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100  +
On 9/20/2016, a coupling sleeve on a pipe On 9/20/2016, a coupling sleeve on a pipe whip restraint located on the 119 foot elevation of the turbine building associated with Unit 2 main steam line 4 was found to be not engaged. As a result of the detached coupling, the restraint was not capable of performing its restraint function for a postulated pipe whip event on the main steam line. The coupling was reconnected on 9/20/2016, restoring its functionality. An extent of condition walkdown was subsequently performed for the other Unit 1 and Unit 2 steam line restraints and no similar issues were identified.</br>This concern did not result in any adverse effect on the radiological health and safety of the public.</br>The purpose of this whip restraint is to restrain the steam line for a postulated loss at the G-line anchor (east side of Turbine Building above the 104 foot elevation). The restraint protects the floor slab at the 104 foot elevation, which extends over the Unit 2 component cooling water heat exchangers.</br>With the detached coupling, equipment in the area may have been vulnerable to damage if a pipe whip event occurred. Further analysis is needed to conclude whether the heat exchangers and other equipment would have remained protected in such an event and whether this would have significantly affected the designed plant response to a pipe event.</br>Based on the need for further analysis, this event is being reported as an unanalyzed condition that may have significantly degraded plant safety in accordance with 10 CFR 50.72(b)(3)(ii)(B).</br>The NRC Senior Resident Inspector was notified.</br>* * * RETRACTION FROM FRANK LEE TO DONALD NORWOOD AT 1953 EST ON 11/18/2016 * * *</br>The purpose of this notification is to retract a previous report made on EN #52260, reported 9/23/2016. NRC notification was initially made as a result of a condition that required further analysis to determine whether the condition would have significantly degraded plant safety in accordance with 10 CFR 50.72(b)(3)(ii)(B).</br>Further analysis of the condition concluded that PG&E Design Class I equipment located inside the Turbine Building would have remained undamaged and capable of performing their safety functions. The Turbine Building would not have experienced failure of major structural elements or adverse impact to the overall building stability. </br>Therefore, the coupling sleeve on a pipe whip restraint located on the 119 foot elevation of the Turbine Building associated with Unit 2 main steam line 4 that was found to be not engaged did not constitute an unanalyzed condition that may have significantly degraded plant safety in accordance with 10 CFR 50.72(b)(3)(ii)(B). </br>The NRC Resident Inspector has been notified.</br>Notified R4DO (Azua)pector has been notified. Notified R4DO (Azua)  
03:47:00, 21 September 2016  +
52,260  +
20:10:00, 23 September 2016  +
03:47:00, 21 September 2016  +
On 9/20/2016, a coupling sleeve on a pipe On 9/20/2016, a coupling sleeve on a pipe whip restraint located on the 119 foot elevation of the turbine building associated with Unit 2 main steam line 4 was found to be not engaged. As a result of the detached coupling, the restraint was not capable of performing its restraint function for a postulated pipe whip event on the main steam line. The coupling was reconnected on 9/20/2016, restoring its functionality. An extent of condition walkdown was subsequently performed for the other Unit 1 and Unit 2 steam line restraints and no similar issues were identified.</br>This concern did not result in any adverse effect on the radiological health and safety of the public.</br>The purpose of this whip restraint is to restrain the steam line for a postulated loss at the G-line anchor (east side of Turbine Building above the 104 foot elevation). The restraint protects the floor slab at the 104 foot elevation, which extends over the Unit 2 component cooling water heat exchangers.</br>With the detached coupling, equipment in the area may have been vulnerable to damage if a pipe whip event occurred. Further analysis is needed to conclude whether the heat exchangers and other equipment would have remained protected in such an event and whether this would have significantly affected the designed plant response to a pipe event.</br>Based on the need for further analysis, this event is being reported as an unanalyzed condition that may have significantly degraded plant safety in accordance with 10 CFR 50.72(b)(3)(ii)(B).</br>The NRC Senior Resident Inspector was notified.</br>* * * RETRACTION FROM FRANK LEE TO DONALD NORWOOD AT 1953 EST ON 11/18/2016 * * *</br>The purpose of this notification is to retract a previous report made on EN #52260, reported 9/23/2016. NRC notification was initially made as a result of a condition that required further analysis to determine whether the condition would have significantly degraded plant safety in accordance with 10 CFR 50.72(b)(3)(ii)(B).</br>Further analysis of the condition concluded that PG&E Design Class I equipment located inside the Turbine Building would have remained undamaged and capable of performing their safety functions. The Turbine Building would not have experienced failure of major structural elements or adverse impact to the overall building stability. </br>Therefore, the coupling sleeve on a pipe whip restraint located on the 119 foot elevation of the Turbine Building associated with Unit 2 main steam line 4 that was found to be not engaged did not constitute an unanalyzed condition that may have significantly degraded plant safety in accordance with 10 CFR 50.72(b)(3)(ii)(B). </br>The NRC Resident Inspector has been notified.</br>Notified R4DO (Azua)pector has been notified. Notified R4DO (Azua)  
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100  +
00:00:00, 18 November 2016  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
05:18:28, 24 February 2020  +
20:10:00, 23 September 2016  +
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2.683 d (64.38 hours, 0.383 weeks, 0.0882 months)  +
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03:47:00, 21 September 2016  +
Steam Line Pipe Whip Restraint Coupling Sleeve Found Not Engaged  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
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