Search by property
Jump to navigation
Jump to search
This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ENS 41692 +
- 05000325/LER-2005-004 +
- ML14093A189 +
- ML13297A103 +
- ML073320364 +
- RA-05-021, Co. 2004 Radiological Reports +
- ML19320B998 +
- ML050460289 +
- ENS 45986 +
- ML031480618 +
- ML031130008 +
- ML042080125 +
- ML20077Q127 +
- ML20095C699 +
- IR 05000250/2020002 +
- ML20149E864 +
- ML20238E459 +
- ML20237E620 +
- ML20235T020 +
- NL-89-046, Forwards Rept of 1988 Annual Emergency Exercise Conducted on 881003.Exercise Included Util & Offsite Agency Participation & Was Evaluated by NRC & FEMA +
- JAFP-87-0534, Reactor Containment Bldg Integrated Leakage Rate Test Types A,B & C Periodic Test +
- RBG-43-503, Forwards Nonroutine Repts Sent to Other Agencies,Per App B (Environ Protection Plan) to River Bend Station License NPF-47 +
- 1CAN098305, Monthly Operating Rept for Aug 1983 +
- ML23251A016 +
- 05000416/LER-1989-006, :on 890505,reactor Tripped on Low Reactor Water Level.Caused by Vessel Overfeed Due to Feedwater Heater Outlet Valves Not Fully Closed But Indicated as Closed. Design Changes to Feedwater Logic Evaluated +
- 05000293/LER-1999-008-02, :on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With +
- 05000461/LER-1986-024, :on 861210,Group I Containment Isolation Signal Generated Resulting in Closure of Main Steam Drain Valves B21-F016 & B21-F019.Caused by Failure of Maint Planners to Review Documents When Preparing Impact Matrix +
- 05000413/LER-1986-028, :on 860606,unidentified RCS Leakage Exceeded Tech Spec Limit of 1 Gpm.Caused by Seal 2 Becoming Unseated. Reactor Coolant Drain Tank Level Transmitter Recalibr & Seal 2 Reseated +
- 05000414/LER-1998-006-04, :on 981021,rod Control Sys Malfunction Occurred Due to Failed Card Leading to Manual Reactor Trip & Esf. Reactor Startup Was Suspended & Troubleshooting Efforts Were Initiated & Slave Cycler Lift Decoder Card Was Replaced +
- 05000498/LER-1988-019, :on 880212 & 13 Unit Cooldown to Satisfy Tech Spec 3.0.3 Prematurely Terminated.Caused by Personnel Error. Addl Guidance for Determining Equipment Operability & Special Training Held +
- 05000331/LER-1985-044, :on 851105,RCIC Taken Out of Svc to Modify RCIC-to-vessel Inject Valve Circuitry.Repair Completed.On 851107,RCIC Tripped on Electrical Overspeed.Caused by Setpoint Drift on Overspeed Trip Monitor +
- 05000397/LER-1985-033, :on 850525,noise Spike in Intermediate Range Monitor Channels Resulted in Reactor Protection Sys Actuation.Caused by Movement of Intermediate Range Monitor by Water Spray.Caution Signs to Be Put in Area +
- 05000265/LER-1995-005-09, :on 950825,Units Experienced Automatic Reactor Scram During EHC Pressure Regulator fail-over Test.Caused by Inadequate EHC Sys Pressure Regulator Setpoint Bias.Adjusted EHC Sys Pressure Setpoint Bias & Time Lag Constants +
- 05000353/LER-1990-015-02, :on 900910,reactor Scram Occurred Due to Spurious Trip Signal from Steam Leak Detection Sys Temp Switch.Caused by Equipment Failure.Temp Switch TTS-25-216D Was Replaced +
- 05000272/LER-1981-062, Forwards LER 81-062/03l-0.Detailed Event Analysis Encl +
- ML20030A487 +
- PLA-8058, Annual Radiological Environmental Operating Report (PLA-8058) +
- 05000397/LER-1993-002, :on 930121,low RPV Level Reactor Scram Initiated by RPS in Response to Low Water Level Condition. Caused by Inadvertent Actuation of Deluge Sys.Plant Procedure PPM 8.3.120 Will Be Revised +
- 05000397/LER-1993-003, :on 930121,determined That Under Certain Ac Electrical Distribution Sys Alignments,Fault Could Result in Unavailability of Both Offsite Power Sources.Caused by Inadequate Sys Analysis.Delay Times Revised +
- 05000280/LER-2010-003, For Surry Power Station, Regarding Loss of Vital Bus Due to Human Error Results in Automatic Reactor Trip +
- BSEP 05-0059, Request for Notice of Enforcement Discretion Technical Specification 3.4.5, RCS Leakage Detection Instrumentation +
- 05000293/LER-1999-008-01, Regarding Automatic Scram at 100 Percent Power Due to Turbine Trip +
- BVY-04-036, March 2004 Monthly Operating Report from Vermont Yankee +
- 05000389/LER-2003-006, Regarding Long-Standing 2C TDAFW Pump Design Issue Resulted in Condition Prohibited by Technical Specifications +
- 05000389/LER-2003-005, Regarding Automatic Reactor Trip Due to Loss of Turbine Generator Excitation +
- ML16214A216 +
- 05000272/LER-1983-026-03, /03L-0:on 830530,containment Fan Coil Unit (Cfcu) 17 Svc Water Flow Observed Below Tech Specs.Cfcu Declared Inoperable.Caused by Valve 15SW57 Being Plugged W/Shells & Debris from Cleaning of Svc Water Sys +
- ENS 57925 +