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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- 05000336/LER-1981-030, Forwards LER 81-030/03L-0 + (19:39:43, 20 December 2024)
- ML20031B038 + (19:39:45, 20 December 2024)
- ML20031B036 + (19:39:46, 20 December 2024)
- ML20031B035 + (19:39:47, 20 December 2024)
- ML20031B034 + (19:39:49, 20 December 2024)
- 05000333/LER-1981-068-03, /03L-0:on 810824,while Conducting Surveillance to Satisfy Tech Spec Table 4.2-2,HPCI High Steam Flow Differential Pressure Switch Was Found Set Above Tech Specs. Caused by Instrument Drift.Instrument Recalibr + (19:39:50, 20 December 2024)
- ML20031B032 + (19:39:52, 20 December 2024)
- 05000333/LER-1981-068, Forwards LER 81-068/03L-0 + (19:39:53, 20 December 2024)
- 05000271/LER-1981-024-03, /03L-0:on 810819,during Monthly Surveillance Testing,Reactor Core Isolation Cooling Tripped Via Mechanical Overspeed.Caused by Failure of Egr.Egr Replaced + (19:39:55, 20 December 2024)
- ML20031B027 + (19:39:57, 20 December 2024)
- 05000293/LER-1981-049-01, /01T-0:on 810828,bypass Condition Existed in B RBCCW Heat Exchanger (E209B) & B Loop Declared Inoperable. Caused by Water Erosion Problem Due to High Delta P Caused by Mussel Incursion in Heat Exchanger + (19:39:58, 20 December 2024)
- 05000271/LER-1981-024, Forwards LER 81-024/03L-0 + (19:40:00, 20 December 2024)
- ML20031B023 + (19:40:02, 20 December 2024)
- 05000293/LER-1981-048-03, /03L-0:on 810830,torus Temp Tech Spec Limit of 80 F Was Exceeded by One Degree F.Caused by One RBCCW Heat Exchanger Being Out of Svc & Entire RBCCW Heat Load Carried by Inservice Heat Exchanger.Operators Counseled + (19:40:05, 20 December 2024)
- 05000316/LER-1981-043-03, /03L-0:on 810815,load Reduction of Approx 240 MW Occurred.Caused by Time Delay Involved in electro-hydraulic Control Sys.Ler Being Circulated to All Control Room Operators as Alert + (19:40:07, 20 December 2024)
- 05000316/LER-1981-043, Forwards LER 81-043/03L-0 + (19:40:10, 20 December 2024)
- 05000293/LER-1981-048, Forwards LER 81-048/03L-0 + (19:40:15, 20 December 2024)
- ML20031B014 + (19:40:17, 20 December 2024)
- 05000333/LER-1981-067-03, /03L-0:on 810821,core Spray Permissive Pressure Switch 02-PS-52A Found Set at 436 Psig Instead of 450 Psig or Greater.Caused by Instrument Drift.Pressure Switch Adjusted to within Tech Spec Limits + (19:40:19, 20 December 2024)
- 05000346/LER-1981-050-03, /03L-0:on 810820,containment Isolation Valves Cv 124,CV 125,NN 58,SA 502 & IA 501 Not Tested Prior to 810812.Caused by Procedure Inaccuracy.Procedures ST 5099.08 & Sp 1102.01 Modified to Test Valves in Cold Shutdown + (19:40:21, 20 December 2024)
- 05000346/LER-1981-050, Forwards LER 81-050/03L-0 + (19:40:23, 20 December 2024)
- 05000333/LER-1981-067, Forwards LER 81-067/03L-0 + (19:40:25, 20 December 2024)
- 05000277/LER-1981-039-01, /01T-0:on 810827,C Average Power Range Monitor Found Receiving Only One Low Power Range Monitor (LPRM) Input to C Level.Caused by 810818 LPRM 32-49C Failure & Operator Failure to Recognize Situation + (19:40:26, 20 December 2024)
- 05000295/LER-1981-039-01, /01T-0:on 810904,during QA Audit,No Calibr Data Found on File to Verify Calibr of Reactor Coolant Pump Trip Undervoltage & Underfrequency Relays.Caused by Lack of Procedures.Procedure Changed to Assure Calibr + (19:40:28, 20 December 2024)
- 05000277/LER-1981-039, Forwards LER 81-039/01T-0.Detailed Event Analysis Encl + (19:40:30, 20 December 2024)
- 05000295/LER-1981-039, Forwards LER 81-039/01T-0 + (19:40:32, 20 December 2024)
- 05000312/LER-1981-043-03, /03L-0:on 810818,performance of Surveillance Procedure Revealed 26 Discrepant Pipe Penetration Fire Stops.Caused by Insufficient Grouting,Supports & Silicone Foam.Fire Watch Will Continue Pending Repairs by 811215 + (19:40:34, 20 December 2024)
- ML20031B000 + (19:40:36, 20 December 2024)
- ML20031A997 + (19:40:38, 20 December 2024)
- ML20031A996 + (19:40:40, 20 December 2024)
- ML20031A994 + (19:40:42, 20 December 2024)
- ML20031A992 + (19:40:44, 20 December 2024)
- TXX-3408, Responds to Generic Ltr 81-21 Re Natural Circulation Cooldown.Facility Will Use Applicable Natural Circulation Cooldown Rates & Primary Sys Subcooling Requirements Outlined in Westinghouse Owners Group 810420 Summary Rept + (19:40:45, 20 December 2024)
- ML20031A988 + (19:40:47, 20 December 2024)
- ML20031A987 + (19:40:48, 20 December 2024)
- ML20031A986 + (19:40:49, 20 December 2024)
- ML20031A984 + (19:40:51, 20 December 2024)
- ML20031A983 + (19:40:52, 20 December 2024)
- 05000029/LER-1981-025-03, /03L-0:on 810820,primary Vent Stack Gaseous & Particulate Radiation Monitor Ratemeters Failed.Caused by Moisture in Detector Due to Air Dryer Coolant Leak.Dryer Replaced.Review Continuing + (19:40:56, 20 December 2024)
- 05000029/LER-1981-025, Forwards LER 81-025/03L-0 + (19:40:58, 20 December 2024)
- ML20031A977 + (19:41:00, 20 December 2024)
- ML20031A976 + (19:41:00, 20 December 2024)
- ML20031A974 + (19:41:01, 20 December 2024)
- ML20031A972 + (19:41:02, 20 December 2024)
- IR 05000155/1981008 + (19:41:03, 20 December 2024)
- ML20031A969 + (19:41:05, 20 December 2024)
- ML20031A968 + (19:41:06, 20 December 2024)
- 05000315/LER-1981-038-03, /03L-0:on 810820,during Routine Insp of 1AB Emergency Diesel,Taper Pin Fuel Rack Assembly Was Loose & Upon Removal Discovered to Be Broken.Cause Unknown.Insp of Linkage Pins Has Been Added to 18-month Insp + (19:41:08, 20 December 2024)
- 05000155/LER-1981-015-03, /03L-0:on 810813,pressure Sensor for Automatic Start of Diesel on Low Fire Sys Header Pressure Found Inadvertently Valved Closed for Excessive Period.Caused by Operator Error.Valve Restored & Procedures re-emphasized + (19:41:10, 20 December 2024)
- ML20031A964 + (19:41:12, 20 December 2024)
- ML20031A963 + (19:41:15, 20 December 2024)