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On July 30, 2016 at 1152 hours (EDT) folloOn July 30, 2016 at 1152 hours (EDT) following a containment walkdown to investigate an increase in RCS unidentified leakage to 0.15 gpm, a leak was identified on the seal return line from 2-RC-P-1C, 'C' Reactor Coolant Pump. The source of the leakage cannot be isolated and is considered RCS pressure boundary leakage. (Technical Specification) LCO 3.4.13, RCS Operational Leakage, Condition B for the existence of pressure boundary leakage was entered. Technical Requirement TR 3.4.6, ASME Code Class 1, 2, and 3 Components is also applicable. Unit 2 is projected to be taken to Mode 5 for repair.</br>This event is reportable in accordance with 10 CFR 50.72(b)(2) for 'the initiation of any nuclear plant shutdown required by the plant's Technical Specifications' and 10 CFR 50.72(b)(3)(ii)(A) for 'any event or condition that results in the condition of the nuclear plant including its principal safety barriers, being seriously degraded.'</br>The licensee will be notifying the Louisa County Administrator and has notified the NRC Resident Inspector.d has notified the NRC Resident Inspector.  +
15:52:00, 30 July 2016  +
52,137  +
15:17:00, 30 July 2016  +
15:52:00, 30 July 2016  +
On July 30, 2016 at 1152 hours (EDT) folloOn July 30, 2016 at 1152 hours (EDT) following a containment walkdown to investigate an increase in RCS unidentified leakage to 0.15 gpm, a leak was identified on the seal return line from 2-RC-P-1C, 'C' Reactor Coolant Pump. The source of the leakage cannot be isolated and is considered RCS pressure boundary leakage. (Technical Specification) LCO 3.4.13, RCS Operational Leakage, Condition B for the existence of pressure boundary leakage was entered. Technical Requirement TR 3.4.6, ASME Code Class 1, 2, and 3 Components is also applicable. Unit 2 is projected to be taken to Mode 5 for repair.</br>This event is reportable in accordance with 10 CFR 50.72(b)(2) for 'the initiation of any nuclear plant shutdown required by the plant's Technical Specifications' and 10 CFR 50.72(b)(3)(ii)(A) for 'any event or condition that results in the condition of the nuclear plant including its principal safety barriers, being seriously degraded.'</br>The licensee will be notifying the Louisa County Administrator and has notified the NRC Resident Inspector.d has notified the NRC Resident Inspector.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
0.0133 d (0.32 hours, 0.0019 weeks, 4.38336e-4 months)  +
00:00:00, 30 July 2016  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
01:44:33, 2 March 2018  +
15:17:00, 30 July 2016  +
false  +
-0.0242 d (-0.58 hours, -0.00345 weeks, -7.94484e-4 months)  +
15:52:00, 30 July 2016  +
Technical Specification Required Shutdown Due to Unisolable Reactor Coolant System Boundary Leakage  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
2  +