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On March 7, 2017, Division 2 Residual Heat … On March 7, 2017, Division 2 Residual Heat Removal (RHR) system was inoperable due to a scheduled maintenance system outage window. At 2258 (CST), Operations identified a Division 1 Unit Substation Switchgear relay was cycling, which is part of the Division 1 AC Power system. The specific relay could not be identified at the time. Division 1 AC Power systems were protected.</br>On March 8, 2017 at 1830 hours, Division 2 RHR was restored to operable status.</br>On March 9, 2017 at 0319 hours, Operations declared Division 1 Emergency Diesel Generator (EDG) inoperable due to the (identification of the) Division 1 relay as related to properly tripping non-essential loads on a bus under-voltage condition. The relay would not have actuated to trip non-essential loads. The proper tripping of non-essential loads is a requirement for Division 1 EDG.</br>The Updated Safety Analysis Report (USAR) Emergency Core Cooling Systems (ECCS) analysis specifies with the Division 1 DG failure, the remaining systems available are: Automatic Depressurization System (ADS), High Pressure Core Spray (HPCS), and 2 Low Pressure Core Injection (LPCI) systems.</br>As a result of Division 2 RHR (being) inoperable at the same time Division 1 EDG was inoperable, an unanalyzed condition existed. While Division 2 RHR was inoperable, Division 1 EDG was inoperable. Technical Specification (TS) Limiting Condition of Operation (LCO) 3.8.1, AC Sources - Operating, was not met. Condition B, One Required DG Inoperable, Required Action B.2 declares required features, (normally) supported by the inoperable DG, inoperable when the redundant required features are inoperable, with a completion time of 4 hours. The action would have required declaring Division 1 ECCS inoperable, which includes Division 1 RHR and Low Pressure Core Spray (LPCS).</br>With Division 1 EDG, Division 1 RHR, and Division 2 RHR inoperable, the station did not satisfy the USAR ECCS analysis and was in an unanalyzed condition. This condition is reportable under 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, since the condition occurred within three years of the date of discovery.</br>The NRC Resident Inspector has been notified. NRC Resident Inspector has been notified.
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09:19:00, 9 March 2017 +
On March 7, 2017, Division 2 Residual Heat … On March 7, 2017, Division 2 Residual Heat Removal (RHR) system was inoperable due to a scheduled maintenance system outage window. At 2258 (CST), Operations identified a Division 1 Unit Substation Switchgear relay was cycling, which is part of the Division 1 AC Power system. The specific relay could not be identified at the time. Division 1 AC Power systems were protected.</br>On March 8, 2017 at 1830 hours, Division 2 RHR was restored to operable status.</br>On March 9, 2017 at 0319 hours, Operations declared Division 1 Emergency Diesel Generator (EDG) inoperable due to the (identification of the) Division 1 relay as related to properly tripping non-essential loads on a bus under-voltage condition. The relay would not have actuated to trip non-essential loads. The proper tripping of non-essential loads is a requirement for Division 1 EDG.</br>The Updated Safety Analysis Report (USAR) Emergency Core Cooling Systems (ECCS) analysis specifies with the Division 1 DG failure, the remaining systems available are: Automatic Depressurization System (ADS), High Pressure Core Spray (HPCS), and 2 Low Pressure Core Injection (LPCI) systems.</br>As a result of Division 2 RHR (being) inoperable at the same time Division 1 EDG was inoperable, an unanalyzed condition existed. While Division 2 RHR was inoperable, Division 1 EDG was inoperable. Technical Specification (TS) Limiting Condition of Operation (LCO) 3.8.1, AC Sources - Operating, was not met. Condition B, One Required DG Inoperable, Required Action B.2 declares required features, (normally) supported by the inoperable DG, inoperable when the redundant required features are inoperable, with a completion time of 4 hours. The action would have required declaring Division 1 ECCS inoperable, which includes Division 1 RHR and Low Pressure Core Spray (LPCS).</br>With Division 1 EDG, Division 1 RHR, and Division 2 RHR inoperable, the station did not satisfy the USAR ECCS analysis and was in an unanalyzed condition. This condition is reportable under 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, since the condition occurred within three years of the date of discovery.</br>The NRC Resident Inspector has been notified. NRC Resident Inspector has been notified.
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