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At 2146 hours on 05/21/04, Unit 2 entered At 2146 hours on 05/21/04, Unit 2 entered a 30 Hr. clock to Cold Shutdown (CSD) in accordance with T.S.3.0.1 due to Auxiliary Feedwater (AFW) not being in compliance for Continued Operation (JCO) SC 03-002 configuration. Auxiliary Feedwater was declared inoperable at 2146 hours. During post trip recovery, Emergency Procedure, 2-ES-0.1, directed that the six (6) AFW motor operated valves (MOVs) be checked opened after securing the AFW Pumps. This is contrary to the AFW JCO, which requires four (4) MOVs out of six (6) to be closed for AFW to remain Operable. At 0040 hours on 5/22/04 the correct valve alignment in accordance with the JCO was established and the 30 hour TS 3.0.1 clock was exited.</br>This event is reportable in accordance with 10CFR50.72(b)(3)(ii)(B); any event or condition that results in the Station being in an unanalyzed condition that significantly degrades plant safety.</br>The NRC resident has been notified.</br>The licensee found out about this event today during event investigation. See Surry Unit 2 events 40769, 40768 and 40771.</br>* * * RETRACTION FROM WOODZELL TO CROUCH ON 05/25/04 @ 2347 EDT * * *</br>The following information was received from the licensee via facsimile:</br>At 1506 hours on 5/22/04, Surry Power Station made an 8-hour Non-Emergency Notification in accordance with 10CFR50.72 (b)(3)(ii)(B) for an unanalyzed condition due to Auxiliary Feedwater (AFW) not being aligned in accordance with Justification for Continued Operation (JCO) SC 03-002 for 2 hours and 54 minutes following a reactor trip. (Event Number 40770).</br>Upon further analysis, this event was determined not to be immediately reportable. Based on calculations performed by Dominion Nuclear Safety Analysis in Engineering Transmittal ET NAF-04-0045, Rev 0, a risk-based period of time was calculated to allow operations personnel a defined period of time to realign the AFW system in accordance with this JCO. Operators must not exceed 150 hours to restore the acceptable JCO configuration during all modes where AFW is required to be operable. Since the amount of time the system was not in the JCO alignment was less than 150 hours, plant risk increase was maintained less than the limits specified in Regulatory Guide 1.177.</br>This notification is being made to retract the report made on 5/22/04 based on the above discussion. The NRC resident has been notified.</br>The NRC Headquarters Operations Officer notified R2DO (Ayres). Operations Officer notified R2DO (Ayres).  
01:46:00, 22 May 2004  +
15:06:00, 22 May 2004  +
01:46:00, 22 May 2004  +
At 2146 hours on 05/21/04, Unit 2 entered At 2146 hours on 05/21/04, Unit 2 entered a 30 Hr. clock to Cold Shutdown (CSD) in accordance with T.S.3.0.1 due to Auxiliary Feedwater (AFW) not being in compliance for Continued Operation (JCO) SC 03-002 configuration. Auxiliary Feedwater was declared inoperable at 2146 hours. During post trip recovery, Emergency Procedure, 2-ES-0.1, directed that the six (6) AFW motor operated valves (MOVs) be checked opened after securing the AFW Pumps. This is contrary to the AFW JCO, which requires four (4) MOVs out of six (6) to be closed for AFW to remain Operable. At 0040 hours on 5/22/04 the correct valve alignment in accordance with the JCO was established and the 30 hour TS 3.0.1 clock was exited.</br>This event is reportable in accordance with 10CFR50.72(b)(3)(ii)(B); any event or condition that results in the Station being in an unanalyzed condition that significantly degrades plant safety.</br>The NRC resident has been notified.</br>The licensee found out about this event today during event investigation. See Surry Unit 2 events 40769, 40768 and 40771.</br>* * * RETRACTION FROM WOODZELL TO CROUCH ON 05/25/04 @ 2347 EDT * * *</br>The following information was received from the licensee via facsimile:</br>At 1506 hours on 5/22/04, Surry Power Station made an 8-hour Non-Emergency Notification in accordance with 10CFR50.72 (b)(3)(ii)(B) for an unanalyzed condition due to Auxiliary Feedwater (AFW) not being aligned in accordance with Justification for Continued Operation (JCO) SC 03-002 for 2 hours and 54 minutes following a reactor trip. (Event Number 40770).</br>Upon further analysis, this event was determined not to be immediately reportable. Based on calculations performed by Dominion Nuclear Safety Analysis in Engineering Transmittal ET NAF-04-0045, Rev 0, a risk-based period of time was calculated to allow operations personnel a defined period of time to realign the AFW system in accordance with this JCO. Operators must not exceed 150 hours to restore the acceptable JCO configuration during all modes where AFW is required to be operable. Since the amount of time the system was not in the JCO alignment was less than 150 hours, plant risk increase was maintained less than the limits specified in Regulatory Guide 1.177.</br>This notification is being made to retract the report made on 5/22/04 based on the above discussion. The NRC resident has been notified.</br>The NRC Headquarters Operations Officer notified R2DO (Ayres). Operations Officer notified R2DO (Ayres).  
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0.0248 d (0.596 hours, 0.00355 weeks, 8.16553e-4 months)  +, 4.62963e-4 d (0.0111 hours, 6.613757e-5 weeks, 1.522e-5 months)  +, 3.472222e-4 d (0.00833 hours, 4.960317e-5 weeks, 1.1415e-5 months)  +, 0.0174 d (0.418 hours, 0.00249 weeks, 5.73033e-4 months)  +, 2.314815e-5 d (5.555556e-4 hours, 3.306878e-6 weeks, 7.61e-7 months)  +  and 0.00174 d (0.0417 hours, 2.480159e-4 weeks, 5.7075e-5 months)  +
00:00:00, 26 May 2004  +
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02:23:27, 2 March 2018  +
15:06:00, 22 May 2004  +
false  +
0.555 d (13.33 hours, 0.0793 weeks, 0.0183 months)  +
true  +
01:46:00, 22 May 2004  +
Unanalyzed Condition Due to Auxiliary Feedwater Not Being in Compliance with Justification for Continued Operation (Jco).  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
2  +