Semantic search

Jump to navigation Jump to search
 Start dateReporting criterionEvent description
05000323/LER-2017-0013 October 201710 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

During an investigation of a nitrogen leak inside the Unit 2 containment, Nitrogen Accumulator Relief Valve (RV) RV-355 was found to be leaking. The leak caused the pressure in the back up nitrogen accumulator supply to Power Operated Relief Valve (PORV) PCV-455C to decrease to a level that made the PORV inoperable. Based on a review of the ti-end data for nitrogen usage in the containment, it is conservatively assumed that RV-355 had been degraded since December 1, 2016, rendering the PORV inoperable for longer than permitted by Technical Specifications.

The presumptive cause was inadequate instructions provided in plant procedures for placing a new nitrogen bottle in service. These instructions did not provide a sequence that assures system pressure transients are mitigated. This may have caused excessive pressure excursions resulting in multiple lifts of RV-355 which resulted in damage to the RV 0-ring seat and a nitrogen leak path.

Corrective actions include replacing RV-355 and revising procedures to provide instructions on placing nitrogen supply bottles in service to maintain back pressure and minimize pressure transients on the nitrogen system.

This event did not affect the health and safety of the public.

05000323/LER-2016-00130 May 2016
28 July 2016
10 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 30, 2016, at 0930 PDT, with Unit 2 in Mode 4, "Hot Shutdown," licensed operators responding to a difference greater than 12 steps between digital rod position indication (DRPI) and demand position indication in the control room, manually opened the Reactor Trip Breakers in accordance with plant procedures. The plant operators stabilized the plant and technicians identified a failure of a control rod moveable gripper fuse. At 1611 PDT, plant operators made an 8-hour, nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A). Plant technicians replaced the fuse and plant operators confirmed proper operation by performance of surveillance testing.

The cause was attributed to Surveillance Test Procedure (STP) R-1C, "Digital Rod Position Indicator Functional Test," which did not explicitly specify actions to identify improper DRPI indications prior to exceeding a 12-step difference between rod demand and rod position indication.

Corrective actions to prevent recurrence include revision of STP R-1C to include guidance regarding verification of rod motion prior to exceeding 12 steps and operator training of the changes to the procedure.

This event did not adversely affect the health and safety of the public.

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 205550001, or by e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

05000323/LER-2014-00214 August 201410 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

On August 13, 2014, while performing scheduled maintenance on Unit 2 Emergency Diesel Generator (EDG) 2-2, Diablo Canyon Power Plant (DCPP) identified a failed Inlet-to-Fuel-Header capscrew on Engine Cylinder 1L. As part of subsequent inspections to determine whether a similar condition existed on any of the other Unit 1 or Unit 2 EDGs, a degraded capscrew was identified on EDG 2-3 Cylinder 8L.

No capscrew issues were identified on the Unit 1 EDGs or on Unit 2 EDG 2-1. EDG 2-3 was declared inoperable at 1631 on August 14, 2014, resulting in two of three EDGs being inoperable at the same time, which requires ensuring at least two EDGs are operable within 2 hours, or be in Mode 3 within the following 6 hours.

Although the capscrew on EDG 2-3 was successfully replaced within 2 hours, during fuel system fill and vent following corrective maintenance, a fuel oil leak from the belt driven fuel oil booster pump occurred. Because repairs of EDG 2-3 could not be completed within the time permitted by Technical Specification 3.8.1 for two EDGs inoperable, a Unit 2 plant shutdown commenced. On August 14, 2014, at 2351 hours, Unit 2 entered Mode 3.

The cause of the failed capscrew on EDG 2-2, and the degraded capscrew on EDG 2-3, was determined to be high cycle fatigue. The cause of the fuel oil booster pump leak was determined to be a manufacturing defect combined with high seal annulus pressure during fuel oil system priming. Corrective actions include replacement of all capscrews with an improved material design, and incorporation of updated vendor guidance and updated fuel system priming instructions into station procedures.

This event did not adversely affect the health or safety of the public.

05000323/LER-2013-00510 July 201310 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

On July 10, 2013, at 09:50 PDT, while performing the periodic hot-washing of the 500 kV insulators, a flashover of the Phase A 500 kV to ground across the Phase A lightning arrestor occurred and actuated the 500 kV differential relay. The actuation of the 500 kV differential relay opened the Unit 2 generator output breakers to isolate the generator, which then actuated a turbine trip. Since Unit 2 was operating above the 50 percent power permissive, the reactor protection system initiated a Unit 2 reactor trip. All plant equipment responded as designed.

Diablo Canyon Power Plant (DCPP) staff determined the root cause of this event to be the hot-washing of the Phase A transmission line string insulators (500 kV dead-end insulators) with inadequate controls for oversight of supplemental PG&E transmission line personnel and on-line maintenance risk analysis that resulted in a conductive overspray, which induced an external arc around the lightning arrester insulation resulting in flashover. The corrective action to prevent reoccurrence involves the development and implementation of a maintenance strategy for 500 kV dead-end insulators to ensure they remain adequately contamination free, structurally sound, and minimize risk to DCPP.

There were no personnel injuries, no offsite radiological releases, and no damage to safety-related equipment associated with this condition. This condition did not have an adverse effect on the health and safety of the public.

05000323/LER-2013-0048 June 201310 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On June 8, 2013, at 08:40 PDT, with Diablo Canyon Power Plant (DCPP) Unit 2 in Mode 1 at 100 percent power, Emergency Diesel Generator (EDG) 2-3 failed to complete a scheduled surveillance run. Cyclic fatigue failure of a wire lug in the EDG 2-3 current differential protection circuit caused an automatic EDG shut down 21 hours and 42 minutes into the 24-hour load run. DCPP determined the last time EDG 2-3 would have been able to complete its 24-hour surveillance run was greater than the technical specification allowed outage time. Additionally, during the time that EDG 2-3 was unable to complete its load run, EDGs 2-1 and 2-2 also had been declared inoperable on several occasions.

DCPP determined that a vibrating terminal block cover induced cyclical fatigue in the wire lug, causing it to fail.

DCPP replaced the broken wire lug and permanently removed the cover. Additionally, DCPP will revise a procedure to periodically inspect for wear on the wires and lugs.

This condition did not adversely affect the health and safety of the public.

05000323/LER-2013-00310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On March 18, 2013, at 09:30 PDT, following a transition from Mode 5 to Mode 4, an operator discovered that Unit 2 service air containment isolation valve (CIV) AIR-S-2-200 was open. Technical Specification (TS) 3.6.3 requires that each manual CIV be verified closed prior to entry into Mode 4, unless open under administrative controls. TS 3.0.4.a specifies that.entry into a Mode shall only be made when associated TS-required actions permit continued operation in that Mode for an unlimited period of time. TS 3.6.3, Required Action A.2, requires Diablo Canyon Power Plant (DCPP) to verify containment Penetration 56 flow path is isolated prior to entering Mode 4 from Mode 5 for isolation devices inside containment. DCPP failed to verify the flow path was isolated prior to the Mode transition, and concluded that the transition from Mode 5 to Mode 4 with AIR S-2-200 open was a condition prohibited by TS 3.0.4.a and TS 3.6.3, and was reportable in accordance with 10 CFR 50.73(a)(2)(i)(B).

DCPP determined that a failure to properly use human performance error prevention tools and an inadequate supervisor review process for sealed component checklist completion caused the event. DCPP will revise the checklist to require independent supervisor verification that it is complete. This condition did not adversely affect the health and safety of the public.

05000323/LER-2013-00212 March 201310 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

Refueling Outage Cycle 17, Unit 2 source range (SR) instrument N-32 experienced an unexpected increase in indicated counts per second (cps). Other available SR indications showed no rise in cps. At the time, SR instrument N-31 was inoperable. Since operators considered N-32 inoperable while N-31 was already inoperable, the audible count rate in the control room was no longer reliable. DCPP determined this condition constituted a loss of a safety function required to maintain the reactor in a safe shutdown condition and was reportable in accordance with 10 CFR 50.73(a)(2)(v)(A).

Following a vendor failure analysis, DCPP determined that a discontinuity in the cable insulation shield caused the N-32 high count rate readings. DCPP replaced the faulted cable. This condition did not adversely affect the health and safety of the public.

05000323/LER-2013-00110 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

On February 28, 2013, at 21:54 PST, with Diablo Canyon Power Plant (DCPP) Unit 1 in Mode 1 at 100 percent deenergized, which generated a valid actuation signal to start emergency diesel generator (EDG) 2-1. The EDG did not start, as it was in manual control in preparation for planned maintenance.

The planned activity did not anticipate an actual loss of power to Bus G. Therefore, the EDG start signal was valid, and was not part of a pre-planned sequence during testing. DCPP determined this condition was reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A).

This condition was caused when technicians did not ensure all maintenance prerequisites were met prior to beginning work. DCPP determined the root cause was a lack of a formal process for evaluating the risk of outage emergent work. Additionally, maintenance leadership has not been proactive in their approach to prevent shortfalls in human performance standards and use. DCPP will revise select site procedures to include risk management when shutdown. DCPP will also perform corrective actions to address human performance shortfalls to internalize the use of error prevention tools. This condition did not adversely affect the health and safety of the public.

05000323/LER-2012-00211 October 201210 CFR 50.73(a)(2)(iv)(A), System Actuation

On October 11, 2012, at 12:08 PDT, the Diablo Canyon Power Plant (DCPP) Unit 2 500kV line differential relay actuated, resulting in a unit trip. The 500kV coupling capacitor voltage transformer (CCVT) bushing experienced a flashover to ground, resulting in a unit trip and turbine trip. With the turbine tripped and Unit 2 operating above the 50 percent power permissive, the reactor protection system initiated a reactor trip as designed. All plant equipment, including the auto-start of the auxiliary feedwater (AFW) system, responded as designed.

DCPP determined that the bushing failed because the insulator minimum creepage distance was not consistent with industry codes and standards for its operating environment. When the bushing was replaced in 2011, DCPP staff made unvalidated assumptions, and over-relied on industry experts. DCPP will move CCVT metering to an area with lower contamination levels, and reinforce expectations to review current industry codes and standards.

Additionally, an unintended AFW pump restart occurred following this event as a result of a human performance error that resulted in a procedure not being revised following a plant modification. DCPP will revise procedure supporting documents and train procedure writing staff on use of the supporting documents to identify all changes required by a plant modification.

05000323/LER-2012-00110 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On August 18, 2012, Diablo Canyon Power Plant (DCPP) Unit 2 Operations personnel discovered that the belt connecting Emergency Diesel Generator (EDG) 2-3 to its fuel oil booster pump (FOBP) was broken. DCPP operators declared EDG 2-3 inoperable, entering Technical Specification (TS) 3.8.1. On August 21, 2012, at 0330, operators declared EDG 2-3 operable after replacing both the FOBP and its drive belt. The cause analysis concluded that the belt and FOBP had failed following satisfactory perfoLtuance of a surveillance test on August 3, 2012, at 1304 PDT.

EDG 2-3 was therefore inoperable longer than allowed by TS 3.8.1.B.4, and is thus reportable under 10 CFR 50.73(a)(2)(i)(B).

During the time between August 3, 2012, at 1304 PDT, and August 21, 2012, at 0330 PDT, EDG 2-2 was declared inoperable twice for testing, but was still available. When EDG 2-2 was inoperable, DCPP Unit 2 only had one operable EDG, since the broken belt rendered EDG 2-3 inoperable. Two EDGs are required to be operable to mitigate the consequences of a design basis accident, making this situation reportable under 10 CFR 50.73(a)(2)(v)(D).

PG&E will reduce the EDG 2-3 drive belt tension specification in plant procedures pending vendor approval. PG&E will establish a periodic replacement strategy for the FOBP in lieu of the present condition-monitored replacement strategy.

05000323/LER-2011-00110 CFR 50.73(a)(2)(iv)(A), System Actuation

On March 26, 2011 at 1449 PDT operators at Diablo Canyon Power Plant (DCPP) Unit 2 manually initiated a reactor trip in response to loss of main feedwater pump 2-1. The main feedwater pump 2-1 tripped after non-radioactive water sprayed on its control console. The water spray was caused by leakage from the flange of the relief valve on the feedwater heater 2-1A condenser dump valve line. All rods fully inserted on the reactor trip. The reactor was cooled by the auxiliary feedwater system with the condenser in service. All systems performed as designed with no unexpected pressure or level transients.

Automatic main feedwater isolation, auxiliary feedwater actuation, and steam generator blowdown isolation occurred as expected.

ENS notification 46701 provided the 4-hour non-emergency event report for the manual reactor trip of DCPP Unit 2 in accordance with 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation (scram). Additionally, this notification provided the 8-hour non-emergency event report of the automatic actuation of the auxiliary feedwater system as a result of the reactor trip in accordance with 10 CFR 50.72(b)(3)(iv)(A), Specified System Actuation.

The cause of the event was determined to be a failed gasket for the relief valve due to bolt torquing practices. Corrective actions include revising DCPP's bolt torquing procedure to provide bolt torquing specifications for bolted connections.

05000323/LER-1985-027, Forwards LER 85-027-00 Re Missed Surveillance on Valve FCV-678 Due to Preventive Maint & Test Schedular Sys File Being Updated in Error.Util Reviewed Surveillance Program Improvement Action Plan at 860425 Mgt Meeting W/Nrc13 June 1986
05000275/LER-2015-0025 October 201510 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

As part of an apparent cause evaluation, Pacific Gas and Electric Company (PG&E) identified an incorrect insulation configuration, installed in 2010, on the thermal extension piping that houses the wires for the wide range (WR) reactor coolant system (RCS) resistance temperature detectors (RTDs). The insulation configuration, as installed, trapped heat inside the thermal extension piping and overheated the wires. The cause of the incorrect configuration of the insulation was insufficient guidance in the associated work package instructions.

An engineering analysis completed on October 5, 2015, determined that the eight WR RCS RTDs had either failed or were operating outside the environmental qualification temperature range. As a result, on October 5, 2015, PG&E determined that the required number of WR RTDs would not have been operable and therefore a violation of Technical Specification 3.3.3, "Post Accident Monitoring (PAM) Instrumentation," had occurred.

As part of the corrective actions, PG&E replaced all eight WR RTDs, restored the insulation per the design requirements, revised the drawings for Unit 1 WR RTDs to provide adequate level of detail, and revised the work order to include the correct drawing and level of details for proper installation of all WR RTDs. This event did not adversely affect the health or safety of the public.

05000275/LER-2015-001, Both Trains of Residual Heat Removal Inoperable Due to Circumferential Crack on a Socket Weld31 December 201410 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

On December 31, 2014, while performing a walkdown as part of a surveillance test procedure, plant personnel identified through-wall seepage in a Diablo Canyon Power Plant Unit 1 socket weld inside residual heat removal system. Subsequent cleanup of the boric acid accumulation revealed active seepage of 30 drops per minute. A visual inspection identified that the source of the seepage was a circumferential crack on the socket weld.

This is the initial Licensee Event Report (LER) for this event. Pacific Gas & Electric will submit a supplemental LER describing event cause and corrective actions no later than May 8, 2015.

This condition did not have an adverse effect on the health and safety of the public.

05000275/LER-2015-00131 December 2014
11 February 2016
10 CFR 50.73(a)(2)(v), Loss of Safety Function

On December 31, 2014, while performing a walkdown as part of a surveillance test procedure, plant personnel identified through-wall seepage in a Diablo Canyon Power Plant Unit 1 socket weld inside containment that provides a flow path to a relief valve protecting a common portion of both trains of the residual heat removal system. Subsequent cleanup of the boric acid accumulation revealed active seepage of 30 drops per minute. A visual inspection identified that the source of the seepage was a circumferential crack on the socket weld.

Pacific Gas and Electric Company determined that the root cause of the cracked socket weld was containment fan cooler unit (CFCU) vibration inducing a resonant condition in the residual heat removal piping that generated stresses above the material endurance limit of the socket weld. Corrective actions included replacing two socket welds, modifying pipe supports, and correcting the condition causing the CFCU vibrations.

This condition did not have an adverse effect on the health and safety of the public.

05000275/LER-2013-0013 January 201310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On January 3, 2013, at 19:32 PST, with Units 1 and 2 in Mode 1 and at 100 percent power, Diablo Canyon Power Plant (DCPP) determined that the Limiting Condition for Operation of Technical Specification (TS) 3.4.12, low temperature overpressure protection system, was not met during Unit 1 and Unit 2 refueling outages over the past 3 years.

Specifically, when TS 3.4.12 was applicable, DCPP operated with more than one centrifugal charging pump (CCP) capable of injecting into the reactor coolant system. DCPP determined this condition was reportable pursuant to 10 CFR 50.73(a)(2)(i)(B). The noncompliance was identified based on a Nuclear Regulatory Commission TS Interpretation letter dated January 3, 2013, to Wolf Creek Nuclear Operating Company.

DCPP concluded that it had not complied with TS 3.4.12 since it replaced the positive displacement pump (PDP) with a CCP in Unit 1 (2005) and in Unit 2 (2007).

Immediate corrective actions in response to this event included revising the affected procedures to ensure compliance with TS 3.4.12.

The apparent cause for this event includes a deficiency in DCPP's 10 CFR 50.59 procedure and human error. The procedure did not provide guidance regarding proposed design changes that may maintain the original intent but create new literal compliance issues. The human error occurred when DCPP staff interpreted the operability requirements outlined in TS 3.4.12 as being equivalent with respect to the PDP to CCP design change.

Corrective actions included revising the associated 10 CFR 50.59 procedure, revising the Current Licensing Basis Determination Procedure and providing a lessons-learned discussion to the staff.

This event did not adversely affect the health and safety of the public.

05000275/LER-2010-0029 March 201010 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

On March 9, 2010, while analyzing the consequences of a postulated sustained degraded grid voltage, Pacific Gas and Electric (PG&E) concluded both Units 1 and 2 were in an unanalyzed condition. On March 9, 2010, at 23:39 (EST), PG&E reported this unanalyzed condition to the NRC in accordance with 50.72(b)(3)(ii)(B) (reference NRC Event Notification Number 45754).

The postulated sustained degraded voltage condition could have resulted in multiple safety-related pump motors, tripping overcurrent relays. As a result, these pumps would not be immediately available to mitigate a postulated accident and is considered a safety system functional failure.

PG&E had not considered this postulated worst case degraded voltage condition credible, and had therefore not analyzed for it. As a result, technical specification (TS) surveillance requirement (SR) 3.3.5.3 values are nonconservative, and several TS Actions were not met.

The immediate compensatory measure was to raise the first level undervoltage relay setpoints on the vital buses of both Units 1 and 2, thus transferring loads to emergency diesel generators prior to tripping motors on overcurrent. PG&E will submit a license amendment request to establish conservative TS SR 3.3.5.3 undervoltage relay settings.

The apparent cause was misinterpretation of the undervoltage relay design criteria in the 1970's.

05000275/LER-2009-00229 June 200910 CFR 50.73(a)(2)(vii), Common Cause Inoperability

On June 29, 2009, at 06:47 PDT, with Unit 1 in Mode 1 (Power Operation) the Eagle 21 Protection Set II, Rack 8, alarmed in the control room due to a Loop Calculation Processor (LCP) card failure. Plant operators declared motor-driven auxiliary feedwater (AFW) Pumps 1-2 and 1-3 inoperable in accordance with TS 3.7.5 Limiting Condition for Operation (LCO).

Plant operators entered Operating Procedure (OP) Abnormal Procedure AP-5, "Malfunction of Eagle 21 Protection or Control Channel," and took manual control actions in the control room.

On June 29, 2009, at 07:14 PDT, Technical Specification (TS) 3.7.5, Condition C, was exited when the first level control valve (LCV) was placed in manual and a dedicated licensed plant operator was assigned to the AFW level controller. TS 3.7.5 LCO was exited when the second LCV was placed in manual at 07:17 PDT.

The cause of the TS 3.7.5 entry was determined to be the result of intended design response to an Eagle 21 LCP failure, i.e., to lockup the control output in a "fail-as-is" status to minimize a plant transient as a result of a single failure. On June 30, 2009, at 08:26 PDT, the failed Eagle 21 LCP card was replaced and the LCVs returned to automatic level control.

05000275/LER-1986-016, Forwards LER 86-016-01 Re Problems W/Retainer Nut Associated W/Discs in Main Steam Line Check valves.Shutte-Koerting Co Will Notify All Customers of Valves W/Similar Design Problem.Item Reportable Per Part 2112 December 1986
05000275/LER-1986-012, Forwards LER 86-012-00 Re Inoperability of Both RHR Trains & Failure to Rept Event within Time Required.Event Did Not Affect Public Health & Safety3 October 1986
05000275/LER-1985-014, Forwards LER 85-014-02 Re Reactor Trip & Safety Injection. Rev Repts Discovery of Addl Damaged Snubber Resulting from Water Hammer After Reactor Trip3 March 1987
05000275/LER-1983-014, Updated LER 83-014/01T-1:on 830526,torque Switch Binding Observed During Maint on Limitorque Operator.Caused by Excessive Size of Mounting Screw Heads.Screws Replaced1 November 1983
05000275/LER-1983-007, Updated LER 83-007/01T-1:on 830509,during Welding of Reinforcement Pad on Branch Connection to Loop C Component Cooling Water Sys,Water Leaked from Weld Area.Caused by Grinding on Fillet Overweld.Overweld Removed26 September 1983
05000275/LER-1983-006, Updated LER 83-006/01T-1:on 830510,possible Undersize Condition Discovered on Reactor Coolant Piping Weld WIB-RC-2-17 During Ultrasonic Testing.Weld Confirmed to Be Above Min Wall Requirements Mechanically13 October 1983
05000275/LER-1983-004, Updated LER 83-004/08X-1:on 830419,grinding Wheel & Rotary File Gouges Discovered on Main Coolant Sys Piping on Discharge Side of Main Coolant Pump 3.Gouges Intentionally Caused by Unknown Persons.Gouges repaired.W/840117 Ltr17 January 1984
05000275/LER-1983-002, Forwards LER 83-002/03L-014 February 1983
05000275/LER-1983-001, Forwards LER 83-001/03L-03 February 1983
05000275/LER-1982-012, Forwards LER 82-012/01T-015 December 1982
05000275/LER-1982-011, Forwards LER 82-011/03L-024 November 1982
05000275/LER-1982-010, Forwards LER 82-010/01T-016 November 1982
05000275/LER-1982-009, Forwards LER 82-009/01T-018 October 1982
05000275/LER-1982-008, Forwards LER 82-008/03L-06 July 1982
05000275/LER-1982-007, Forwards LER 82-007/03L-024 June 1982
05000275/LER-1982-005, Forwards LER 82-005/03X-17 June 1982