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(The reactor automatically scrammed) on a … (The reactor automatically scrammed) on a Main Turbine Trip >27.6% rated thermal power. The main turbine trip was due to reactor high level. Post scram, reactor level decreased to approximately -26 inches. Reactor water level was restored with the condensate system.</br>Both reactor recirc pumps tripped as required on EOC RPT Logic when the main turbine tripped. Both pumps have been restarted.</br>A Group 2 isolation was received at +3 inches reactor water level with all valves closing as required.</br>Investigation as to the cause of the transient is underway.</br>All rods inserted during the scram. No relief valves actuated during the transient. Decay heat is being removed via turbine bypass valves to the main condenser. The plant is within normal shutdown temperature and pressure limits. The electrical grid is stable and the plant is in a normal shutdown electrical lineup. The Group 2 has been reset. There was no effect on Unit 1.</br>The licensee has notified the NRC Resident Inspector.nsee has notified the NRC Resident Inspector. +
07:51:00, 23 June 2009 +
05:08:00, 23 June 2009 +
07:51:00, 23 June 2009 +
(The reactor automatically scrammed) on a … (The reactor automatically scrammed) on a Main Turbine Trip >27.6% rated thermal power. The main turbine trip was due to reactor high level. Post scram, reactor level decreased to approximately -26 inches. Reactor water level was restored with the condensate system.</br>Both reactor recirc pumps tripped as required on EOC RPT Logic when the main turbine tripped. Both pumps have been restarted.</br>A Group 2 isolation was received at +3 inches reactor water level with all valves closing as required.</br>Investigation as to the cause of the transient is underway.</br>All rods inserted during the scram. No relief valves actuated during the transient. Decay heat is being removed via turbine bypass valves to the main condenser. The plant is within normal shutdown temperature and pressure limits. The electrical grid is stable and the plant is in a normal shutdown electrical lineup. The Group 2 has been reset. There was no effect on Unit 1.</br>The licensee has notified the NRC Resident Inspector.nsee has notified the NRC Resident Inspector. +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
61 +
00:00:00, 23 June 2009 +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:11:50, 2 March 2018 +
05:08:00, 23 June 2009 +
true +
-0.113 d (-2.72 hours, -0.0162 weeks, -0.00373 months) +
07:51:00, 23 June 2009 +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.