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 Discovered dateReporting criterionTitleEvent description
ENS 571593 June 2024 04:51:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Actuation of Emergency Feedwater SystemThe following information was provided by the licensee via phone and email: At 0051 EDT on June 3, 2024, with Unit 3 in Mode 3 at 0 percent power, an actuation of the emergency feedwater system (EFW) occurred as main steam pressure was being lowered as part of reactor coolant system (RCS) cooldown for a planned shutdown. The reason for the EFW auto-start was lowering levels in the 3A and 3B steam generators following loss of the operating main feedwater pump. The main feedwater pump automatically tripped when main steam pressure was lowered below the automatic feedwater isolation system (AFIS) actuation setpoint before AFIS channels were taken to bypass. The 3A and 3B motor driven emergency feedwater pumps automatically started as designed when the low steam generator level signal was received for the 3A and 3B steam generators. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the EFW system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 571582 June 2024 21:08:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor TripThe following information was provided by the licensee via phone and email: Surry Unit 1 reactor automatically tripped at 1708 EDT on 6/2/24 due to a turbine trip (with the reactor operating at greater than 10 percent reactor power). The turbine control system is currently under investigation. Reactor coolant temperature is being maintained via main steam dumps with main feedwater supplying the steam generators. All systems operated as required. The trip was uncomplicated and all control rods fully inserted into the core. There was no emergency core cooling system (ECCS) or auxiliary feedwater system actuation. Offsite power remains available. There is no impact to Surry Unit 2. This notification is being made pursuant to 10 CFR 50.72(b)(2)(iv)(B) for 4-hour notification of reactor protection system activation. The NRC Resident Inspector has been notified. There were no radiation releases, personnel injuries, or contamination events due to this event.
ENS 5704623 March 2024 04:04:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip

The following information was provided by the licensee via email: At 0004 EDT on March 23, 2024, with the unit in Mode 1 at 23 percent power, the reactor automatically scrammed due to high reactor pressure vessel pressure when the turbine bypass valves unexpectedly closed while attempting to lower generator MW to 55 MWe to support shutdown for a refueling outage. The scram was not complex, with systems responding normally post-scram, with the exception of the pressure control system. The transient occurred while lowering on turbine speed/load demand which caused a rise in pressure and power until the reactor protection system setpoint for reactor pressure high was exceeded and resulted in an automatic reactor scram. The plant was preparing to shut down for a refueling outage when the trip occurred. Operations responded and stabilized the plant. Reactor water level is being maintained at normal level. Decay heat is being removed by the main steam system to the main condenser using manual operation of the turbine bypass valves. All control rods inserted into the core. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CPR 50.72(b)(2)(iv)(B). Additionally, received expected (primary containment) isolations for Level 3: Group 13 drywell sumps, Group 15 (traverse in-core probe) TlPs (which was already isolated) and Group 4 (residual heat removal - shutdown cooling) RHR-SDC (which was already isolated). The primary containment isolation event is being reported under 10 CFR 50.72(b)(3)(iv)(A). Also, due to the main turbine bypass valves unexpectedly closing, this is also being reported under 10 CFR 50.72(b)(3)(v)(D). There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 4/22/24 AT 1448 EDT FROM WHITNEY HEMINGWAY TO ADAM KOZIOL * * *

The purpose of this notification is to retract the 10 CFR 50.72(b)(3)(v)(D) reporting criteria of event notification 57046 reported on March 23,2024. Based on further evaluation, Fermi 2 has concluded that there was no event or condition that could have prevented fulfillment of a safety function that was needed to mitigate the consequence of an accident. Although discussed in Chapter 15 of the UFSAR, the turbine bypass valves do not provide a safety related function and are not credited safety related components for accident mitigation. Therefore, Fermi 2 is retracting the 10 CFR 50.72(b)(3)(v)(D) reporting criteria that was included on the March 23, 2024 event notification. Notified R3DO (Betancourt-Roldan)

ENS 5703216 March 2024 19:49:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Main Feedwater and Main Steam IsolationsThe following information was provided by the licensee via phone and email: At 1449 CDT, Waterford 3 Steam Electric Station was operating at 100 percent power when a manual reactor trip was initiated due to main feed isolation valve (FW-184B) and main steam isolation valve (MS-124B) going closed unexpectedly. Emergency feedwater (EFW) was automatically actuated. Preliminary evaluation indicates that all plant systems functioned normally after the reactor trip. The unit is currently stable in Mode 3. All control rods fully inserted as expected. This event is being reported as a 4-hour non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B) as an actuation of the reactor protection system (RPS) when the reactor is critical and as an 8-hour nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as valid actuation of the EFW system. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Decay heat is being removed through the turbine bypass valves and the atmospheric dump valve on loop '2'. There is no primary to secondary system leakage. The cause of the isolations is still being investigated.
ENS 5679013 October 2023 01:27:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor TripThe following information was provided by the licensee via email: On 10/12/23 at 2127 EDT, with the Unit 1 in Mode 1 at 100% Power, operators identified degrading condenser vacuum and manually tripped the reactor. All control rods inserted as expected. The trip was not complex, and all systems responded normally post-trip. The cause of the degraded condenser vacuum was an unexpected closure of the condenser air ejector regulator. The cause of the air ejector regulator going closed is not fully understood and is being investigated. Following the SCRAM, Operators responded and stabilized the plant. Decay heat is being removed by the Main Steam System through the Atmospheric Relief Valves (ARVs) and Auxiliary Feed Water (AFW) systems. Due to the Reactor Protection System (RPS) actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for a valid specified system actuation. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 567319 September 2023 15:43:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via email: On 9/9/23 at 1143 EDT, with the Unit 1 in Mode 1 at 100 percent power, all 4 turbine control valves closed resulting in a reactor protection system (RPS) automatic reactor trip on over temperature differential temperature. All control rods inserted as expected. The trip was not complex and all systems responded normally post-trip. The cause of the control valve closure has not been determined. Following the SCRAM, operators responded and stabilized the plant. Decay heat is being removed by the main steam system through the atmospheric relief valves and auxiliary feed water systems. Due to the RPS actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for a valid specified system actuation. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5669222 August 2023 21:24:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip and Automatic Actuation of Auxiliary Feedwater SystemThe following information was provided by the licensee via email: At 1724 EDT, on August 22, 2023, with Unit 1 in Mode 1 at 100 percent power, the reactor was manually tripped due to a failure of the non-safety heater drain pump 'B' and the failure of the non-safety condensate pump 'A' to automatically or manually start. At 1735 EDT, a fire was identified on heater drain pump 'B' and was extinguished by the onsite fire brigade at 1807 EDT. Operations responded and stabilized the plant. The trip was not complex, with all safety systems responding normally post-trip. Decay heat is being removed by the main steam system to the main condenser using the steam dumps. There was no impact to Units 2, 3, or 4. An automatic actuation of the auxiliary feedwater system (AFW) also occurred, as expected, due to lo-lo steam generator levels resulting from the reactor trip. AFW is currently controlling all steam generator levels at their normal levels. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the notification of another government agency, the Burke County Fire Department, this event is being reported as a four-hour, non-emergency notification under 10 CFR 50.72(b)(2)(xi). The Burke County Fire Department was not needed to extinguish the fire. This event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the auxiliary feedwater system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5662517 May 2023 10:39:0010 CFR 50.73(a)(1), Submit an LER60-DAY Optional Telephonic Notification for an Invalid Actuation of an Emergency AC Electrical Power SystemThe following information was provided by the licensee email: At 0339 CDT on May 17, 2023, diesel generator 3 (DG3) had an auto-start during a surveillance test of excess flow check valves in containment atmosphere instrument sensing lines. During the surveillance, workers failed to recognize residual pressure in the system from the test. Per procedure, MS-PS-47C (main steam pressure switch) was placed back in service, resulting in initiation logic for both the high pressure core spray (HPCS) system and DG3 auto-start. Because the HPCS system was tagged out of service for maintenance it did not actuate. The auto-start of DG3 was an expected response to the high drywell pressure indication. The signals cleared, and DG3 was shutdown per procedure. As indicated in 10 CFR 50.73(a)(1), in the case of an invalid actuation reported under 10 CFR 50.73(a)(2)(iv)(A), the licensee may, at its option, provide a telephonic notification to the NRC Operations Center within 60 days of discovery of the event instead of submitting a written licensee event report. This 60-day telephone notification is being made in accordance with 10 CFR 50.73(a)(1) for invalid actuations reported under 10 CFR 50.73 (a)(2)(iv)(A). This actuation was invalid since it was caused by programmatic issues in quality of procedural guidance and not the result of actual plant conditions warranting auto-start of DG3. The actuations were not initiated in response to actual plant conditions, this was not an intentional manual initiation, and there were no parameters satisfying the requirements for initiation. Therefore, this event has been determined to be an invalid actuation. Diesel generator 3 system responded as designed to the actuation signal. The HPCS system did not actuate since it was tagged out of service. There was no impact on the health and safety of the public or plant personnel. The following information is provided as specified in NUREG-1022: (a) The diesel generator 3 was actuated. (b) The actuation of DG3 was complete. (c) The DG3 train was started and functioned successfully. The NRC Resident Inspector has been notified.
ENS 564599 April 2023 04:44:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Loss of Reactor Coolant Pumps

The following information was provided by the licensee via email: The following event description is based on information currently available. If through subsequent reviews of this event additional information is identified that is pertinent to this event or alters the information being provided at this time a follow-up notification will be made via the ENS or under the reporting requirements of 10 CFR 50.73. At 2144 MST on April 8, 2023, the Unit 1 reactor automatically tripped due to the loss of reactor coolant pumps stemming from the loss of 13.8 kV power to the pumps. Prior to the reactor trip, the main turbine tripped due to a loss of hydraulic pressure. The main generator output breakers did not automatically open on the turbine trip as expected so the control room operators opened the breakers per procedural guidance. Once the breakers were opened, the two 13.8 kV electrical distribution buses failed to complete a fast bus transfer, which resulted in the loss of power to the reactor coolant pumps, initiating the reactor trip. The control room operators manually actuated a main steam isolation signal per procedure, requiring use of the atmospheric dump valves. Following the reactor trip, all control element assemblies inserted fully into the core. No automatic specified system actuation was required or occurred. No emergency plan classification was required per the Emergency Plan. Safety related buses remained powered from offsite power during the event and the offsite power grid is stable. Unit 1 is stable and in Mode 3. Decay heat is being removed by the atmospheric dump valves and the class 1E powered motor driven auxiliary feedwater pump. The loss of hydraulic pressure, the main generator output breakers failing to automatically open and the fast bus transfer not actuating are being investigated. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B). The NRC Senior Resident Inspector has been informed. Unit 2 is in a refueling outage in Mode 5 and Unit 3 is in Mode 1 at 100 percent power.

  • * * UPDATE ON 4/9/23 AT 0835 EDT FROM TANNER GOODMAN TO ADAM KOZIOL * * *

This update is being made to report the manual actuation of the B-train auxiliary feedwater pump and manual main steam isolation signal (MSIS) actuation affecting multiple main steam isolation valves (MSIVs) following the reactor trip. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B) and a specified system actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector has been informed of the update. Notified R4DO (Warnick)

  • * * UPDATE ON 5/3/23 AT 1945 EDT FROM LORRAINE WEAVER TO JOHN RUSSELL * * *

This update is intended to clarify the initial description of the event that occurred on 4/8/2023. Prior to the reactor trip, the main turbine tripped due to a loss of hydraulic pressure. The main generator output breakers did not automatically open on the turbine trip. The control room operators manually opened the breakers per procedural guidance. Once the breakers were opened, the two 13.8 kV electrical distribution buses de-energized. A fast bus transfer did not occur per design, which resulted in the loss of power to the reactor coolant pumps, initiating the reactor trip. The control room operators manually actuated a main steam isolation signal per procedure, requiring use of the atmospheric dump valves. The NRC Senior Resident Inspector has been informed of the update. Notified R4DO (Gaddy)

ENS 5641115 March 2023 03:57:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedReactor Coolant System (RCS) Boundary Degraded Condition

The following information was provided by the licensee via email: At 2257 (CDT) on 3/14/2023 during the 2R22 refueling outage on Browns Ferry Nuclear Plant Unit 2, it was determined there was RCS boundary leakage from five of eight sensing lines that pass through containment penetrations X-30 and X-34 that did not meet the requirements of Section XI, of the ASME Boiler and Pressure Vessel Code. The condition will be resolved prior to plant startup. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 03/28/2023 AT 1059 EST FROM CASEY CARTWRIGHT TO THOMAS HERRITY * * *

The following information was provided by the licensee via email: The purpose of this notification is to retract a previous Event Notification, EN 56411 reported on 3/14/23. Following the initial notification, further analysis of the condition was performed. It was determined that the leaking pipe weld was ASME Section XI Code Class 2 piping which falls under the requirements of ASME Section XI Subsection IWC and not Subsection IWB. Therefore, this condition does not represent a serious degradation of the nuclear power plant, including its principle safety barriers. Based upon the above, the leaks identified on the ASME Section XI Code Class 2 equivalent Main Steam sense lines are not reportable under 10 CFR 50.72(b)(3)(ii). Therefore, the NRC non-emergency 10 CFR 50.72(b)(3)(ii) report was not required and the NRC report 56411 can be retracted and no Licensee Event Report under 10 CFR 50.73(a)(2)(ii) is required to be submitted. Notified R2DO (Miller)

ENS 5626913 October 2022 22:48:0010 CFR 21.21(d)(3)(i), Failure to Comply or DefectPart 21 - Inadequate Torque ValuesThe following information was provided by the licensee via email: On October 13, 2022, during Refueling Outage 25, 2 bolts and 2 washers were discovered in the strainer basket upstream of the main steam stop valve in the steam line from the 'A' steam generator. It was determined that these bolts and washers were from the main steam isolation valve (MSIV) upstream of the stop valve. One bolt and one washer were also determined to be missing from the MSIV on the line from the 'B' steam generator. The MSIVs are a similar design as the Main Feedwater Isolation Valves (MFIVs). It appears that the torque values for these backseat bolts provided by the vendor weren't sufficient to prevent the bolts from coming loose. Wolf Creek Nuclear Operating Corporation personnel evaluated the condition and determined that the inadequate torque values provided by the vendor could have constituted a substantial safety hazard if left uncorrected. In particular, if bolts had come loose from the MFIVs, they could have traveled downstream to the steam generators and then challenged the integrity of steam generator tubes. The NRC Senior Resident Inspector has been notified. This is a non-emergency notification required by 10 CFR 21.21(d)(3)(i). A written notification will be provided within 30 days.
ENS 5618930 October 2022 10:53:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip and Auxiliary Feedwater System ActuationThe following information was provided by the licensee via email: At 0653 Eastern Daylight Time (EDT), with Unit 1 in Mode 1, at 16 percent power, an automatic reactor trip occurred due to an under-voltage condition on the 'A' reactor coolant pump (RCP) and the 'C' RCP. Power was lost from the 'A' auxiliary bus while performing an operating procedure to transfer power from the 'A' start-up transformer to the 'A' unit auxiliary transformer. Operations responded and stabilized the plant. Decay heat is being removed by the main steam system to the atmosphere using the steam generator power-operated relief valves. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the auxiliary feedwater system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5596425 June 2022 03:38:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram Due to Main Turbine TripThe following information was provided by the licensee via email: At 2338 EDT, on June 24, 2022, with the unit in Mode 1 at 100 percent power, the reactor automatically scrammed due to an RPS actuation following a Main Turbine Trip. The cause of the turbine trip is not known at this time. The scram was not complex, with systems responding normally post-scram. Operations responded and stabilized the plant. Reactor water level has been recovered and maintained at the normal level. Decay Heat is being removed by the Main Steam system to the main condenser using the Turbine Bypass Valves. All Control Rods inserted into the core. The transient occurred with no surveillances or activities in progress. Investigation into the cause of the Turbine Trip is in progress. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The low reactor water level caused an isolation of Primary Containment (Groups 4/13/15) as expected. The Primary Containment Isolation Event is being reported under 10 CFR 50.72(b)(3)(iv)(A). There was no impact to the health and safety of the public or plant personnel. The NRC resident has been notified.
ENS 5591024 May 2022 08:14:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Following Manual Turbine Trip from High Vibrations on Main TurbineThe following information was provided by the licensee via email: On May 24, 2022, at 0414 EDT, while rolling the Unit 1 main turbine during the Unit 1 Cycle 31 refueling outage, the Unit 1 main turbine experienced high vibrations and the main turbine was manually tripped with reactor power at 12 percent. Main turbine vibrations persisted and the reactor was manually tripped, Main Steam Stop Valves were closed, and main condenser vacuum was broken. This notification is being made in accordance with 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System (RPS) actuation as a four (4) hour report, and under 10 CFR 50.72(b)(3)(iv)(A), specified system actuation of the Auxiliary Feedwater System, as an eight (8) hour report. The DC Cook Resident NRC Inspector has been notified. Unit 1 is being supplied by offsite power. All control rods fully inserted. Both Motor Driven Auxiliary Feedwater Pumps started properly. Decay heat is being removed via Steam Generator Power Operated Relief Valves. Preliminary evaluation indicates all plant systems functioned normally following the Reactor Trip. DC Cook Unit 1 remains stable in Mode 3 while conducting the Post Trip Review. No radioactive release is in progress as a result of this event.
ENS 5586829 April 2022 08:05:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip and Auxiliary Feedwater System ActuationThe following information was provided by the licensee via email: At 0405 Eastern Daylight Time (EDT), with Unit 1 in Mode 1 at 100 percent power, the reactor was manually tripped due to degrading condenser vacuum. The trip was not complex, with all systems responding normally post-trip. The Auxiliary Feedwater System started automatically as expected. Operations responded and stabilized the plant. Decay heat is being removed by the Main Steam System to the main condenser using the turbine bypass valves. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the Auxiliary Feedwater System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: No Tech Spec limits were exceeded. Offsite power is available. The suspected cause for the loss of condenser vacuum is when performing the scheduled monthly swap of condenser vacuum pumps, a suction valve failed to shut.
ENS 557324 February 2022 22:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor ScramThe following information was provided by the licensee via email: At 1700 EST, on February 4, 2022 with the unit in Mode 1 at 58 percent power, the reactor automatically scrammed due to low Reactor water level due to a transient on the Feedwater System while preparing to shutdown for a refueling outage. The scram was not complex, with systems responding normally post-scram. Operations responded and stabilized the plant. Reactor water level has been recovered and maintained at normal level. Decay Heat is being removed by the Main Steam system to the main condenser using the Turbine Bypass Valves. All Control Rods inserted into the core. The transient occurred while in the process of removing the South Reactor Feed Pump from service. While reducing speed on the South, the North Reactor Feed Pump increased in speed and tripped on low suction. The plant was preparing to shut down for a refueling outage when the trip occurred. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, in preparation of plant shutdown, Primary Containment De-Inerting was in progress. The low Reactor water level caused an isolation of Primary Containment (Groups 4/13/15). The Primary Containment Isolation Event is being reported under 10 CFR 50.72(b)(3)(iv)(A). There was no impact to the health and safety of the public or plant personnel. The NRC resident has been notified.
ENS 5532021 June 2021 05:51:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationReactor Trip on Generator Lockout Relay TripAt 0051 CDT Braidwood Unit 1 experienced an automatic reactor trip due to a generator lockout relay trip and subsequent turbine trip and reactor trip. The cause of the generator lockout relay trip is unknown at this time and is under investigation. Numerous lightning strikes were present in the area during the time of the generator lockout relay trip. Both trains of auxiliary feedwater started automatically following the reactor trip to maintain steam generator water levels. All systems responded as expected with the exception of failure of source range nuclear instruments to automatically re-energize following the reactor trip. Both source range nuclear instruments were manually energized in accordance with station procedures. The main steam dump valves are in service to the main condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. AC power is being provided by Offsite Power with the 1B Diesel Generator in standby. 1A Diesel Generator is out of service for planned maintenance. All other safety systems are available. There is no impact to Unit 2. This report is being made per 10 CFR 50.72(b)(2)(iv)(B) for a RPS actuation, 4 hr. notification, and per 10 CFR 50.72(b)(3)(iv)(A) for an automatic actuation of the Auxiliary Feedwater system, 8 hr. notification. The NRC Resident Inspector and Illinois Emergency Management Agency have been informed.
ENS 5526519 May 2021 10:15:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor Trip Due to High Pressurizer Pressure

At 0315 MST on May 19, 2021, Unit 2 reactor automatically tripped during testing of the Plant Protection System. The Reactor Protection System actuated to trip the reactor on High Pressurizer Pressure, although no plant protection setpoints were exceeded. Main Steam Isolation Signal (MSIS), Safety Injection Actuation Signal (SIAS), and Containment Isolation Actuation Signal (CIAS) were received. No injection of water into the Reactor Coolant System occurred. Auxiliary Feedwater Actuation Signals (AFAS) 1 and 2 actuated on low Steam Generator water level post trip as designed. This event is being reported as a reactor protection system and a specified system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). Following the reactor trip, all (Control Element Assemblies) CEAs inserted fully into the core. All systems operated as expected. No emergency plan classification was required per the Emergency Plan. Safety related busses remained powered during the event from offsite power and the offsite power grid is stable. Unit 2 is stable and in Mode 3. Steam Generator heat removal is via the class 1 E powered motor driven auxiliary feedwater pump and Atmospheric Dump Valves. The NRC Senior Resident Inspector has been informed.

  • * * UPDATE ON 5/19/21 AT 1351 EDT FROM JASON HILL TO BRIAN P. SMITH * * *

The Unit 2 reactor tripped because of actual High Pressurizer Pressure that occurred as a result of a Main Steam Isolation Signal actuation. At 0337 MST, both trains of Low Pressure and High Pressure Safety Injection (LPSI and HPSI) were made inoperable when the injection valves were overridden and closed in accordance with station procedures. At 0346 MST, in accordance with station procedures, both trains of Containment Spray, LPSI, and HPSI pumps were overridden and stopped, rendering Containment Spray inoperable as well. This represents a condition that would have prevented the fulfillment of a safety function required to mitigate the consequences of an accident per 10 CFR 50.72(b)(3)(v)(D). Additionally, at the time of the Safety Injection Actuation Signal (0315 MST), both trains of Emergency Diesel Generators actuated as required and both 4160 VAC busses remained energized from off-site power. The NRC Senior Resident Inspector has been informed. Notified R4DO (Young)

  • * * UPDATE ON 7/02/21 AT 1943 EDT FROM YOLANDA GOOD TO JEFFREY WHITED * * *

The inoperability of both trains of Low Pressure and High Pressure Safety Injection (LPSI and HPSI) and both trains of Containment Spray (CS) following the Unit 2 reactor trip has been determined to be an unanalyzed condition per 10 CFR 50.72(b)(3)(ii)(B). Additionally, inoperability of both trains of HPSI resulted in a reportable condition that could prevent fulfillment of its credited safety function to maintain the reactor in a safe shutdown condition per 10 CFR 50. 72(b)(3)(v)(A). The additional reporting criteria were discovered during review of the event and corresponding safety analyses. The NRC Senior Resident Inspector has been informed. Notified R4DO (Werner)

ENS 5499613 November 2020 07:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor Scram Due to High Reactor Pressure SignalAt 0245 EST on November 13, 2020, the Limerick Unit 1 reactor automatically scrammed on a valid Reactor High Pressure signal (1096psig). The Reactor High Pressure signal was caused by the closure of the 1B Inboard Main Steam Isolation Valve (MSIV), causing reactor pressure to rise, exceeding the Reactor Protection System (RPS) setpoint of 1096psig. The shutdown was normal and the plant is stable in Hot Shutdown with normal pressure control via the Main Steam Bypass Valves to the Main Condenser and normal level control using the Feedwater System. The closure of the 1B Inboard MSIV appears to have been caused by a loss of Primary Containment Instrument Gas (PCIG) pneumatic supply to the valve. The licensee notified the NRC Resident Inspector, and will be notifying Berks, Chester, and Montgomery Counties, as well as the Pennsylvania Emergency Management Agency.
ENS 5483918 August 2020 01:13:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip Due to Rising Steam Generator LevelOn 08/17/20 at 2113 EDT, with Unit 3 in Mode 1 at approximately 92% (Rated Thermal Power) RTP, the reactor was manually tripped. This was due to a turbine runback caused by CV-3-2011, Low Pressure Feedwater Heater Bypass Control Valve, failing open, followed by rising Steam Generator (S/G) levels. Unit 3 reactor was tripped manually when the 3C S/G Level reached 78% narrow range. Unit 3 Main Steam Isolation Valves were closed manually in accordance with Emergency Operating Procedure (EOP) network due to 38 MSR Main Steam Stop valve position indication lost. All other systems operated normally. Auxiliary Feedwater initiated as designed to provide S/G water level control. EOPs have been exited and General Operating Procedures (GOPs) were entered. Unit 3 is stable in Mode 3 at normal operating temperature and pressure. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. All rods are inserted, decay heat is being removed via S/G through normal secondary systems. The plant is in normal electrical line up. Lightning strike is believed to be the initial cause of the runback.
ENS 548273 August 2020 21:59:0010 CFR 21.21(d)(3)(i), Failure to Comply or DefectPart 21 Report - Defect of Masoneilan 8012N-3C Electropneumatic PositionerThe following was received from the licensee: On August 3, 2020, Entergy Operations, Inc. (Entergy) completed an evaluation of a deviation at Waterford 3 which concluded the condition constitutes a defect pursuant to 10 CFR 21. The Waterford 3 Site Vice President was notified of the result of this evaluation on August 10, 2020. The Masoneilan 8012N-3C electropneumatic positioner installed on Emergency Feedwater Valve EFW-223A locked during as-found diagnostic testing. Failure analysis concluded that the condition was due to an internal failure of the magnet-coil assembly due to the magnet base had poor solder joints. This has been attributed to a manufacturing defect. Entergy concluded that this condition could affect the ability to properly respond to an Emergency Feedwater Actuation Signal / Main Steam Isolation Signal if present on any of the four air operated Emergency Feedwater to Steam Generator flow control valves; therefore, it could have created a substantial safety hazard. Licensees affected: Waterford. The licensee notified the NRC Resident Inspector. Notified R4DO and the Part 21 group via email.
ENS 5443711 December 2019 18:56:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionPotential Tornado Missile VulnerabilitiesOn December 11, 2019, at 1356 EST, it was concluded that certain safety-related equipment is vulnerable to design basis tornado missiles which could render the equipment inoperable and not able to perform its design function. This applies to the following Technical Specification equipment: 1. Component cooling water piping for the 'A' spent fuel cooling water system heat exchanger. This heat exchanger is vulnerable to a horizontal missile traveling through the roll-up door, which would challenge operability of the Technical Specification required component cooling system equipment. 2. All three (3) emergency service water pumps and their diesel fuel oil supply tank. The emergency service water pumps and diesel fuel oil tank are vulnerable to a horizontal missile penetrating the missile screens. 3. Certain component cooling water system pump discharge piping is vulnerable from a vertical missile penetrating the auxiliary building roof. 4. The Unit 1 auxiliary feedwater (AFW) system pumps and the pump suction and discharge piping are vulnerable to a missile traveling through the screens on the sides and roof of the main steam valve house. This vulnerability also exists for the Unit 2 AFW. This condition puts Unit 1 and 2 into Technical Specification 3.01 which requires the units to be in hot shutdown within 6 hours and in cold shutdown within the following 30 hours. The NRC Resident Inspector has been notified.
ENS 5428923 September 2019 16:06:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Lowering Steam Generator Levels

At 1106 CDT Braidwood Unit 1 experienced an automatic reactor trip due to lowering steam generator water levels following closure of the 1B steam generator feed water regulating valve.

The cause of the 1B steam generator feedwater regulating valve failing closed is unknown at this time and is under investigation.

Both trains of auxiliary feedwater started automatically following the reactor trip to maintain steam generator water levels.

All systems responded as expected with the exception of intermediate range nuclear instrument N-36 which was identified as being undercompensated following the reactor trip. Both source range nuclear instruments were manually energized in accordance with station procedures. Steam generator power operated relief valves lifted momentarily and reseated as designed in response to the secondary transient due to the reactor trip. The main steam dump valves are in service to the main condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. AC power is being provided by offsite power with the diesel generators in stand by and all safety systems available. There is no impact to Unit 2. This report is being made per 10 CFR 50.72(b)(2)(iv)(B) for a RPS actuation, 4 hour notification, and per 10 CFR 50.72(b)(3)(iv)(A) for an automatic actuation of the auxiliary feedwater system, 8 hour notification. The NRC Resident Inspector has been informed.

ENS 5422416 August 2019 15:21:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Turbine TripAt 0821 MST, on August 16, 2019, a main turbine trip occurred followed by a loss of power to all reactor coolant pumps. The Palo Verde Nuclear Generating Station (PVNGS) Unit 2 control room then received reactor protection system alarms for low departure from nucleate boiling ratio and an automatic reactor trip occurred. Following the reactor trip, auxiliary feedwater was manually started to maintain steam generator levels. A Main Steam Isolation Signal was manually initiated as directed by the Emergency Operating Procedures. Unit 2 is currently stable in Mode 3. Prior to the reactor trip, Unit 2 was operating normally at 100 percent power. No major equipment was inoperable prior to the event that contributed to the event or challenged operator response. All control element assemblies fully inserted into the core and no emergency classification was required per the PVNGS Emergency Plan. The cause of the reactor trip is under investigation. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. The NRC Resident Inspector has been informed of the Unit 2 reactor trip. Decay heat is being removed via the atmospheric steam dump valves. Units 1 and 3 were unaffected by this event.
ENS 5421111 August 2019 12:14:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Feedwater Regulating Valve MalfunctionAt 0814 EDT on 8/11/19, with Unit 2 at 83 percent power during a planned load reduction, the reactor was manually tripped due to degraded feedwater flow control to the 23 Steam Generator caused by a malfunction of the associated Feedwater Regulating Valve, 23BF19. The trip was not complex, with all systems responding normally post trip. An actuation of the Auxiliary Feedwater system occurred following the manual reactor trip as expected due to low level in the steam generators. The unit is stable in Mode 3. Decay heat is being removed by the Main Steam Dumps and Auxiliary Feedwater System. Due to the actuation of the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an eight-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Auxiliary Feedwater System. There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The licensee notified the State of New Jersey. Unit 1 remains at 100 percent power.
ENS 5412130 April 2019 11:50:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification Due to Invalid Actuation of a General Containment Isolation SignalThis 60-day telephone notification is being made in accordance with the reporting requirements specified by 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A) to describe an invalid actuation of a general containment isolation signal affecting multiple systems. On April 30, 2019, at approximately 0650 CDT, a level 2 containment isolation signal was introduced when a fuse for the Nuclear Steam Supply Shutoff System was removed for a maintenance clearance. The level 2 containment isolation signal caused a trip of the Division I DC bus back-up charger, leaving only the Division I battery to carry the DC bus. At 0707 CDT the bus was de-energized when another unrelated clearance opened the battery supply breaker to the DC bus causing another containment isolation signal. This event did not affect Shutdown Cooling or any other protected Safety Related Equipment. The containment isolation signals caused an isolation of the systems listed below. All components that were not removed from service, gagged in position, already in the expected position due to plant conditions, or de-energized due to plant condition performed as designed. Containment Isolation valves for the following systems isolated as expected: Drywell and Containment Floor Drains, Drywell and Containment Equipment Drains, Condensate Makeup, Fire Protection Water, Service Air, Instrument Air, Reactor Water Cleanup, Spent Fuel Cooling and Cleanup, Reactor Plant Component Cooling Water, Chilled Water, Reactor Recirculation, Main Steam Drains, Reactor Building Ventilation, and Fuel Building Ventilation. The licensee notified the NRC Resident Inspector.
ENS 5392310 March 2019 04:59:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Scram Resulting in Rps and Eccs ActuationAt 2259 CST on 3/9/2019, Browns Ferry Unit-3 received an automatic SCRAM on Main Generator Breaker Failure and Turbine Load Reject. Unit-3 declared a Notification of Unusual Event SU1 for loss of offsite AC power to Unit-3 specific 4kV Shutdown Boards for greater than 15 minutes. Primary Containment Isolation Systems (PCIS) Groups 1, 2, 3, 6, and 8 isolation signals were received. Upon receipt of these signals, all required components actuated as required. Main steam relief valves lifted on the initial transient. High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) initiated on low reactor water level. HPCI remains in service for reactor level and pressure control. RCIC is not in service at this time, the station is investigating low flow from the pump. All four Unit-3 Diesel Generators started and loaded as expected. Residual Heat Removal System is in service for suppression pool cooling. 4kV Station Unit Boards have been restored from the 161kV system. Actions are in progress to restore 4kV Shutdown Boards to offsite power. This event is reportable within 1 hour in accordance with 10 CFR 50.72(a)(1)(i) for declaration of the Licensees Emergency Plan. Complete as documented on EN 53922. This event requires a 4 hour report per 10 CFR 50.72(b)(2)(iv)(B), 'Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' This event also requires an 8 hour report per 10 CFR 50.72(b)(3)(iv)(A). 'Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B), (1) Reactor protection system (RPS) including: reactor scram or reactor trip, (2) General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs), (4) ECCS (Emergency Core Cooling System) for boiling water reactors (BWRs) including: core spray systems; high-pressure coolant injection system; low pressure injection function of the residual heat removal system, (5) BWR reactor core isolation cooling system; isolation condenser system; and feedwater coolant injection system, and (8) Emergency AC electrical power systems, including: Emergency diesel generators (EDGs).' The NRC resident inspector has been notified. As of the event report, the MSIVs were opened and decay heat was being removed via the bypass valves to the condenser.
ENS 5385231 January 2019 08:01:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip - Circulating Water Icing ConditionsAt 0301 (EST) on 1/31/19, with Unit 2 in Mode 1 at 100% power, the reactor was manually tripped due to icing conditions requiring the removal of 4 Circulating Water Pumps from service. The trip was not complex, with all systems responding normally post-trip. 21 CFCU (Containment Fan Cooler Unit) was inoperable prior to the event for a planned maintenance window and did not contribute to the cause of the event and did not adversely impact the plant response to the trip. An actuation of the Auxiliary Feedwater System occurred following the manual reactor trip. The reason for the Auxiliary Feed Water System auto-start was due to low level in a steam generator. Operations responded and stabilized the plant. Decay heat is being removed by the Main Steam Dumps and Auxiliary Feedwater System. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an eight hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Auxiliary Feed Water System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The icing condition was described as frazil ice. Unit-1 reduced power to 88% because one circulating water pump was shutdown.
ENS 537641 December 2018 08:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip of Unit 2 Due to a Load RejectionAt 1006 (PST), on December 1, 2018, with Unit 2 at 100 percent power, the reactor automatically tripped due to a load rejection from the 500 kV offsite electrical system. Operations responded and stabilized the plant. Decay heat is being removed by the Main Steam system to the main condenser using the steam dump valves. The cause of the load rejection is currently under investigation. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, due to the actuation of the Auxiliary Feedwater System, as expected, this event is being reported per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Senior Resident Inspector was notified. A press release is planned for this event. All control rods fully inserted and the trip was uncomplicated. There was no effect on Unit 1.
ENS 5375627 November 2018 06:00:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialEn Revision Imported Date 12/4/2018

EN Revision Text: INOPERABILITY OF EQUIPMENT FOR CONTROL OF RADIOLOGICAL RELEASE At 2130 CST on 11/27/2018, Division 1 Main Steam Positive Leakage Control System (MS-PLCS) was declared inoperable because of a leaking check valve that caused excessive cycling of the associated air compressor. Division 2 MS-PLCS had been declared inoperable on 11/27/2018 at 1400 CST when a pressure control valve in the system exceeded the maximum allowable stroke time. Because MS-PLCS supplements the isolation function of the main steam isolation valves (MSIVs) by processing fission products that could leak through the closed MSIVs, both divisions of MS-PLCS inoperable at the same time represents a condition that could prevent the fulfillment of a safety function of an SSC (Structures, Systems and Components) that is needed to control the release of radioactive material. The station diesel air compressor is available to supply backup air to the safety relief valves as required by the Technical Requirements Manual." (This is associated with operability of the safety relief valves, due to the inoperable MS-PLCS air compressor.) The unit is in a 7 day shutdown Limiting Condition for Operation (LCO), 1-TS1-18-Div 1 & 2 MSPLCS-685, for the two divisions of MS-PLCS being inoperable. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 12/03/18 AT 1551 EST FROM TIM GATES TO BETHANY CECERE * * *

This event was initially reported under 10 CFR 50.72(b)(3)(v)(C) as a condition that could have prevented the Main Steam Positive Leakage Control System (MS-PLCS) from fulfilling its safety function to control the release of radioactive material. Division I was declared inoperable due to a failed component. Division II was declared inoperable due to a pressure control valve in the system exceeding the maximum allowable time to close by 0.50 seconds. An engineering evaluation has since been performed and concluded that the 2 second maximum allowable time to close was based on the pressure control valve being classified as a rapid closure valve and was established from the original baseline data of 0.50 seconds. This baseline data is an administrative target value per the In-Service Testing Program. There are no technical specification requirements associated with the 2 second closure time. The engineering evaluation also determined that the volume of air supplied through the pressure control valve during the extra 0.50 seconds of valve closure would have an inconsequential effect on the pressure within the volume of leakage barrier between the Main Steam Isolation Valves associated with the MS-PLCS pressure control valve or have any effect on containment over-pressurization. Based on the information provided by the engineering evaluation, the Division II MS-PLCS has been declared operable-degraded non-conforming since time of initial discovery. Consequently, this event is not reportable as a condition that could have prevented the Main Steam Positive Leakage Control System (MS-PLCS) from fulfilling its safety function. The (NRC) Resident Inspector has been notified via e-mail. Notified the R4DO (Gaddy).

ENS 536434 October 2018 04:00:0010 CFR 50.72(b)(3)(iv)(A), System ActuationEn Revision Imported Date 10/22/2018

EN Revision Text: MANUAL REACTOR TRIP DURING LOW POWER PHYSICS TESTING At 0544 EDT on October 4, 2018, with Unit 1 in Mode 2 with reactor power in the intermediate range performing low power physics testing, the reactor was manually tripped due to a rod control urgent failure alarm. The trip was not complex, with all systems responding normally. Operations stabilized the plant in Mode 3. Decay heat is being removed through the main steam system. Unit 2 was not affected. There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspectors have been notified. All control rods inserted as expected. The cause of the rod control urgent failure is being investigated.

  • * * UPDATE FROM KEVIN LOWE TO DONALD NORWOOD AT 1408 EDT ON 10/19/2018 * * *

This Event Notification is being updated to clarify that the reactor was not critical when this event occurred. Therefore, the reporting requirement is changed from 10 CFR 50.72(b)(2)(iv)(B) to 10 CFR 50.72 (b)(3)(iv)(A). During Dynamic Rod Worth Measurement testing, Control Bank Charlie was inserted approximately 153 steps when the urgent failure occurred (CBC positioned at 75 steps out). Following the scram, additional analysis concluded that the reactor was subcritical when the Reactor Protection System was actuated." The licensee notified the NRC Resident Inspector. Notified the R2DO (McCoy).

ENS 5360614 September 2018 04:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to a Failure of the Steam Generator Feed Regulating ValveAt 1323 (EDT) on 9/14/18, with Unit 2 in Mode 1 at 90% power, the reactor automatically tripped due to a failure of 23BF19, 23 Steam Generator (SG) Feed Regulating Valve. The trip was not complex, with all systems responding normally post-trip. No equipment was inoperable prior to the event. An actuation of the auxiliary feedwater system occurred following the automatic reactor trip. The reason for the auxiliary feed water system auto-start was due to low level in the steam generator. Operations responded and stabilized the plant. Decay heat is being removed by the main steam dumps and auxiliary feedwater system. Unit 1 is not affected. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non- emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the auxiliary feed water system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The Lower Alloways Creek Township will be notified.
ENS 5347727 June 2018 07:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip on Low Steam Generator Water LevelThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS (Emergency Notification System) or under the reporting requirements of 10 CFR 50.73. On June 27th, 2018 at approximately 2310 Mountain Standard Time (MST), in Palo Verde Unit 3, the #1 Steam Generator Economizer valve started closing. This caused Steam Generator #1 water level to decrease. Both Feed water pumps speed increased to raise Steam Generator level. At approximately 2311 (MST), the B Main Feed water pump tripped resulting in a Reactor Power Cutback. Steam Generator #1 level continued to decrease resulting in an Automatic Reactor Trip on Low Steam Generator #1 water level. All control rods inserted to shut down the Reactor to Mode 3 using Main Feed water and Steam Bypass. Post trip Steam Generator #1 level then increased and at approximately 2316 (MST) a Main Steam Isolation Signal (MSIS) was received on high Steam Generator level. The 'B' Auxiliary Feed water pump was manually started to maintain Steam Generator water levels and Steam Generator pressure was controlled using the Atmospheric Dump Valves (ADVs). Following the reactor trip, all CEAs (Control Element Assemblies) inserted fully into the core. All systems operated as expected. No emergency plan classification was required per the Emergency Plan. Safety related busses remained powered during the event from offsite power and the offsite power grid is stable. No major equipment was inoperable prior to the event that contributed to the event or complicated operator response. Unit 3 is stable and in Mode 3 feeding Steam Generators with Auxiliary Feed water Pump 'B'. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. The NRC Resident Inspector was informed of the Unit 3 reactor trip. Unit 1and Unit 2 were unaffected by the Unit 3 trip.
ENS 534434 June 2018 14:20:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip on Lowering Steam Generator Water LevelAt 0920 CDT, Braidwood Unit 1 reactor was manually tripped due to lowering steam generator water levels following a trip of the 1C main feedwater pump. The cause of the 1C main feedwater pump trip is unknown at this time and is under investigation. Both trains of Braidwood Unit 1 auxiliary feedwater started automatically following the reactor trip to maintain steam generator water levels. All systems responded as expected. Steam generator power operated relief valves lifted momentarily and reseated as designed in response to the secondary transient due to the reactor trip. The main steam dump valves are in service to the main condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. AC power is being provided by offsite power with the diesel generators in standby and all safety systems available. There is no impact to Unit 2. This report is being made per 10CFR50.72(b)(2)(iv)(B) for a RPS actuation, 4-hr. notification, and per 10CFR50.72(b)(3)(iv)(A) for an automatic actuation of the auxiliary feedwater system, 8-hr. notification. All rods inserted into the core during the trip. Concerning the relief valves momentarily lifting and reseating, there is no known primary-to-secondary leakage. The licensee has notified the NRC Resident Inspector.
ENS 533877 May 2018 07:36:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Rx Trip Due to High-High Level in Moisture Separator Drain TankOn May 7, 2018 at 0336 (EDT), DC Cook Unit 2 Reactor was manually tripped due to a high-high level experienced in the East Moisture Separator Drain Tank (MSDT) of the Moisture Separator Reheater (MSR). This notification is being made in accordance with 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System (RPS) actuation as a four (4) hour report, and under 10 CFR 50.72(b)(3)(iv)(A), specified system actuation of the Auxiliary Feedwater System, as an eight (8) hour report. The NRC Resident Inspector has been notified. Unit 2 is being supplied by offsite power. All control rods fully inserted. All Aux Feedwater Pumps started properly. Decay heat is being removed via the Steam Generator Power Operated Relief Valves following Main Steam Stop Valve closure at 0431 due to a slow RCS (Reactor Coolant System) cooldown. Preliminary evaluation indicates all plant systems functioned normally following the Reactor Trip. DC Cook Unit 2 remains stable in Mode 3 while conducting the Post Trip Review. No radioactive release is in progress as a result of this event.
ENS 533867 May 2018 07:25:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor TripThis 4 and 8 hour notification is being made to report that Salem Unit 2 initiated a manual reactor trip and subsequent automatic Auxiliary Feedwater system actuation. The trip was initiated due to a 21 Reactor Coolant Pump reaching its procedural limit for motor winding temperature of 302F. Salem Unit 2 is currently stable in Mode 3. Reactor Coolant system pressure is 2235 PSIG and Reactor Coolant System temperature is 547 F with decay heat removal via the Main Steam Dump and Auxiliary Feedwater Systems. Unit 2 has no active shutdown technical specification action statements in effect. All control rods inserted on the reactor trip. All ECCS (emergency core cooling systems) and ESF (emergency safety function) systems functioned as expected. No safety related equipment or major secondary equipment was tagged for maintenance prior to this event. No personnel were injured during this event. The NRC Resident Inspector was notified. The Lower Alloways Creek Township will be notified.
ENS 5337130 April 2018 16:24:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Following Turbine TripAt 1124 CDT, Braidwood Unit 1 experienced an automatic Reactor Trip. The cause of the Reactor Trip was a Turbine Trip with reactor power greater than P-8. The turbine trip was actuated as a result of a Turbine Motoring Generator Trip. The cause of the generator trip is unknown at this time and is under investigation. After the Reactor Trip occurred, the 1A Auxiliary Feedwater pump was manually started to provide feedwater flow to all four steam generators. The 1A Auxiliary Feedwater pump was subsequently secured and placed in standby when the Startup Feedwater pump was placed in service. Train A Main Control Room Ventilation Filtration system shifted to Makeup Mode due to a spurious actuation signal. No secondary relief valves lifted and no secondary steam was released as a result of the Reactor Trip. The Main Steam dump valves are in service to the Main Condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. AC power is being provided by Offsite Power with the Diesel Generators in standby and all safety systems available. There is no impact to Unit 2. This report is being made per 10 CFR 50.72(b)(2)(iv)(B) for a RPS actuation, 4-hr notification, and per 10 CFR 50.72(b)(3)(iv)(A) for a manual actuation of the Auxiliary Feedwater system, 8-hr notification. The licensee notified the NRC Resident Inspector and Illinois Emergency Management Agency.
ENS 5332913 April 2018 06:27:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip Following Main Feedwater Control ProblemOn 4/13/2018 at 0227 (EDT), the Oconee Unit 1 Reactor was manually tripped from 24 percent power due to the inability to control main feedwater flow through the Main Feedwater Control Valves using the Integrated Control System. Due to the RPS actuation while critical, this event is being reported as a 4-hour Non-Emergency per 10 CFR 50.72(b)(2)(iv)(B). Following the reactor trip, multiple Main Steam Relief Valves failed to reseat at the expected pressure. Using procedure guidance, Main Steam Pressure was lowered by 115 psig, resulting in the closing of all Main Steam Relief Valves. All other post-trip conditions are normal and all other systems performed as expected. Unit 1 is currently in Mode 3 and stable. Decay heat is being removed by the steam generators discharging steam to the main condenser using the turbine bypass valves. Units 2 and 3 are not affected by the Unit 1 reactor trip. The licensee notified the NRC Resident Inspector.
ENS 5326918 March 2018 16:58:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram Due to Turbine Control Valve ClosureAt 1158 CDT on March 18, 2018, the Unit 1 reactor automatically scrammed due to a Reactor Protection System (RPS) signal generated from High Reactor Steam Dome Pressure in response to Turbine Control Valve Closure. The reactor had been operating at 100 percent power. Investigation is in progress. All control rods fully inserted into the core. Main Steam Isolation Valves remained open with Main Steam Relief Valves (MSRVs) operating on the initial transient as expected. Main Turbine Bypass Valves are currently controlling reactor pressure. Reactor Feedwater pumps remained in service to control reactor water level. Primary Containment Isolation Signals Groups 2, 3, 6, and 8 containment isolation and initiation signals were received. Upon receipt of these signals all required components actuated as required. All safety system operated as expected. At no time was public health and safety at risk. This event is reportable within 4 hours per 10 CFR 50.72(b)(2)(iv)(B) 'any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' It is also reportable within 8 hours per 10 CFR 50.72(b)(3)(iv)(A) 'any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) of this section, except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation' and requires an LER within 60 days per 10 CFR 50.73(a)(2)(iv)(A). The NRC Resident Inspector has been notified.
ENS 530608 November 2017 00:57:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip on Turbine Trip

On 11/7/2017 at 1957 (EST), VC Summer Nuclear Station automatically tripped due to a turbine trip. The cause of the turbine trip is under investigation at this time. All systems responded as expected. All Control Rods fully inserted and all Emergency Feedwater pumps started as required. The plant is stable in Mode 3. This event is reportable per 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The unit is currently stable in Mode 3 with decay heat removal via the Main Steam to the Main Condenser. The NRC Resident Inspector has been notified. The licensee will notify the South Carolina State Emergency Management Division, the Fairfield, Richland, Lexington and Newberry Counties.

  • * * UPDATE FROM BETH DALICK TO VINCE KLCO ON 11/8/17 AT 1409 EST * * *

All systems responded as expected, with the exception of 'B' Steam Generator Feedwater Isolation Valve XVG1611 B-FW. This valve did not appear to automatically close and was slow to indicate closed from the Main Control Board. All Control Rods fully inserted and all Emergency Feedwater pumps started as required. The plant is stable in Mode 3. Notified the R2DO (Musser).

ENS 5293228 August 2017 12:37:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip on Turbine TripOn 8/28/2017 at 0837 (EDT), VC Summer Nuclear Station automatically tripped due to a turbine trip. The turbine trip was caused by the Main Generator Differential Lockout due to a fault on the center phase lightning arrester on the Main Transformer (XTF-001). There were no complications with the trip. All control rods fully inserted. Balance of Plant (BOP) buses automatically transferred to their alternate power source XTF 31/32. All Emergency Feedwater pumps started as required. All systems responded as required. The plant is stable in Mode 3. Station personnel are investigating the cause of the fault on the main transformer lightning arrester. This event is reportable per 10 CFR 50. 72(b)(2)(iv)(B) and 10 CFR 50. 72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. The unit is currently stable in Mode 3 with decay heat removal via the Main Steam to the Main Condenser. The licensee will inform both State and local authorities.
ENS 527958 June 2017 19:27:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Scram After Main Turbine Control Logic Loss of PowerAt 1527 hrs (EDT) on June 8, 2017, Susquehanna Steam Electric Station Unit 1 reactor automatically scrammed due to a loss of Main Turbine Electro-Hydraulic Control (EHC) logic power causing a High Flux Reactor Power RPS (Reactor Protection System) trip. All control rods (fully) inserted and both reactor recirculation pumps tripped due to reaching reactor water level 2. Reactor water level lowered to -49 inches causing Level 3 (+13 inches) and Level 2 (-38 inches) isolations. HPCI (High Pressure Coolant Injection) and RCIC (Reactor Core Isolation Cooling) automatically initiated and were overridden by control room operators after RPV (Reactor Pressure Vessel) water level was restored to the normal band with feedwater. HPCI and RCIC injected to the Reactor Coolant System during reactor level stabilization. All isolations and initiations occurred as expected. No main steam relief valves opened. Pressure was controlled via main turbine bypass valve operation. All safety systems operated as expected. Secondary Containment Zone 1, 2, and 3 differential pressure lowered to 0 inch WG (Water Gauge) due to a trip of the Reactor Building Ventilation system that resulted from Unit 1 Level 2 isolation. Differential pressure was restored to Zones 1, 2, and 3 by the initiation of Standby Gas Treatment System on the Unit 1 Level 2 initiation. Unit 1 reactor is currently stable in Mode 3. Investigation into the loss of Main Turbine EHC logic power is underway. The NRC Resident Inspector has been notified. A voluntary notification to PEMA and press release will occur. The suspected cause of the loss of power to the EHC logic circuit is ongoing maintenance on the system.
ENS 527252 May 2017 23:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Failed Reactor Coolant Pump Power TransferOn May 2nd, 2017, at 1945 EDT, Watts Bar Nuclear (WBN) Plant Unit 1 reactor was manually tripped due to a failure of the #3 Reactor Coolant Pump normal feeder breaker to close during the planned power transfer to unit power following startup. Concurrent with the reactor trip, the Auxiliary Feedwater system actuated as designed. All control and shutdown rods fully inserted. All safety systems responded as designed. The unit is currently stable in Mode 3, with decay heat removal via auxiliary feedwater and main steam dump systems. Unit 1 is in a normal shutdown electrical alignment. This reactor trip and system actuation is being reported under 10CFR 50.72(b)(3)(iv)(A) and 10CFR 50.72 (b)(2)(iv)(B). There was no effect on WBN Unit 2. The NRC Senior Resident (Inspector) has been notified.
ENS 522929 October 2016 06:54:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Following Main Generator Differential Lockout Turbine TripSurry Unit 2 reactor automatically tripped at 0254 hours on 10/09/2016, due to a Main Generator Differential Lockout Turbine Trip. The cause of the generator differential lockout is under investigation at this time. Reactor Coolant System temperature is currently being maintained at 547 degrees Fahrenheit on the main steam dump valves. All three Auxiliary Feedwater Pumps automatically started as designed on Low-Low Steam Generator Water Level following the trip. Auxiliary feedwater pumps have since been secured and Main Feedwater is in use. All systems operated as required. The source range nuclear instruments had to be manually reinstated following the reactor trip due to indications of undercompensation on Intermediate Range Nuclear Instrument channel N-36. Off site power remains available. There is no impact on Surry Unit 1. This notification is being made pursuant to 10CFR50.72(b)(2)(iv)(B) for 4-hour notification of Reactor Protection System activation and 10CFR50.72(b)(3)(iv)(A) for 8-hour notification of automatic actuation of the Auxiliary Feedwater System. The NRC Resident Inspector has been notified and is responding to the site. There were no radiation releases, personnel injuries, or contamination events due to this event. All control rods fully inserted. Secondary reliefs lifted and reseated as expected following a reactor trip from 100% power.
ENS 5221331 August 2016 19:11:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip on Low Reactor Coolant FlowThis 4-hour and 8-hour notification is being made to report that Salem Unit 2 had an unplanned automatic reactor trip and automatic actuation of the auxiliary feedwater system. The trip occurred due to the loss of the 21 reactor coolant pump (RCP) resulting in a reactor trip on low reactor coolant flow. The 21 RCP remains unavailable. The cause of the loss of the 21 reactor coolant pump is unknown at this time. All control rods inserted on the reactor trip. All emergency core cooling systems and engineered safety feature systems functioned as expected. The auxiliary feed pumps started as expected. Salem Unit 2 is currently in Mode 3. Reactor coolant system pressure is at 2235 psig and temperature is 547 degrees Fahrenheit with decay heat removal via the main steam dumps and auxiliary feedwater systems. Unit 2 has no active technical specification action statements in effect requiring a lower mode of operation due to the transient. The 21 and 22 containment fan coil units (CFCU) were out of service for surveillance testing prior to the event. There was no major secondary equipment tagged for maintenance prior to the event. There were no personnel injuries as a result of this event. Normal offsite power is available to the site. There is no effect on Unit 1. The licensee notified the NRC Resident Inspector.
ENS 5221031 August 2016 01:20:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Notice of Unusual Event - Fire in a Main Bank Transformer

A fault occurred on the unit 2 "B" main bank transformer resulting in an oil fire. The main turbine tripped resulting in a reactor trip. All control rods fully inserted and no safety or relief valves lifted. Decay heat is being removed via steam dumps to the main condenser and feeding steam generators with auxiliary feedwater. Electrical power is through the normal shutdown electrical lineup. Offsite assistance was requested from the county and off duty fire brigade members. At 2228, the fire was reported as out. Spray is continuing and a reflash watch is being set. Unit 1 continued to operate at 100% power throughout the event. Notified the DHS SWO, FEMA Ops Center, DHS NICC, FEMA National Watch Center (E-mail) and Nuclear SSA (E-mail).

  • * * UPDATE AT 2352 EDT ON 08/30/2016 FROM MICHAEL BOTTORFF TO JEFF HERRERA * * *

On August 30, 2016, at 2110 EDT, Watts Bar Nuclear Plant Unit 2 reactor tripped due to an electrical fault affecting the 2B Main Bank Transformer, resulting in a fire in the transformer. Concurrent with the reactor trip, the Auxiliary Feedwater system actuated as designed. All Control and Shutdown rods fully inserted. All safety systems responded as designed. The unit is currently stable in Mode 3, with decay heat removal via Auxiliary Feedwater and main steam dump systems. Unit 2 is in a normal shutdown electrical alignment. The fire was out at 2230 EDT. The cause of the fire is currently under investigation. The fire was reported at 2149 EDT. Local Fire Departments responded to the site as requested. The reactor trip and system actuation is being reported under 10CFR50.72(b)(3)(iv)(A) and 10CFR50.72 (b)(2)(iv)(B). There was no effect on WBN Unit 1. The NOUE was exited at 2342. The NRC Senior Resident Inspector has been notified. The Licensee notified the State of Tennessee. Notified the R2DO (Bartley), IRD MOC (Stapleton), NRR EO (Miller), DHS SWO, FEMA Ops Center, DHS NICC, FEMA National Watch Center (E-mail) and Nuclear SSA (E-mail).

ENS 5219423 August 2016 17:56:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Trip Due to a Loss of Main FeedwaterOn August 23, 2016, at 1356 EDT, Watts Bar Nuclear Plant (WBN) Unit 2 reactor was manually tripped due to a loss of main feedwater. Concurrent with the reactor trip, the Auxiliary Feedwater system actuated as designed. All control and shutdown rods fully inserted. All safety systems responded as designed. The unit is currently stable in Mode 3, with decay heat removal via Auxiliary Feedwater and main steam dump systems. Unit 2 is in a normal shutdown electrical alignment. The cause is currently under investigation. This is being reported under 10CFR 50.72(b)(3)(iv)(A) and 10CFR 50.72(b)(2)(iv)(B). There was no effect on WBN Unit 1. The NRC Senior Resident Inspector has been notified.
ENS 5212928 July 2016 09:41:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Source Range Instruments Reading Improperly During a Reactor Startup

This four and eight hour notification is being made to report that at 0541 (EDT) on 7/28/16, Salem Unit 1 initiated a shutdown to comply with Technical Specifications due to the inoperability of both source range nuclear instruments. During a reactor startup, with Unit 1 in Mode 2, both source range instruments were reading approximately one decade lower than expected compared to intermediate range and Gamma-Metric instruments and due to the proximity to the estimated critical condition. The condition could also have prevented the fulfilment of the source range instruments safety function to trip the reactor when required. Salem Unit 1 is currently stable in Mode 3. Reactor Coolant system pressure is 2235 psig and reactor coolant system temperature is 547 F with decay heat removal via the main steam dump and auxiliary feedwater systems. Unit 1 has one active shutdown tech spec action statement in effect due to the inoperability of the containment radiation monitor 1R11A. The inoperability of this radiation monitor had no effect on the event. All control rods were manually inserted to place Unit 1 in Hot Standby (Mode 3). No ECCS (emergency core cooling system) or ESF (emergency safety features) systems were required to function during this event. No major secondary equipment was tagged for maintenance prior to this event. No personnel were injured during this event. The reactor was manually shut down and a shutdown margin calculation verified sufficient margin. The licensee notified the NRC Resident Inspector and the local township.

  • * * RETRACTION FROM MATT MOG TO VINCE KLCO ON 9/26/16 AT 1519 EDT * * *

The purpose of this notification is to retract event report number 52129 made on 7/28/2016 at 0925 (EDT). Previously PSEG reported that Salem Unit 1 initiated a shutdown to comply with Technical Specifications (TS) due to the inoperability of both source range nuclear instruments. Additionally PSEG reported that the condition could have prevented the fulfillment of the safety function needed to, 'Shut down the reactor and maintain it in a safe shutdown condition.' Subsequent review identified that the condition did not meet either reporting criteria. Maintenance and Engineering evaluation of the source range nuclear instruments determined that the instruments were fully operable at the time of the event. TS 3.3.1.1, Reactor Trip Instrumentation remained met, no TS shutdown was required and the instruments were capable of performing their required function. Therefore PSEG is retracting the notifications made under 10 CFR 50.72(b)(2)(i) and 10 CFR 50.72(b)(3)(v)(A). The NRC Resident Inspector was notified of this retraction by the licensee. Notified the R1DO (Cook).

ENS 5204828 June 2016 08:23:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip on Main Generator Protection SignalThis 4 and 8 hour notification is being made to report that Salem Unit 2 suffered an unplanned automatic reactor trip and subsequent automatic auxiliary feedwater system actuation. The trip was initiated due to a Main Turbine Trip above P-9 (49% power). The Main Turbine trip was caused by a Main Generator Protection signal. Salem unit 2 is currently stable in Mode 3. Reactor coolant system pressure is 2235 psig and Reactor Coolant System temperature is 547 F with decay heat removal via the main steam dump and auxiliary feedwater systems. Unit 2 has no active shutdown tech spec action statements in effect. All control rods (fully) inserted on the reactor trip. All ECCS (Emergency Core Cooling System) and ESF (Emergency Safety Features) systems functioned as expected. No safety related equipment or major secondary equipment was tagged for maintenance prior to this event. No personnel were injured during this event. The main generator protection signal was either a ground fault or a differential current trip. The plant is in its normal shutdown electrical lineup. No safeties or relief valves lifted during this event. Unit 1 is defueled and was not affected by this event. The licensee notified the NRC Resident Inspector and will notify the Lower Alloways Creek Township.
ENS 5202620 June 2016 19:40:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripOn June 20, 2016 at 1540 EDT, Watts Bar Nuclear Plant Unit 2 reactor tripped due to (reaching the) automatic Lo-Lo steam generator trip (setpoint) on (the) #4 steam generator. Concurrent with the reactor trip the Auxiliary Feedwater system actuated as designed. All control and shutdown rods fully inserted. All safety systems responded as designed. The unit is currently stable in Mode 3, with decay heat removal via Auxiliary Feedwater and main steam dump systems. The station is in a normal shutdown electrical alignment. The cause is currently under investigation. This is being reported under 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.72 (b)(2)(iv)(B). The NRC Senior Resident has been notified. There was no effect on Unit 1.