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On May 20, 2014, at 0835 hours during planOn May 20, 2014, at 0835 hours during plant startup, Beaver Valley Power Station Unit 2 Operations personnel manually tripped the reactor due to meeting the pre-briefed trip criteria of 85% narrow range level on the 'A' Steam Generator. This manual trip criterion was reached after the steam generator water level began to oscillate following the start of the 'A' Condensate pump. A manual main steam line isolation was performed in order to limit reactor coolant system cool down. Plant trip response was as expected without complications, and all control rods fully inserted in the core. The plant is currently stable in Mode 3.</br>This event is reportable pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A).</br>Beaver Valley Power Station Unit 1 was not affected by this event.</br>The NRC Resident Inspector has been notified.</br>No relief or safety valves lifted during this event. The unit is maintaining primary temperature using the atmospheric steam dumps and main feedwater pumps. There is no primary to secondary leakage. The plant is in its normal shutdown electrical lineup. in its normal shutdown electrical lineup.  +
12:35:00, 20 May 2014  +
10:52:00, 20 May 2014  +
12:35:00, 20 May 2014  +
On May 20, 2014, at 0835 hours during planOn May 20, 2014, at 0835 hours during plant startup, Beaver Valley Power Station Unit 2 Operations personnel manually tripped the reactor due to meeting the pre-briefed trip criteria of 85% narrow range level on the 'A' Steam Generator. This manual trip criterion was reached after the steam generator water level began to oscillate following the start of the 'A' Condensate pump. A manual main steam line isolation was performed in order to limit reactor coolant system cool down. Plant trip response was as expected without complications, and all control rods fully inserted in the core. The plant is currently stable in Mode 3.</br>This event is reportable pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A).</br>Beaver Valley Power Station Unit 1 was not affected by this event.</br>The NRC Resident Inspector has been notified.</br>No relief or safety valves lifted during this event. The unit is maintaining primary temperature using the atmospheric steam dumps and main feedwater pumps. There is no primary to secondary leakage. The plant is in its normal shutdown electrical lineup. in its normal shutdown electrical lineup.  +
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0.00966 d (0.232 hours, 0.00138 weeks, 3.177175e-4 months)  +
00:00:00, 20 May 2014  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
22:20:05, 24 September 2017  +
10:52:00, 20 May 2014  +
-0.0717 d (-1.72 hours, -0.0102 weeks, -0.00236 months)  +
12:35:00, 20 May 2014  +
Manual Reactor Trip During Reactor Startup  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
2  +