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At 0802 (CDT) on 10/12/2007 with Unit 1 atAt 0802 (CDT) on 10/12/2007 with Unit 1 at 100% power, an automatic reactor scram was received due to a turbine trip. Unit 2 and 3 were also at 100% power and were unaffected by the event. All expected PClS isolations, Group 2 (RHR Shutdown Cooling), Group 3 (RWCU), Group 6 (Ventilation), and Group 8 (TIP) were received along with the auto start of CREVs and 3 SBGT trains.</br>This event is reportable as a 4-hour and 8-hour non-emergency notification along with a 60-day written report in accordance with 10 CFR50.72(b)(2)(iv)(B), 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.73(a)(2)(iv)(A) as 'any event or condition that results in valid actuation of RPS or PCIS'.</br>All control rods fully inserted, the electrical grid is stable, the EDGs and ESF systems remain available, and decay heat is being removed via the Turbine Bypass Valves. The licensee notified the NRC Resident Inspector.</br>The cause of the turbine trip is under investigation.</br>The 1D RHR pump is OOS for planned maintenance. Isolations occurred as a result of low reactor water level +2 inches.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
13:02:00, 12 October 2007  +
43,718  +
11:07:00, 12 October 2007  +
13:02:00, 12 October 2007  +
At 0802 (CDT) on 10/12/2007 with Unit 1 atAt 0802 (CDT) on 10/12/2007 with Unit 1 at 100% power, an automatic reactor scram was received due to a turbine trip. Unit 2 and 3 were also at 100% power and were unaffected by the event. All expected PClS isolations, Group 2 (RHR Shutdown Cooling), Group 3 (RWCU), Group 6 (Ventilation), and Group 8 (TIP) were received along with the auto start of CREVs and 3 SBGT trains.</br>This event is reportable as a 4-hour and 8-hour non-emergency notification along with a 60-day written report in accordance with 10 CFR50.72(b)(2)(iv)(B), 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.73(a)(2)(iv)(A) as 'any event or condition that results in valid actuation of RPS or PCIS'.</br>All control rods fully inserted, the electrical grid is stable, the EDGs and ESF systems remain available, and decay heat is being removed via the Turbine Bypass Valves. The licensee notified the NRC Resident Inspector.</br>The cause of the turbine trip is under investigation.</br>The 1D RHR pump is OOS for planned maintenance. Isolations occurred as a result of low reactor water level +2 inches.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
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00:00:00, 12 October 2007  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:15:45, 2 March 2018  +
11:07:00, 12 October 2007  +
-0.08 d (-1.92 hours, -0.0114 weeks, -0.00263 months)  +
13:02:00, 12 October 2007  +
Automatic Reactor Scram Due to Turbine Trip  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
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