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Issue date | Title | |
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ML22340A160 | 30 November 2022 | Technical Specifications Bases, List of Effective Pages |
ML22340A202 | 30 November 2022 | Technical Specifications Bases, List of Effective Pages |
ML21125A576 | 19 April 2021 | 9 Technical Specification Bases, List of Effective Pages (Unit 2) |
ML21125A534 | 19 April 2021 | 0 to Updated Final Safety Analysis Report, Chapter 4, Reactor Coolant System |
ML21125A548 | 19 April 2021 | 2 to Technical Specifications Bases, List of Effective Pages (Unit 1) |
ML21077A010 | 16 March 2021 | Handout for Pre-Submittal Meeting with NRC and DC Cook Plant in March 19, 2021 |
ML17346A766 | 8 December 2017 | Enclosures 2 & 3 to AEP-NRC-2017-56 - Response to Request for Additional Information Regarding the License Amendment Request to Revise Emergency Action Levels and EAL Technical Basis Manual |
ML14357A447 | 23 April 2013 | Emergency Plan, Revision 32, Part 1 of 3 |
IR 05000315/2012003 | 2 August 2012 | IR 05000315-12-003, 05000316-12-003, 04/01/2012 - 06/30/2012, D.C. Cook Nuclear Power Plant, Units 1 & 2 |
ML11188A146 | 29 June 2011 | Transition to 10 CFR 50.48(c) - NFPA 805 Performance-Based Standard for Fire Protection for Light Water Reactor Electric Generating Plants, 2001 Edition. Without Attachments C, E, G, I & W |
ML080670419 | 7 March 2008 | CDBI Findings |
ML051440510 | 15 April 2005 | Attachment 1, Volume 8, Rev. 1, Cook Nuclear Power Plant Units 1 & 2, Improved Technical Specifications Conversion, ITS Section 3.3 - Instrumentation |
ML041200392 | 6 April 2004 | CNP Units 1 and 2 Improved Technical Specifications Conversion, Volume 14, Rev 0, ITS Section 3.9 Refueling Operations. |
ML040560523 | 17 February 2004 | Revision 4, Change 2 to PMP-2080-EPP-101, Emergency Classification. |
ML032900444 | 8 October 2003 | Transmittal of Emergency Plan Implementing Procedures |
ML032670614 | 18 September 2003 | to PMP-2080-EPP-101, Emergency Classification. |
ML031470264 | 19 April 2003 | Revised Emergency Plan Implementing Procedures. Rev 7 to PMI-2080 Through Rev 4 of PMP-2080-EPP-108 |
Information Notice 1999-14, Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick | 5 May 1999 | Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick |
NRC Generic Letter 1998-02 | 28 May 1998 | NRC Generic Letter 1998-002: Loss of Reactor Coolant Inventory and Associated Potential for Loss of Emergency Mitigation Functions While in a Shutdown Condition |
Information Notice 1997-83, Recent Events Involving Reactor Coolant System Inventory Control During Shutdown | 5 December 1997 | Recent Events Involving Reactor Coolant System Inventory Control During Shutdown |
Information Notice 1996-65, Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown | 11 December 1996 | Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown |
Information Notice 1996-56, Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power | 22 October 1996 | Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power |
ML17333A587 | 2 October 1996 | Expresses Apologies for Pages Being Omitted from Out Aep: NRC:1192D Ltr Submitted 960927 |
ML17333A593 | 27 September 1996 | Clarifies Emergency Action Level (EAL) Statement as Requested by NRC Staff on 960926 |
Information Notice 1996-42, Unexpected Opening of Multiple Safety Relief Valves | 5 August 1996 | Unexpected Opening of Multiple Safety Relief Valves |
Information Notice 1996-37, Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown | 18 June 1996 | Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown |
Information Notice 1996-05, Partial Bypass of Shutdown Cooling Flow from Reactor Vessel | 18 January 1996 | Partial Bypass of Shutdown Cooling Flow from Reactor Vessel |
ML17332A584 | 28 February 1995 | DC Cook Nuclear Plant IPE for External Events Revised Fire Pra. |
Information Notice 1994-52, Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 1 | 15 July 1994 | Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 1 |
ML17331B430 | 13 June 1994 | Rev 0 to DC Cook Nuclear Plant E-Plan Classification Vs NUMARC/NESP-007 Deviation Basis Document. |
Information Notice 1994-36, Undetected Accumulation of Gas in Reactor Coolant System | 24 May 1994 | Undetected Accumulation of Gas in Reactor Coolant System |
ML071040017 | 28 April 1994 | 59 FRN 12990, Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations |
Information Notice 1993-89, Potential Problems with BWR Level Instrumentation Backfill Modifications | 26 November 1993 | Potential Problems with BWR Level Instrumentation Backfill Modifications |
Information Notice 1993-62, Thermal Stratification of Water in BWR Reactor Vessels | 10 August 1993 | Thermal Stratification of Water in BWR Reactor Vessels |
Information Notice 1993-27, Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization | 8 April 1993 | Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization |
ML20118C013 | 1 October 1992 | Forwards Detailed Info on Level Instrumentation for ERDS, Per 920828 Discussion Re Approval Status of ERDS Data Point Library.Encl Info Includes,Rvlis,Sg Level,Pressurizer Level, Containment Sump Levels & Borated Water Storage Tank Level |
ML17334B446 | 24 September 1992 | Application for Amends to Licenses DPR-58 & DPR-74,deleting TS Table 3.6-1, Containment Isolation Valves,Per Guidance Provided in GL 91-08, Removal of Component Lists from Ts. Lists of Valves Will Be Incorporated Into Plant Procedures |
NRC Generic Letter 1992-04 | 19 August 1992 | NRC Generic Letter 1992-004 - Resolution of Issues Related to Reactor Vessel Water Level Instrumentation in BWRs Pursuant to 10 CFR 50.54(F) |
ML20101G231 | 17 June 1992 | Provides Data Point Library for DC Cook Nuclear Plant in Response to 10CFR50,App E,Section VI |
Information Notice 1992-16, Loss of Flow from the Residual Heat Removal Pump During Refueling Cavity Draindown | 25 February 1992 | Loss of Flow from the Residual Heat Removal Pump During Refueling Cavity Draindown |
ML17328A770 | 9 November 1990 | Updates 881005 Submittal Re Reg Guide 1.97.Licensee Completed All Upgrade Work Shown in Table Portion W/Listed Exceptions |
Information Notice 1990-22, Unanticipated Equipment Actuations Following Restoration of Power to Rosemount Transmitter Trip Units | 23 March 1990 | Unanticipated Equipment Actuations Following Restoration of Power to Rosemount Transmitter Trip Units |
ML17325B087 | 9 January 1989 | Forwards Response to Generic Ltr 88-17, Loss of DHR, Including Actions & Controls That Will Be Implemented Prior to Operating in Reduced Inventory Condition W/Irradiated Fuel in Reactor Vessel |
NRC-86-3095, Part 21 Rept Re Nonupper Head Injection Analog Versions of Reactor Vessel Water Level Instrumentation Sys.Initially Reported on 860109.Changes to Upgrade Steam Density Compensation Circuit Identified | 9 January 1986 | Part 21 Rept Re Nonupper Head Injection Analog Versions of Reactor Vessel Water Level Instrumentation Sys.Initially Reported on 860109.Changes to Upgrade Steam Density Compensation Circuit Identified |
IR 05000316/2004030 | 31 May 1985 | Insp Repts 50-352/85-16 & 50-353/85-04 on 850316-0430. Violation Noted:Inadequate cross-discipline Review Capability in Plant Operations Review Subcommittee Reviewing Rev 2 to Procedures Re Sodium Pentaborate Analysis |
NRC Generic Letter 1985-08 | 23 May 1985 | NRC Generic Letter 1985-008: 10 CFR 20.408 Termination Reports - Format |
NRC Generic Letter 1985-09 | 23 May 1985 | NRC Generic Letter 1985-009: Technical Specifications for Generic Letter 1983-028, Item 4.3 |
NRC Generic Letter 1985-07 | 2 May 1985 | NRC Generic Letter 1985-007: Implementation of Integrated Schedules for Plant Modifications |
IR 05000316/2004011 | 24 April 1985 | Insp Rept 50-416/85-09 on 850316-0411.Violations Noted: Steps in Sp 06-EL-1E31-M-0001 Performed Out of Sequence Resulting in ESF Containment Isolation Valve Actuation & Causing Isolation of RCIC Sys |
NRC Generic Letter 1985-02 | 17 April 1985 | NRC Generic Letter 1985-002: Staff Recommended Actions Stemming from NRC Integrated Program for the Resolution of Unresolved Safety Issues Regarding Steam Generator Tube Integrity |