NRC-97-0107, Application for Amend to License NPF-43,adding Special Test Exception to Allow Unit to Remain in Operational Condition 4 W/Reactor Coolant Temps Greater than 200 F,But Less than 212 F,When Performing Inservice Leak & Hydrostatic Testing

From kanterella
(Redirected from NRC-97-0107)
Jump to navigation Jump to search
Application for Amend to License NPF-43,adding Special Test Exception to Allow Unit to Remain in Operational Condition 4 W/Reactor Coolant Temps Greater than 200 F,But Less than 212 F,When Performing Inservice Leak & Hydrostatic Testing
ML20216F350
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 09/05/1997
From: Farley A
DETROIT EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20216F355 List:
References
CON-NRC-97-0107, CON-NRC-97-107 NUDOCS 9709110226
Download: ML20216F350 (12)


Text

...

~

Dehog 3,,,,,n -

y,s EdisonlEEF" c=-

i September 5,1997

{

NRC-97-0107 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555-0001

References:

1)

Fermi 2 NRC Docket No. 50 34i NRC License No. NPF-43 2)

NUREG-1433, " Standard Technical Specifications, General Electric Plants, BWR/4", Revision 1. April 1995.

Subject:

Proposed Technical Specification Change (License Amendment) for the Addition of a Special Test Exception to Allow inservice Leak and 1lydrostatic Testing to be Performed at Temperatures Greater Than 200*F but Less Than or Equal to 212*F While Considering the Reactor to Remain in OPERATIONAL CONDITION 4 Pursuant to 10CFR50.90, The Detroit Edison Company hereby proposes to amend Operating License NPF-43 for the Fermi 2 nuclear power plant by incorporating the enclosed changes into the Fermi 2 Technical Specifications. The proposed change adds a Special Test Exception to allow the unit to remain in OPERATIONAL CONDITION 4 (reactor coolant temperature less than or equal to 200*F) with actual /l/.

reacter coolant temperatures greater than 200*F, but not to exceed 212*F, when performing insenice leak and hydrostatic testing.

This proposed amendment is similar to amendments previously approved by the NRC Staff for Nine Mile Point Unit 2 in a Safety Evaluation Report (SER) dated

-November 12,1993, for Ilope Creek Generating Station in an SER dated April 18, 1994, and for Susquehanna Steam Electric Station in an SER dated February 13, khk EN41:

l[\\llkk!$$!hlh P

PDR L

s

-USNRC NRC-97-0107 Page 2 1995. This change is also consistent with the improved Technical Specifications (Reference 2) which allow performance ofinservice leak and hydrostatic testing while in Mode 4 (OPERATIONAL CONDITION 4 - COLD S!!UTDOWN"vith the reactor coolant temperaturc greater than 200*F.

Detroit Edison is requesting that this license amendment request be processed in an exigent manner in order to support an upcoming mid-cycle outage to replace a leaking fuel assembly. This outage is scheduled to begin October 3,1997, The outage will be shorter in duration and will not result in replacement of the amount of fuel typical of a refueling outage, therefore, the reactor coolant system leakage test will be performed at a higher decay heat load than is encountered following a normal refueling outage. The added temperature range allowed by the requested license amendment is necessary to support performance of the required system leakage testing on the disassembled components. provides a description and an evaluation of the proposed change.

. provides the no significant hazards consideration assessment for this change using the standards delineated in 10CFR50.92. provides the ratiouale for supporting an exigent change as described in 10CFR50.91(a)(6). provides the environmental impact analysis of this change required by 10CFR51.22. provides hand marked pages of the current Technical Specifications showing the proposed changes. A typed version of the affected Technical Specification pages with the proposed changes incorporated is also included.

Detroit Edison has evaluated the proposed Technical Specification change and has determined that no significant hazards are considered to be involved pursuant to 10CFR50.92. The Fermi 2 Onsite Review Organization has reviewed and recommends approval of the proposed changes. The Nuclear Safety Review Group has reviewed the proposed changes and concurs with the enclosed detemiinations. In accordance with 10CFR50.91, Detroit Edison is providing a copy of this letter to the State of Michigan.

In order to support the upcoming mid-cycle outage, we request approval of this license amendment request no later than October 8,1997.

1..

g i

- IJSNRC

~1 NRC-97-0107L

.Page 3!

4

-There are no commitments being made in this letter. -

- Please. contact Mr. Norman K. Peterson at (313) 586-4258 if you have any questions regarding this submittal.

Sincerely, 9

s

' Anth'ony

  1. arley, Jr.

President & COO -

Enclosures cc: A.' B.' Beach G. A. liarris M. J. Jordan -

A. J. _ Kugler J. R. Padgett Supervisor, Electric Operators, Michigan Public Senice Commission i

l

i.-

r_

.USNRC _

NRC-97-0107-Page 4 E

I, ANTIIONY F. EARLEY, JR. do hereby affirm that the foregoing statements are based on facts and circumstances that are true and accurate to the best of my-knowledge and belief.

)

/)f ti:L r

ANTHONY IMXRlfY, JR.

d President & COO On this 8

day of

.1997 before me personally

/

appeared Anthony F. Earley, Jr. being first duly sworn and says that he executed the foregoing as his free act and deed.

_$ Y c.

Notary Public I

SERNA0ETTE E.WLSON

% Putne, Wayne County, MI My Commission Expres Dec.7,2001 1l-wi w

.r Enclosure I to NRC 97-0107 Page1 ENCLOSUREI MCRIPTION AND EVALUATION OF TIIE REQUESTED REYlSION TO Tile TECIINICAL SPECIFICATIONS:

Addition of a Special Test Exception to Allow Inservice Leak and liydrostatic Testing to be Performed at Temperatures Greater Than 200*F but Less Than or Egaal to 212'F While Considering the Reactor to Remain in OPERATIONAL CONDITION 4 DESCRIPTION OF CIIANGE:

This proposed change adds a Special Test Exception,3/4.10.7," Inservice I eak and Ilydrostatic Testing," to allow the performance of pressure testing at a reactor coolant temperature of greater than 200'F but less than or equal to 212*F while considering the plant to remain in OPERATIONAL CONDITION 4. This Special Test Exception will relax the Primary Containment Integrity requirements normally associated with reactor coolant temperatures greater than 200*F, thus allowing less restricted access to the Reactor Pressure Vessel (RPV) head area of primary containment for the performance of required inspections. This Special Test Exception however, will require that the OPERATIONAL CONDITION 3 Technical Specification requirements for Secondary Containment Isolation, Secondary Containment Integrity, Secondary Containment Automatic isolation Dampers, and Standby Gas Treatment System (SGTS) OPERABILITY be met.

This change includes the associ,ated revisions to the Index, the Table 1.2,

" OPERATIONAL CONDITIONS" definition of OPERATIONAL CONDITION 4, and the Bases for Emergency Core Cooling Systems (ECCS) and Special Test Exceptions, to support incorporation of the proposed Special Test Exception. The hand-marked current Technical Specification pages showing the proposed changes are attached.

EVALUATION:

Inservice leak and hydrostatic testing required by Section XI of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code is perfonned following a refueling outage or other activity which has resulted in the reactor coolmt system being breached. The minimum temperatures (at the required pressures) allowed for these t sts are determined from the RPV pressure and temperature (P/f) limits required by Limiting Condition for Operation (LCO) 3.4.6,

" Reactor Coolant System Pressureffemperature Limits." These limits are

9 i

- Enclosure 1 to NRC 97-0107 Page 2 conservatively based on the fmeture toughness of the reactor vessel, taking into account anticipated vessel neutron fluence.

Allowing the reactor to be considered to rem,:in in OPERATIONAL CONDITION 4 during inservice leak and hydrostatic tein;;, when the reactor coolant temperature is greater than 200*F, but less than or equal to 212'F, is an exception to the OPERATIONAL CONDITION 3 requirements for Primary Containment Integrity and the required full complement of redundant Eugency Core Cooling Systems -

(ECCS) associated with operation above 200*F. Because inservice leak and hydrostatic tests will be performed water solid or nearly water solid, at less than cr equal to 212'F, and at relatively low decay heat values in comparison to those assumed in the safety analyses, the stored energy in the reactor core and coolant will be very low. Uader these conditions, the potential for failed fuel with a s?> sequent increase in reactor coolant activity to above the LCO 3.4.5," Reactor Coolant System Specific Activity" limits will be minimized. The secondary containment, including automatic isolation dampers, and the SGTS will be OPERABLE and capable of handling airborne radioactivity from leaks that could occur during the perfbrmance ofinservice leak. hydrostatic testing.

Airbome activity will not be significant in the event of a leak because the reactor coolant temperature will be limited to 212*F and therefore, little or no flashing of reactor coolant will occur. Requiring Secondary Containment Integrity and the secondary containment related systems to remain OPERABLE will ensure that potential airhorne radiation from leaks will be filtered through the SGTS, and thus will limit radiation releases to the environment. The required pressure testing conditions ensure that the consequences of a steam or water leak will be conservatively bounded by the consequences of the main steam line break outside of primary containment analysis described in Section 15.6.4 of the Lpdated Final Safety Analysis Report (UFSAR). Therefore, these requirements will conservatively limit radiation releases to the environment.

Large primary system leaks will result in the reactor vessel rapidly depressurizing, allowing the low pressure ECCS systems to operate. The capability of the low

- pressure coolant injection and core spray subsystems, as required in OPERATIONAL CONDITION 4 by LCO 3.5.2,"ECCS-Shutdown," will be more than adequate to maintain the core flooded under this relatively low decay heat load condition. Small system leaks will be detected by leakage inspections before any

- sigaificant inventory loss can occur,

- The protection prov'ded by the existing OPERATIONAL CONDITION 4 Technical Specifications, in conjunction with the OPERATIONAL CONDITION 3 secondary containment operability requirements imposed by this Special Test Exception, will

Li

. i.

. Enclosure I to :

NRC-97-0107 --

Page 3 _

ensure plant safety during the performance ofinservice leak and hydrostatic tests and ?

would ensure that the plant resporJs appropriately during accident conditions,--

.should they occur. Therefore, the requested changes can be implemented without endangering the health and safety of the public.

4 4

4

-t.-'

'l i

4 4

1 V

i -

d 4

t 4

J 4

1 m-er.

v y-*%

n e

y-e 7

wy..g y4

j-t to NPC-97 0107 -

Pagei ENCLOSURE 2 NO SIGNIFICANT II AZARDS CONSIDERATION Addition of a Special Test Exception to Allow Inservice Leak and Ilydrostatic Testing to be Performed at Temperatures Greater Than 200'F but Less Than or Equal to 212'F While Considermg the Reactor to Remain in OPERATIONAL CONDITION 4 1.

- Does this change involve a significant increase in the probability or consequences of an accident previously evaluated The proposed change allows the performance ofinservice leak and hydrostatic testing at a reactor coolant tempcrature of gre:.ter than 200*F but less than or equal to 212*F while considering the plant to remain in OPERATIONAL CONDITION 4. This change to permit the average teactor coolant temperature to be increased above 200'F, but not greater than 212'F while performing inservice leak and hydrostatic :esting will not significantly increase the probability of an accident previously evaluated. These tests are performed nearly water solid with all control rods fully inserted. Therefore, the stored er.ergy in the reactor core and coolant will be very low and the potential for causing fuel failures with a subsequent increase in coolant activity is minimal. The restrictions provided in the proposed Special Test Exception, to require Secondary Containment integrity and Standby Gas Treatment System OPERABILITY, provide assurance that any potential releases into secondary containmeint will be restricted from direct release to the environment and will be adequately filtered if released. With the reactor coolant temperature limited to 212'F, there will be little or no flashing of coolant to steam, and any release of radioactive materials will be minimized.

Therefore, this change will not significantly increase the consequences of an

- accident. In the event of a large prima.y system leak, the reactor vessel will rapidly depressurize allowing the low p: essure Emergency Core Cooling Systems (ECCS) to operate. The capability of the required ECCS in OPERATIONAL CONDITION 4 is adequate to maintain the core flooded under these conditions. Small system leaks will be detected by leakage inspections, which are an integral part of the insersice leak and hydrostatic testing program, before any significant inventory loss can occur. Therefore, this change will not involve a significant increase in the probA or consequences of an accident previously evaluated.

g' l to

= NRC-97 0107 Page 2.

9 2.

Does this change create the possibility of a new or different kind of

-accident from any accident previously evaluated.

Al' awing the reactor to be considered to remain in OPERATIONAL CONDITION 4 during inservice leak and hydrostatic testing with reactor coolant temperatures greater than 200'F but less than or equal to 212*F, is an exception to certain 01 ERATIONAL CONDITION 3 requirements including those associated with Primary Containment Integrity and full complement operability of the ECCS systems. The insenice leak and hydrostatic test coi.ditions remain unchanged otherwise. The reactor coolan' system is designed for temperatures exceeding 500'F with similar pressures; and therefore, any leaks occurring will be bounded by the main steam line break outside containment analysis provided in Section 15.6.4 of the UFSAR.

Therefore, this change will not create the possibility of a new or different kind of accident from any accident previously evaluated.

3.

Does this chs.nge involve a significant reduction m a margin of safety.

The proposed change allows insenice leak and hydrostatic testing to be performed with reactor coolant temperatures of up to 212'F, and the reactor to be considered to remain in OPERATIONAL CONDITION 4. The reactor vessel head will be in place, Secondary Comainment Integrity will be maintained and the systems required in OPERATIONAL CONDITION 4 will be OPERABLE in accordance with the Technical Specifications;

< therefore, the proposed change will not have a significant impact on any design basis accident or safety limit. Insenice leak and hydrostatic testing is performed water solid, or nearly water solid with reactor coolant temperature

$ 212*F. The stored energy in the core and coolant will be very low and the potential for failed fuel and a subsequent increase in coolant activity will be minimal. The reactor pressure vessel will rapidly depressurize in the event of a large primary system leak, and tlie low pressure ECCS systems required to be OPERABLE in OPERATIONAL CONDITION _4 will be adequate to maintain the core flooded, thus ensuring that the fuel will not exceed the 2200

'F peak clad temperature limit. Additionally, requiring Secondary Containment Integrity will result in any potential airbome radictim being filtered through the SGTS, thus ensuring that offsite doses remain well within the 10CFR100 limits. Small system leaks will be detected by leakage inspections before any significant inventory loss can occur. Therefore, this special test exception will not involve a significant reduction in a margin of

safety, o

' to NRC-97-0107 Page1 ENCLOSURE 3 RATIONAL E FOR SUPPORT OF ENIGENT CIIANGE Detroit Edison requests that this license amendment request be processed in an exigent manner as allowed by 10CFR50.91(a)(6). During May of 1997, increasing offgas radiation levels led to the identification of a small fuelleak. At that time, action was taken to mitigate the leak, and planning was initiated for an outage to allow for identification and replacement of the leaking fuel. It was determined that the best time for this outage, based upon plant safety, customer needs, system load demands, and fuel optimization concerns, would be October of 1997. Conducting an outage at that time is a conservative measure even though the leakage has not approached regulatory limits. This mid-cycle outage is expected to begin October 3, 1997, with an expected duration of 16 days. A reactor coolant system insersice leak test (System Leakage Test) will be required to be performed prior to startup from this outage. The outage will be shorter in duration and will not result in replacement of the amount of fuel typical of a refueling outage, therefore, the reactor cockat tystem insersice leak test will be performed at a higher decay heat load than is encountered following a normal refueling outage. During the fmal planning for this outage, it was recently recognized that the anticipated de,:ay heat levels would not allow for sumcient time to conduct the required leakage test in a controlled, deliberate manner within the Technical Specification limits governing test temperatures. Without this Special Test Exception, Detroit Edison is not confident that the leakage test pressurization, inspection, and recovery can be accomplished within the 200 F reactor coolant temperature limit, thus necessitating receipt of this Special Test Exception prior to the performance of the leak test.

Detroit Edison has used its best efforts to make a timely application for this amendment. However, this short time frame may not allow the normal public notice and comment period described in 10CFR50.91(a)(2), and still ensure receipt of the license amendment in time to support leak testing and subsequent plant startup as currently scheduled. Therefore, the requested exigent treatment of this license amendment request could not be avoided. In making preparetions for this unexpected outage, it was only recently concluded that a Special Test Exception would be necessary The matter was discussed with the NRC Staff, and the license amendment request was prepared and reviewed in an expeditious manner. Therefore, Detroit Edison requests that this license amendment request be handled in an exigent manner as allowed by 10CFR50.91(a)(6), and that it be approved by October 8,1997.

_n

. =.. -

..,4.2 y

9 9,

~

.Encissure 4 to x

NRC.97-0107 v i

4-.

p.g, j, -

.l

,.f

~

a

. ENCLOSURE 4-a

.m n

ENVIRONMENTAL IMPACT i

Detroit Edison has reviewed the proposed Technical Specification change against the criteria of 10CFR51.22 for environmental considerations. The proposed change does

not involve a significant hazards consideration. Neither does it significantly change the types or significantly increase the amounts of efliuents that may be released -

offsite, nor significantly increase individual or cumulative occupational radiation exposures. Based on the foregoing, Detroit Edison concludes that the proposed --

l J Technical. Specifications do meet the criteria given in 10CFR51.22(c)(9) for a categorical exclusion from the requirements for an Environmental Impact Statement.-

i.

2 9

k a

v M

1 S

0

+

?

9

..u-,

.w+.

,,m

.-,,.v.,.

+,,,..

.y 4

c Enclosur S to-

. NRC-97-0107 '

Page1.

ENCLOSURE 5 FERMI 2 NRC DOCKET NO. 50-341 OPERATING 1,1 CENSE NPF-43 LICENSE AMENDMENT REQUEST:

.TECIINICAL SPECIFICATION Cif ANGE Part 1 of this enclosure contains a hand marked copy of the current Technical Specifications,iadicating the proposed changes. A typed version of the Technical Specifications incorporating the proposed changes is provided in Part 2.

l

~

,