With this report, Carolina Power & Light Company considers this matter closed.
Attached is our final report on the subject item, which was deemed reportable per the provisions of 10CFR50.55(e) and 10CFR, Part 21 on October 31, 1984. With this report, Carolina Power & Light Company considers this matter closed.
If you have any questions concerning this matter, please do not hesitate to contact me.
If you have any questions concerning this matter, please do not hesitate to contact me.
ours very truly, f
ours very truly, f R.\\ WatsonA. 1" t
t    R.\ WatsonA. 1"
' Vice President Shearon Harris Nuclear Power Plant RAW:sae Attachment cc:
                                                      ' Vice President Shearon Harris Nuclear Power Plant RAW:sae Attachment cc:   Messrs. G. Maxwell /R. Prevatte (NRC-SHNPP)
Messrs. G. Maxwell /R. Prevatte (NRC-SHNPP)
Mr. R. C. DeYoung (NRC) 8507120383 DR           850627                                            -
Mr. R. C. DeYoung (NRC) 8507120383 850627 DR ADOCK oso o
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XEX-SMI/1-OS5


CAROLINA POWER & LIGHT COMPANY SHEARON HARRIS NUCLEAR POWER PLANT UNIT NO. 1 FINAL REPORT COMPONENT COOLING WATER SYSTEM BUTTERFLY VALVE OPERATORS ITEM NO. 181 JUNE 27, 1985 REPORTABLE UNDER 10CFR50.55(e) AND 10CFR21 i
CAROLINA POWER & LIGHT COMPANY SHEARON HARRIS NUCLEAR POWER PLANT UNIT NO. 1 FINAL REPORT COMPONENT COOLING WATER SYSTEM BUTTERFLY VALVE OPERATORS ITEM NO. 181 JUNE 27, 1985 REPORTABLE UNDER 10CFR50.55(e) AND 10CFR21 i
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==SUBJECT:==
==SUBJECT:==
10CFR50.55(e) and 10CFR2l Reportable Item, Shearon Harris Nuclear Power Plant Unit 1, Unqualified Valve Operators for Component Cooling Water System Butterfly Valves.
10CFR50.55(e) and 10CFR2l Reportable Item, Shearon Harris Nuclear Power Plant Unit 1, Unqualified Valve Operators for Component Cooling Water System Butterfly Valves.
ITEM:     ,
ITEM:
Valve operators (Limitorque) for component cooling water system valves.
Valve operators (Limitorque) for component cooling water system valves.
                                \
\\
SUPPLIED BY ,   Westinghouse Water Reactor Divisions.
SUPPLIED BY,
NATURE OF DEFICIENCY     CPSL identified in July, 1984 that motor operators supplied by Westinghouse for certain butterfly valves in the component cooling water system were not qualified as 1E.
Westinghouse Water Reactor Divisions.
i DATE PROBLEM WAS CONFIRMED TO EXIST       CP&L determined on July 3, 1984 that a potentially reportable condition existed.
NATURE OF DEFICIENCY CPSL identified in July, 1984 that motor operators supplied by Westinghouse for certain butterfly valves in the component cooling water system were not qualified as 1E.
PROBLEM REPORTED:       K. V. Hate' notified the NRC (Mr. A. Hardin) that this item was potentially reportable under 10CFR50.55(e) and 10CFR21 on July 5, 1984.
i DATE PROBLEM WAS CONFIRMED TO EXIST CP&L determined on July 3, 1984 that a potentially reportable condition existed.
PROBLEM REPORTED:
K. V. Hate' notified the NRC (Mr. A. Hardin) that this item was potentially reportable under 10CFR50.55(e) and 10CFR21 on July 5, 1984.
K. V. Hate' notified the NRC (Mr. P. Fredrickson) that thia item was reportable under 10CFR50.55(e) and 10CFR21 on October 31, 1984.
K. V. Hate' notified the NRC (Mr. P. Fredrickson) that thia item was reportable under 10CFR50.55(e) and 10CFR21 on October 31, 1984.
SCOPE OF PROBLEM:       SHNPP Unit 1 component cooling water system butterfly valve operatore (four).
SCOPE OF PROBLEM:
SAFETY IMPLICATIONS:   Failure of the operators could create the inability to separate the redandant trains of component cooling water, except by manual closure via the hand operators.
SHNPP Unit 1 component cooling water system butterfly valve operatore (four).
SAFETY IMPLICATIONS:
Failure of the operators could create the inability to separate the redandant trains of component cooling water, except by manual closure via the hand operators.
REASON PROBLEM IS REPORTABLE: Failure of the operators could lead to a degraded safety condition.
REASON PROBLEM IS REPORTABLE: Failure of the operators could lead to a degraded safety condition.
I IBMD-WKBB01-OS4
I IBMD-WKBB01-OS4


x CORRECTIVE ACTION:                       Westinghouse has evaluated the Limitorque operators supplied for these valves and has determined that they are qualified for IE applications without modification. Westinghouse submitted the
x CORRECTIVE ACTION:
                                                  " Qualification of CCWS 18 inch Butterfly Valve Limitorque Motor / Gear Operator Assemblies" to Carolina Power and Light via letter CQL-8367.
Westinghouse has evaluated the Limitorque operators supplied for these valves and has determined that they are qualified for IE applications without modification. Westinghouse submitted the
FINAL REPORT                 Carolina Power & Light considers these valve operators qualified for their intended service. This item is considered complete.
" Qualification of CCWS 18 inch Butterfly Valve Limitorque Motor / Gear Operator Assemblies" to Carolina Power and Light via letter CQL-8367.
FINAL REPORT Carolina Power & Light considers these valve operators qualified for their intended service. This item is considered complete.
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Latest revision as of 18:04, 6 December 2024

Part 21 & Final Deficiency Rept,Item 181 Re Component Cooling Water Sys Butterfly Valve Operators Not Qualified as Class 1E.Initially Reported on 841031.Westinghouse Determined Limitorque Operators Qualified W/O Mod
ML20209F079
Person / Time
Site: Harris 
Issue date: 06/27/1985
From: Watson R
CAROLINA POWER & LIGHT CO.
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
CON-NRC-375, REF-PT21-85, REF-PT21-85-305-000 181, PT21-85-305, PT21-85-305-000, NUDOCS 8507120383
Download: ML20209F079 (4)


Text

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Caroliria Power & Light Company

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P. O. Box 101, New Hill, NC 27562 June 27,1985 m

en Dr. 3. Nelson Grace NRC-375 United States Nuclear Regulatory Commission Region 11 101 Marietta Street, Northwest (Suite 2900)

Atlanta, Georgia 30323 CAROLINA POWER & LIGHT COMPANY SHEARON HARR5 NUCLEAR POWER PLANT 1986 - 900,000 KW - UNIT 1 COMPONENT COOLING WATER SYSTEM BUTTERFLY VALVE OPERATORS, ITEM 181

Dear Dr. Grace:

Attached is our final report on the subject item, which was deemed reportable per the provisions of 10CFR50.55(e) and 10CFR, Part 21 on October 31, 1984. With this report, Carolina Power & Light Company considers this matter closed.

If you have any questions concerning this matter, please do not hesitate to contact me.

ours very truly, f R.\\ WatsonA. 1" t

' Vice President Shearon Harris Nuclear Power Plant RAW:sae Attachment cc:

Messrs. G. Maxwell /R. Prevatte (NRC-SHNPP)

Mr. R. C. DeYoung (NRC) 8507120383 850627 DR ADOCK oso o

i o FIC}hLC g

XEX-SMI/1-OS5

CAROLINA POWER & LIGHT COMPANY SHEARON HARRIS NUCLEAR POWER PLANT UNIT NO. 1 FINAL REPORT COMPONENT COOLING WATER SYSTEM BUTTERFLY VALVE OPERATORS ITEM NO. 181 JUNE 27, 1985 REPORTABLE UNDER 10CFR50.55(e) AND 10CFR21 i

IBMD-WKBB01-OS4

SUBJECT:

10CFR50.55(e) and 10CFR2l Reportable Item, Shearon Harris Nuclear Power Plant Unit 1, Unqualified Valve Operators for Component Cooling Water System Butterfly Valves.

ITEM:

Valve operators (Limitorque) for component cooling water system valves.

\\

SUPPLIED BY,

Westinghouse Water Reactor Divisions.

NATURE OF DEFICIENCY CPSL identified in July, 1984 that motor operators supplied by Westinghouse for certain butterfly valves in the component cooling water system were not qualified as 1E.

i DATE PROBLEM WAS CONFIRMED TO EXIST CP&L determined on July 3, 1984 that a potentially reportable condition existed.

PROBLEM REPORTED:

K. V. Hate' notified the NRC (Mr. A. Hardin) that this item was potentially reportable under 10CFR50.55(e) and 10CFR21 on July 5, 1984.

K. V. Hate' notified the NRC (Mr. P. Fredrickson) that thia item was reportable under 10CFR50.55(e) and 10CFR21 on October 31, 1984.

SCOPE OF PROBLEM:

SHNPP Unit 1 component cooling water system butterfly valve operatore (four).

SAFETY IMPLICATIONS:

Failure of the operators could create the inability to separate the redandant trains of component cooling water, except by manual closure via the hand operators.

REASON PROBLEM IS REPORTABLE: Failure of the operators could lead to a degraded safety condition.

I IBMD-WKBB01-OS4

x CORRECTIVE ACTION:

Westinghouse has evaluated the Limitorque operators supplied for these valves and has determined that they are qualified for IE applications without modification. Westinghouse submitted the

" Qualification of CCWS 18 inch Butterfly Valve Limitorque Motor / Gear Operator Assemblies" to Carolina Power and Light via letter CQL-8367.

FINAL REPORT Carolina Power & Light considers these valve operators qualified for their intended service. This item is considered complete.

t l

b I

IBMD-WKBB01-OS4

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