Browse wiki

Jump to navigation Jump to search
At approximately 1203 (EDT) on June 7, 201At approximately 1203 (EDT) on June 7, 2013, Susquehanna Steam Electric Station Unit One reactor was manually scrammed during reactor startup. Pressure setpoint was being adjusted to the normal operating setpoint, from 750 psig to 934 psig, when all turbine bypass valves unexpectedly opened. Reactor Feed Pumps, Main Turbine, HPCI and RCIC tripped on the high level setpoint Level 8 (+54 inches) due to the resultant reactor level swell. The reactor operator then inserted a manual scram.</br>All control rods inserted. Reactor water level lowered to approximately -10 inches causing Level 3 (+13 inches) isolations. There were no automatic emergency core cooling system initiations. No steam relief valves opened during the event. All safety systems operated as expected. The cause of the Turbine Bypass valve opening is under investigation.</br>Unit 2 was unaffected.</br>The licensee notified the NRC Resident Inspector and will notify the Pennsylvania Emergency Management Agency. Pennsylvania Emergency Management Agency.  +
16:03:00, 7 June 2013  +
13:50:00, 7 June 2013  +
16:03:00, 7 June 2013  +
At approximately 1203 (EDT) on June 7, 201At approximately 1203 (EDT) on June 7, 2013, Susquehanna Steam Electric Station Unit One reactor was manually scrammed during reactor startup. Pressure setpoint was being adjusted to the normal operating setpoint, from 750 psig to 934 psig, when all turbine bypass valves unexpectedly opened. Reactor Feed Pumps, Main Turbine, HPCI and RCIC tripped on the high level setpoint Level 8 (+54 inches) due to the resultant reactor level swell. The reactor operator then inserted a manual scram.</br>All control rods inserted. Reactor water level lowered to approximately -10 inches causing Level 3 (+13 inches) isolations. There were no automatic emergency core cooling system initiations. No steam relief valves opened during the event. All safety systems operated as expected. The cause of the Turbine Bypass valve opening is under investigation.</br>Unit 2 was unaffected.</br>The licensee notified the NRC Resident Inspector and will notify the Pennsylvania Emergency Management Agency. Pennsylvania Emergency Management Agency.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
00:00:00, 7 June 2013  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:00:46, 2 March 2018  +
13:50:00, 7 June 2013  +
-0.0925 d (-2.22 hours, -0.0132 weeks, -0.00304 months)  +
16:03:00, 7 June 2013  +
Manual Scram Due to a Reactor Water Level Transient During Startup  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
1  +