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This 60-day optional report, as allowed byThis 60-day optional report, as allowed by 10 CFR 50.73(a)(1), is being made under the reporting requirement in 10CFR50.73(a)(2)(iv)(A) to describe an unplanned, invalid actuation of specified systems, specifically the Units 2 and 3 Primary Containment Isolation Systems (PCIS).</br>On 9/18/04, at approximately 0357 hours (EDT), the 343SU offsite-power source tripped resulting in a fast transfer of expected 4 kV emergency busses to the alternate offsite power source. The fast transfer resulted in system isolations on both units due to the affect on the PCIS instrumentation logic. The system isolations are an expected occurrence for a fast transfer. The isolations involved various process lines such as Reactor Water Cleanup (RWCU) and Containment Atmospheric Control (CAC) / Containment Atmospheric Dilution (CAD). The Units 2 and 3 PCIS isolations were reset by approximately 0420 hours in accordance with procedures. All required isolation valves operated as designed.</br>The offsite power source (343SU) was lost as a result of a momentary deenergization of the 220-34 Newlinville Transmission Line to clear a ground fault. The fault was approximately 29 miles from the PBAPS site and was caused by a lightning strike to a transmission tower near the Newlinville substation. Field inspections of the 220-34 Transmission Lines and Towers were performed and it was identified that there was a flash mark on the tower insulator confirming the lightning strike. It was determined that the protective relaying for the 220-34 Newlinville Transmission Line operated as designed. The 343SU offsite power source was returned to service by approximately 2115 hours on 9/18/04. This issue has been entered into the site Corrective Action Program (CR 254392) for evaluation and implementation of further corrective actions.</br>The NRC Resident Inspector has been informed of this notification.or has been informed of this notification.  +
08:57:00, 18 September 2004  +
10:58:00, 12 November 2004  +
08:57:00, 18 September 2004  +
This 60-day optional report, as allowed byThis 60-day optional report, as allowed by 10 CFR 50.73(a)(1), is being made under the reporting requirement in 10CFR50.73(a)(2)(iv)(A) to describe an unplanned, invalid actuation of specified systems, specifically the Units 2 and 3 Primary Containment Isolation Systems (PCIS).</br>On 9/18/04, at approximately 0357 hours (EDT), the 343SU offsite-power source tripped resulting in a fast transfer of expected 4 kV emergency busses to the alternate offsite power source. The fast transfer resulted in system isolations on both units due to the affect on the PCIS instrumentation logic. The system isolations are an expected occurrence for a fast transfer. The isolations involved various process lines such as Reactor Water Cleanup (RWCU) and Containment Atmospheric Control (CAC) / Containment Atmospheric Dilution (CAD). The Units 2 and 3 PCIS isolations were reset by approximately 0420 hours in accordance with procedures. All required isolation valves operated as designed.</br>The offsite power source (343SU) was lost as a result of a momentary deenergization of the 220-34 Newlinville Transmission Line to clear a ground fault. The fault was approximately 29 miles from the PBAPS site and was caused by a lightning strike to a transmission tower near the Newlinville substation. Field inspections of the 220-34 Transmission Lines and Towers were performed and it was identified that there was a flash mark on the tower insulator confirming the lightning strike. It was determined that the protective relaying for the 220-34 Newlinville Transmission Line operated as designed. The 343SU offsite power source was returned to service by approximately 2115 hours on 9/18/04. This issue has been entered into the site Corrective Action Program (CR 254392) for evaluation and implementation of further corrective actions.</br>The NRC Resident Inspector has been informed of this notification.or has been informed of this notification.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
0.00413 d (0.0992 hours, 5.902778e-4 weeks, 1.358385e-4 months)  +, 0.00486 d (0.117 hours, 6.944444e-4 weeks, 1.5981e-4 months)  +  and 0.0245 d (0.588 hours, 0.0035 weeks, 8.047575e-4 months)  +
0  +  and 100  +
00:00:00, 12 November 2004  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:22:20, 2 March 2018  +
10:58:00, 12 November 2004  +
false  +  and true  +
false  +
55.043 d (1,321.02 hours, 7.863 weeks, 1.81 months)  +
08:57:00, 18 September 2004  +
Invalid Specified System Actuation Due to Off Site Power Source Fast Transfer  +
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2  +  and 3  +