Search by property
Jump to navigation
Jump to search
This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20084A065 + (ML20084A065)
- 05000364/LER-1984-004-01, :on 840327,reactor Tripped from 100% Power Due to Power Range Neutron High Flux Negative Rate.Caused by Control Rods Dropping Into Core Due to Voltage Surge Caused by Severe Lightning.Power Supplies Reset + (ML20084A066)
- 05000373/LER-1984-019, :on 840320,while Investigating Differential Flow Indication Problem,Incorrect Calibr Data Used to Calibr Reactor Water Cleanup Sys Inlet Flow Transmitter.Caused by Conflicting Instrument Data Sheets + (ML20084A067)
- ML20084A068 + (ML20084A068)
- 05000237/LER-1976-070-03, /03L-0:on 761218,diesel Generator Failed to Carry Required Load Following Monthly Surveillance.Caused by Water in Diesel Fuel Supply.Fuel Oil Day Tank Drained & Lines & Piping Flushed + (ML20084A073)
- 0CAN948401, Informs of Effects of Util General Ofc Work Disruption Due to 840408 Electrical fire.NUREG-0737,Suppl 1 Unit 2 Safety Parameter Display Sys Safety Analysis & NUREG-0737,Suppl 1 Update Will Be Delayed Due to Word Processor Breakdown + (ML20084A074)
- 2CAN948403, Forwards Results of Fuel Insps at End of Third Cycle.Rept Completes FSAR Commitment for Fuel Insp Submittals + (ML20084A077)
- PLA-2033, Interim Deficiency Rept Re Clamps on Control Rod Drive Insert/Withdraw Lines Not Providing Axial Restraint. Initially Reported on 831209.Design Mod to Pedestal Support Initiated.Also Reportable Per Part 21 + (ML20084A079)
- RBG-17-615, Forwards State of La Re Historical & Archaeological Investigation of Ruins of Nineteenth Century Sugar Mill in West Feliciana Parish,La,Per Request. Property Ineligible for Inclusion in Natl Register + (ML20084A086)
- 05000237/LER-1976-034-01, /01T-0:on 760525,during Automatic Blowdown Surveillance Testing,Relief Valve 203-3A Remained Open. Caused by Excessive Leakage in Pilot Stage of Valve.Valve Pilot & Secondary Stages Replaced + (ML20084A087)
- ML20084A090 + (ML20084A090)
- ML20084A093 + (ML20084A093)
- 3F0484-15, Forwards Annual Financial Repts 1983 for Florida Power Corp & Participants,Excluding Cities of Kissimmee & Tallahassee. Comprehensive Financial Statements & Auditors Rept Also Encl + (ML20084A094)
- ML20084A097 + (ML20084A097)
- ML20084A099 + (ML20084A099)
- 05000237/LER-1976-069-01, /01T-0:on 761214,notification Received from GE That MAPLHGR Limits No Longer Considered Sufficiently Conservative.Caused by Adminstrative Error.Tech Spec Rev Request Initiated + (ML20084A104)
- 05000244/LER-1976-007-03, /03L:on 760227,sump a Discharge AOV Not Closed. Caused by Westinghouse Type MG-6 Relays Having Improper Latch Screw Factory Adjustment.Relays Replaced + (ML20084A105)
- ML20084A113 + (ML20084A113)
- 05000244/LER-1976-006-03, /03L:on 760206,undervoltage Device 274/11B Failed to Drop to de-energized Position After Undervoltage Signal Simulated.Caused by Buildup of Bushing Deposits on Plunger Shaft.New Relays to Be Installed + (ML20084A119)
- 05000237/LER-1976-068-03, /03L-0:on 761212,CRD F-5 Found to Uncouple & Overtravel When Withdrawn to Position 48 Following 50% Core Scram Testing.Caused by Loosened Inner Filter.Crd F-5 to Be Disassembled & Insp + (ML20084A122)
- ML20084A125 + (ML20084A125)
- 05000237/LER-1976-033-03, /03L-0:on 760523,prior to Unit Startup,Diesel Generator 43 Failed to Start on First Attempt.Possibly Caused by Problem in Airstart sys.Sequential-event Checklist for Each Start Being Used to Track Problem + (ML20084A134)
- ML20084A135 + (ML20084A135)
- ML20084A136 + (ML20084A136)
- ML20084A139 + (ML20084A139)
- ML20084A141 + (ML20084A141)
- ML20084A149 + (ML20084A149)
- ML20084A156 + (ML20084A156)
- AECM-84-0240, Forwards Update Rept on Tdi Standby Diesel Generators. Info Provided in Support of Resolution of Tdi Diesel Generator Issues + (ML20084A160)
- 05000237/LER-1976-067-01, /01T-0:on 761203,GE Informed That Current Upper Limit of 10% Power for Required Rod Worth Minimizer Operation Not Sufficiently Conservative.Procedures Revised to Include New Upper Limit + (ML20084A163)
- ML20084A166 + (ML20084A166)
- ML20084A170 + (ML20084A170)
- 05000244/LER-1976-004-03, /03L:on 760129,during Load Decrease for Shutdown, Both Control Power Fuses Blew for N42 Power Range Channel. Caused by Component Failure.Capacitor Replaced + (ML20084A174)
- ML20084A175 + (ML20084A175)
- 05000237/LER-1976-031-03, /03L-0:on 760519,during Standby Liquid Control Sys Operability Testing,Approx 700 Gallons of Sodium Pentaborate Solution Leaked Into Reactor Vessel.Caused by Inadequate Procedure.Vessel Water Discharged + (ML20084A178)
- ML20084A181 + (ML20084A181)
- ML20084A188 + (ML20084A188)
- ML20084A194 + (ML20084A194)
- 05000237/LER-1976-066, Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced + (ML20084A197)
- ML20084A200 + (ML20084A200)
- ML20084A207 + (ML20084A207)
- 05000237/LER-1976-030-03, /03L-0:on 760423,lab Analysis Showed Standby Gas Treatment Train a Iodine Removal Efficiency Below Tech Spec Limit.Caused by Deterioration of Charcoal Bed Due to High Usage.Mod Issued Installing Elapse Time Meters + (ML20084A211)
- ML20084A215 + (ML20084A215)
- ML20084A218 + (ML20084A218)
- ML20084A227 + (ML20084A227)
- ML20084A232 + (ML20084A232)
- ML20084A233 + (ML20084A233)
- ML20084A238 + (ML20084A238)
- ML20084A245 + (ML20084A245)
- 05000237/LER-1976-066-01, /01T-0:on 761113,during Maint Outage,Hpci Injection Valve M02-2301-8 Found in Closed Position W/Severed Stem.Cause Undetermined.Valve Clamped in Open Position + (ML20084A246)
- 05000237/LER-1976-029-03, /03L-0:on 760421,when Control Rod Drive R-9 Withdrawn to 02,all Rods in Relays Did Not de-energize as Required.Caused by Malfunctioning Probe Buffer Circuit Card. Card Replaced + (ML20084A249)