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On August 1, 2016 at 0342 EDT St. Lucie UnOn August 1, 2016 at 0342 EDT St. Lucie Unit 1 commenced a unit shutdown required by Technical Specifications due to Reactor Coolant System Pressure Boundary Leakage in excess of the allowable limit of zero leakage. The leak was initially identified on July 31, 2016 at 2115 EDT as not Pressure Boundary leakage. After further analysis, the leak was determined to be Reactor Coolant System Pressure Boundary leakage at 0123 on August 1, 2016. The leakage is estimated as less than one tenth of a gallon per minute and is not impacting the ability to shut down the unit. Additional impact of the leak is under evaluation.</br>This report is submitted in accordance with 10CFR50.72(b)(2)(i) as 'The initiation of any nuclear plant shutdown required by the plant's Technical Specifications.'</br>The location of the leak is on the Instrumentation piping welded connection at Flow Element FE-3311 attached to (the) Emergency Core Cooling System Injection header to Reactor Coolant System Loop 1A2. The leak activity is 0.167 microCuries per ml.</br>The NRC Resident Inspector has been notified.</br>* * * RETRACTION AT 1335 EDT ON 09/23/16 FROM RICHARD SCISCENTE TO JEFF HERRERA * * * </br>The purpose of this notification is to retract a previous report made on EN 52138. NRC notification was initially made as a result of a plant shutdown required by technical specifications (TS) for Reactor Coolant System (RCS) pressure boundary leakage. </br>Subsequent to the initial report, St. Lucie has determined that the RCS leakage was from a seal weld on a threaded connection that was not pressure boundary leakage. However, the leak was non-isolable and required RCS depressurization to allow immediate investigation to ensure there were no faults in a RCS component body or pipe wall.</br>The leakage was estimated to be less than one tenth of a gallon per minute and did not impact the ability to shut down the unit. No TS limits were exceeded during this event.</br>Therefore, the plant shutdown to investigate and correct leakage past the seal weld of a threaded connection does not meet the reporting requirements of 10 CFR 50.72 or 10 CFR 50.73.</br>The NRC Resident Inspector has been notified.</br>Notified the R2DO (Blamey).been notified. Notified the R2DO (Blamey).  
07:42:00, 1 August 2016  +
52,138  +
06:33:00, 1 August 2016  +
07:42:00, 1 August 2016  +
On August 1, 2016 at 0342 EDT St. Lucie UnOn August 1, 2016 at 0342 EDT St. Lucie Unit 1 commenced a unit shutdown required by Technical Specifications due to Reactor Coolant System Pressure Boundary Leakage in excess of the allowable limit of zero leakage. The leak was initially identified on July 31, 2016 at 2115 EDT as not Pressure Boundary leakage. After further analysis, the leak was determined to be Reactor Coolant System Pressure Boundary leakage at 0123 on August 1, 2016. The leakage is estimated as less than one tenth of a gallon per minute and is not impacting the ability to shut down the unit. Additional impact of the leak is under evaluation.</br>This report is submitted in accordance with 10CFR50.72(b)(2)(i) as 'The initiation of any nuclear plant shutdown required by the plant's Technical Specifications.'</br>The location of the leak is on the Instrumentation piping welded connection at Flow Element FE-3311 attached to (the) Emergency Core Cooling System Injection header to Reactor Coolant System Loop 1A2. The leak activity is 0.167 microCuries per ml.</br>The NRC Resident Inspector has been notified.</br>* * * RETRACTION AT 1335 EDT ON 09/23/16 FROM RICHARD SCISCENTE TO JEFF HERRERA * * * </br>The purpose of this notification is to retract a previous report made on EN 52138. NRC notification was initially made as a result of a plant shutdown required by technical specifications (TS) for Reactor Coolant System (RCS) pressure boundary leakage. </br>Subsequent to the initial report, St. Lucie has determined that the RCS leakage was from a seal weld on a threaded connection that was not pressure boundary leakage. However, the leak was non-isolable and required RCS depressurization to allow immediate investigation to ensure there were no faults in a RCS component body or pipe wall.</br>The leakage was estimated to be less than one tenth of a gallon per minute and did not impact the ability to shut down the unit. No TS limits were exceeded during this event.</br>Therefore, the plant shutdown to investigate and correct leakage past the seal weld of a threaded connection does not meet the reporting requirements of 10 CFR 50.72 or 10 CFR 50.73.</br>The NRC Resident Inspector has been notified.</br>Notified the R2DO (Blamey).been notified. Notified the R2DO (Blamey).  
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Plant Shutdown Due to Pressure Boundary Leakage Greater than Allowable Limit  +
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