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{{#Wiki_filter:NRV'FORM | {{#Wiki_filter:DOC~T NUMBER NRV'FORM | ||
PROP | <2.7G) | ||
J5 U.S. NUCLEAR REGULATORV Co SSION | |||
'SO~BM FILE NUMBER NRC DISTRIBUTION FoR PART 50 DOCKET MATERIAL INCIDENT REPORT TO: . DATE OF DOCUMENT Florida Power 6 Light Company 4/4/77 Miami, Florida Mr. Norman C. Moseley A~ D~ Schmidt. | |||
DATE RECEIVED 4/18/77 ETTER ONOTORIZED PROP INPUT FORM NUMBER OF COPIES RECEIVED CRRIGINAL Ocopv PRONCLASSIFIED ENCLOSURE sE<~~ | |||
DESCRIPTION Ltr, trans the following: Licensee Event Report (RO 50-335/77-16) on 3/5/77 concerning low steam gener'ator pressure trips being received on channel A RPS and channel A MSIS ~ ~ ~ ~ ~ ~ | |||
<m@@BSI I | |||
PLANT NAME: (1-P) (2-P) | |||
) ~ | |||
ISt. Lucie Unit No. 1 Ig Jiff hHBf.. | |||
RJL NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFORMATION BRANCH CHIEF: R iC~nrt 8 3 CYS FOR ACTION LICo ASST,: | |||
W CYS'CRS CYS S!%&INC S NT INTERNAL D IST R I BUTION EG RIL NRC PDR M6cE 2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES CASE BUTLER HANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS E NAL DISTRIBUTION CONTROL NUMBER LPDR0 TZC0 N | |||
PPJo go+ 5'f NRC FORM 196 (2 7GI | |||
==Dear Mr.Moseley:== | 4 ~ | ||
REPORTABLE OCCURRENCE 335-77-16 ST.LUCIE UNIT 1 DATE OF OCCURRENCE: | Ivy 4 yg | ||
MARCH 5, 1977 STEAM GENERATOR PRESSURE TRANSMITTER The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence. | |||
Very truly yours, D.c it Vice President Power Resources MAS/cpc Attachment cc: Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (30)Director, Office of Management Information and Program Control (3)>7mb'dA Y$I PEOPLE...SERVING PEOPLE | FLORIOA POWER & LIGHT COMPANY April 4, 1977 | ||
~-.e.~>~P'I P | -Px-77-PQ$ j; Mr. Norman C. Moseley, Director, Region Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. W., Suite 1217 Atlanta, Georgia 30303 | ||
UCENSEE NAME 01 F L S L S 1 0 | |||
! | ==Dear Mr. Moseley:== | ||
~~4 0 0 0 7 8 9 11 12 PROBABLE CONSEQUENCES Qg | |||
,7 89 80 7 89 NAME M.A.Scho man | REPORTABLE OCCURRENCE 335-77-16 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: MARCH 5, 1977 STEAM GENERATOR PRESSURE TRANSMITTER The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence. | ||
Very truly yours, D. c it Vice President Power Resources MAS/cpc Attachment cc: Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (30) | |||
Director, Office of Management Information and Program Control (3) | |||
> 7mb'dA Y$ | |||
I PEOPLE... SERVING PEOPLE | |||
~-.e. ~> ~ | |||
P'I P | |||
LICENSEE EVENT REPORT CONTROL 8LOCK | |||
~ | |||
(PLEASE PRINT ALL RECIUIREO INFORMATION) | |||
UCENSEE UCENSE EVENT ~ | |||
NAME UCENSE NUMSER TYPE TYPE 01 F L S L S 1 0 0 0 0 0 0 0 0 0 A 1 1 1 1 L0OO3~I | |||
.7 89 | |||
~ | |||
14 15 25 26 30 31 32 REPORT AEPOAT CATEGORY TYPE SOURCE OOCKET NUh18EA EVENT OATE REPORT OATE I001] coN'T ~L L 0 5 0 0 3 3 5 0 3 0 5 7 7 0 3 1 6 7 7 7 8 57 58 59 60 61 68 69 74 75 , 8O EVENT DESCRIPTION Qg Durin 89 Power 0 eration low steam enerator 'essure tri s were received on channel A 8O t003j RPS and channel A MSIS. Action was taken in accordance with Technical S ecifications 7 89 80 | |||
~4 7 8 9 | |||
. .1 ion 2. and . .2.1 action' . The affected channel A tri s were 80 Qog d o service in 1.25 hours. This was the fourth occurrence of an ino erable RPS 7 8 9 80 Jog FAS channe . The revious occurrences were re orted as LER's 335-76-5 loss of 7 8 9 PAME 80 SYSTEM CAUSE COMPONENT COOE COOE, COMPONENT COOE SUPPUER I007I ~TA ~E x x x x x x z z 9 9 9 N 7 8 9 10 11 12 17 43 a7 48 CAUSE OESCRIPTION I008 The fuse rotectin the DC ower su 1 for steam enerator channel A ressure trans-7 8 9 80 7 | |||
Q~ I8 9 mitter PT-8013A failed. The ower su 1 and'nstrument loo were checked for other 80 7 89 roblems and none were found. The fuse was re laced and the channel A tri set oint was FACiUTY 8O METHOO OF STATUS .1 POWER OTHER STATUS OISCOVEAY OISCOVEAY OESCAIPTION 0~g 0 ~O NA A NA 7 8 9 10 12 13 44 45 46 80 FOAM OF ACTIVITY COATENT RELEASEO OF RELEASE AhIOUNT OF ACTIVITY LOCATION OF RELEASE KRI NA NA 7 8 9 10 11 44 45 PERSONNEL EXPOSURES NUMSER TYPE OFSCAIPTION 7 | |||
Q~~] | |||
8 9 | |||
~(~0 11 z | |||
12 13 NA 80 PERS'ONNEL !NJURIES OESCAIPTION | |||
~~4 0 0 0 NA 7 8 9 11 12 60 PROBABLE CONSEQUENCES Qg NA | |||
'7 89 80 LOSS OR OAMAGE TO FACIUTY TYPE OESCAIPTICN z NA 7 89 10 80 PUSLICITY NA 7 89 ~ 80 AOOITIONAL FACTORS Q~ g See a e two for continuation of Event Descri tion and Cause Description. | |||
,7 89 80 7 89 80 NAME M. A. Scho man 305/552-3779 PHONEI CPO IISI 6IIT | |||
LICENSEE EVENT REPORT REPORTABLE OCCURRENCE 335-77-16 PAGE TWO EVENT DESCRIPTION (Continued) power caused by loose electrical connections), 335-76-17 (ESFAS setpoint drift), | |||
and 335-76-26 (loss of power due to 1C inverter failure). This occurrence was not related to the previous occurrences. | |||
(335-77-16). | (335-77-16). | ||
CAUSE DESCRIPTION (Continued) | CAUSE DESCRIPTION (Continued) | ||
Verified. | Verified. | ||
y'~ | |||
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Latest revision as of 03:30, 3 February 2020
ML18110A891 | |
Person / Time | |
---|---|
Site: | Saint Lucie |
Issue date: | 04/04/1977 |
From: | Schmidt A Florida Power & Light Co |
To: | Moseley N NRC/IE, NRC/RGN-II |
References | |
PRN-LI-77-98 LER 1977-016-00 | |
Download: ML18110A891 (7) | |
Text
DOC~T NUMBER NRV'FORM
<2.7G)
J5 U.S. NUCLEAR REGULATORV Co SSION
'SO~BM FILE NUMBER NRC DISTRIBUTION FoR PART 50 DOCKET MATERIAL INCIDENT REPORT TO: . DATE OF DOCUMENT Florida Power 6 Light Company 4/4/77 Miami, Florida Mr. Norman C. Moseley A~ D~ Schmidt.
DATE RECEIVED 4/18/77 ETTER ONOTORIZED PROP INPUT FORM NUMBER OF COPIES RECEIVED CRRIGINAL Ocopv PRONCLASSIFIED ENCLOSURE sE<~~
DESCRIPTION Ltr, trans the following: Licensee Event Report (RO 50-335/77-16) on 3/5/77 concerning low steam gener'ator pressure trips being received on channel A RPS and channel A MSIS ~ ~ ~ ~ ~ ~
<m@@BSI I
PLANT NAME: (1-P) (2-P)
) ~
ISt. Lucie Unit No. 1 Ig Jiff hHBf..
RJL NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFORMATION BRANCH CHIEF: R iC~nrt 8 3 CYS FOR ACTION LICo ASST,:
W CYS'CRS CYS S!%&INC S NT INTERNAL D IST R I BUTION EG RIL NRC PDR M6cE 2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES CASE BUTLER HANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS E NAL DISTRIBUTION CONTROL NUMBER LPDR0 TZC0 N
PPJo go+ 5'f NRC FORM 196 (2 7GI
4 ~
Ivy 4 yg
FLORIOA POWER & LIGHT COMPANY April 4, 1977
-Px-77-PQ$ j; Mr. Norman C. Moseley, Director, Region Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. W., Suite 1217 Atlanta, Georgia 30303
Dear Mr. Moseley:
REPORTABLE OCCURRENCE 335-77-16 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: MARCH 5, 1977 STEAM GENERATOR PRESSURE TRANSMITTER The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.
Very truly yours, D. c it Vice President Power Resources MAS/cpc Attachment cc: Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (30)
Director, Office of Management Information and Program Control (3)
> 7mb'dA Y$
I PEOPLE... SERVING PEOPLE
~-.e. ~> ~
P'I P
LICENSEE EVENT REPORT CONTROL 8LOCK
~
(PLEASE PRINT ALL RECIUIREO INFORMATION)
UCENSEE UCENSE EVENT ~
NAME UCENSE NUMSER TYPE TYPE 01 F L S L S 1 0 0 0 0 0 0 0 0 0 A 1 1 1 1 L0OO3~I
.7 89
~
14 15 25 26 30 31 32 REPORT AEPOAT CATEGORY TYPE SOURCE OOCKET NUh18EA EVENT OATE REPORT OATE I001] coN'T ~L L 0 5 0 0 3 3 5 0 3 0 5 7 7 0 3 1 6 7 7 7 8 57 58 59 60 61 68 69 74 75 , 8O EVENT DESCRIPTION Qg Durin 89 Power 0 eration low steam enerator 'essure tri s were received on channel A 8O t003j RPS and channel A MSIS. Action was taken in accordance with Technical S ecifications 7 89 80
~4 7 8 9
. .1 ion 2. and . .2.1 action' . The affected channel A tri s were 80 Qog d o service in 1.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />. This was the fourth occurrence of an ino erable RPS 7 8 9 80 Jog FAS channe . The revious occurrences were re orted as LER's 335-76-5 loss of 7 8 9 PAME 80 SYSTEM CAUSE COMPONENT COOE COOE, COMPONENT COOE SUPPUER I007I ~TA ~E x x x x x x z z 9 9 9 N 7 8 9 10 11 12 17 43 a7 48 CAUSE OESCRIPTION I008 The fuse rotectin the DC ower su 1 for steam enerator channel A ressure trans-7 8 9 80 7
Q~ I8 9 mitter PT-8013A failed. The ower su 1 and'nstrument loo were checked for other 80 7 89 roblems and none were found. The fuse was re laced and the channel A tri set oint was FACiUTY 8O METHOO OF STATUS .1 POWER OTHER STATUS OISCOVEAY OISCOVEAY OESCAIPTION 0~g 0 ~O NA A NA 7 8 9 10 12 13 44 45 46 80 FOAM OF ACTIVITY COATENT RELEASEO OF RELEASE AhIOUNT OF ACTIVITY LOCATION OF RELEASE KRI NA NA 7 8 9 10 11 44 45 PERSONNEL EXPOSURES NUMSER TYPE OFSCAIPTION 7
Q~~]
8 9
~(~0 11 z
12 13 NA 80 PERS'ONNEL !NJURIES OESCAIPTION
~~4 0 0 0 NA 7 8 9 11 12 60 PROBABLE CONSEQUENCES Qg NA
'7 89 80 LOSS OR OAMAGE TO FACIUTY TYPE OESCAIPTICN z NA 7 89 10 80 PUSLICITY NA 7 89 ~ 80 AOOITIONAL FACTORS Q~ g See a e two for continuation of Event Descri tion and Cause Description.
,7 89 80 7 89 80 NAME M. A. Scho man 305/552-3779 PHONEI CPO IISI 6IIT
LICENSEE EVENT REPORT REPORTABLE OCCURRENCE 335-77-16 PAGE TWO EVENT DESCRIPTION (Continued) power caused by loose electrical connections), 335-76-17 (ESFAS setpoint drift),
and 335-76-26 (loss of power due to 1C inverter failure). This occurrence was not related to the previous occurrences.
(335-77-16).
CAUSE DESCRIPTION (Continued)
Verified.
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