ENS 40770
ENS Event | |
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01:46 May 22, 2004 | |
Title | Unanalyzed Condition Due to Auxiliary Feedwater Not Being in Compliance with Justification for Continued Operation (Jco). |
Event Description | At 2146 hours0.0248 days <br />0.596 hours <br />0.00355 weeks <br />8.16553e-4 months <br /> on 05/21/04, Unit 2 entered a 30 Hr. clock to Cold Shutdown (CSD) in accordance with T.S.3.0.1 due to Auxiliary Feedwater (AFW) not being in compliance for Continued Operation (JCO) SC 03-002 configuration. Auxiliary Feedwater was declared inoperable at 2146 hours0.0248 days <br />0.596 hours <br />0.00355 weeks <br />8.16553e-4 months <br />. During post trip recovery, Emergency Procedure, 2-ES-0.1, directed that the six (6) AFW motor operated valves (MOVs) be checked opened after securing the AFW Pumps. This is contrary to the AFW JCO, which requires four (4) MOVs out of six (6) to be closed for AFW to remain Operable. At 0040 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> on 5/22/04 the correct valve alignment in accordance with the JCO was established and the 30 hour3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> TS 3.0.1 clock was exited.
This event is reportable in accordance with 10CFR50.72(b)(3)(ii)(B); any event or condition that results in the Station being in an unanalyzed condition that significantly degrades plant safety. The NRC resident has been notified. The licensee found out about this event today during event investigation. See Surry Unit 2 events 40769, 40768 and 40771.
The following information was received from the licensee via facsimile: At 1506 hours0.0174 days <br />0.418 hours <br />0.00249 weeks <br />5.73033e-4 months <br /> on 5/22/04, Surry Power Station made an 8-hour Non-Emergency Notification in accordance with 10CFR50.72 (b)(3)(ii)(B) for an unanalyzed condition due to Auxiliary Feedwater (AFW) not being aligned in accordance with Justification for Continued Operation (JCO) SC 03-002 for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 54 minutes following a reactor trip. (Event Number 40770). Upon further analysis, this event was determined not to be immediately reportable. Based on calculations performed by Dominion Nuclear Safety Analysis in Engineering Transmittal ET NAF-04-0045, Rev 0, a risk-based period of time was calculated to allow operations personnel a defined period of time to realign the AFW system in accordance with this JCO. Operators must not exceed 150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br /> to restore the acceptable JCO configuration during all modes where AFW is required to be operable. Since the amount of time the system was not in the JCO alignment was less than 150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br />, plant risk increase was maintained less than the limits specified in Regulatory Guide 1.177. This notification is being made to retract the report made on 5/22/04 based on the above discussion. The NRC resident has been notified. The NRC Headquarters Operations Officer notified R2DO (Ayres). |
Where | |
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Surry Virginia (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition | |
Time - Person (Reporting Time:+13.33 h0.555 days <br />0.0793 weeks <br />0.0183 months <br />) | |
Opened: | Larry Wheeler 15:06 May 22, 2004 |
NRC Officer: | John Mackinnon |
Last Updated: | May 26, 2004 |
40770 - NRC Website
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Unit 2 | |
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Reactor critical | Not Critical |
Scram | No |
Before | Hot Standby (0 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 554592021-09-13T22:22:00013 September 2021 22:22:00
[Table view]10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition of Fire Safe Shutdown Equipment ENS 544372019-12-11T18:56:00011 December 2019 18:56:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Potential Tornado Missile Vulnerabilities ENS 407702004-05-22T01:46:00022 May 2004 01:46:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition Due to Auxiliary Feedwater Not Being in Compliance with Justification for Continued Operation (Jco). ENS 403892003-12-12T16:19:00012 December 2003 16:19:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Both Trains of Auxiliary Feewater Were Declared Inoperable for One Hour and 22 Minutes. ENS 402922003-11-03T22:20:0003 November 2003 22:20:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Non-Conservatism in Design Methodology for Loss of Rcp (Reactor Coolant Pump) Seal Cooling 2021-09-13T22:22:00 | |