ML24066A197

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NRC Inspection Report 05000327-2024090 and 05000328-2024090 and Preliminary Greater than Green Finding and Apparent Violation
ML24066A197
Person / Time
Site: Sequoyah  
(DPR-077, DPR-079)
Issue date: 03/19/2024
From: Gregory Suber
NRC/RGN-II/DRP/RPB5
To: Jim Barstow
Tennessee Valley Authority
References
EA-24-008 IR 2024090
Download: ML24066A197 (19)


See also: IR 05000327/2024090

Text

EA-24-008

Jim Barstow

Vice President Nuclear Regulatory

Affairs & Support Services

Tennessee Valley Authority

1101 Market Street, LP 4A-C

Chattanooga, TN 37402-2801

SUBJECT:

SEQUOYAH, UNITS 1 AND 2 - NRC INSPECTION REPORT

05000327/2024090 AND 05000328/2024090 AND PRELIMINARY GREATER-

THAN-GREEN FINDING AND APPARENT VIOLATION

Dear Jim Barstow:

The enclosed inspection report documents a finding and associated apparent violation that the

U.S. Nuclear Regulatory Commission (NRC) has preliminarily determined to be of greater than

very low safety significance (i.e. greater-than-Green), resulting in the need for further evaluation

to determine significance and therefore the need for additional NRC action. As described in

Enclosure 1, a self-revealed apparent violation of Technical Specification (TS) 5.4.1,

Procedures, was identified for Sequoyah Nuclear Plants failure to establish, implement, and

maintain adequate procedures for maintenance activities on the 1B Diesel Generator (DG)

exhaust valves, which resulted in its failure on September 19, 2023. We assessed the

significance of the finding using the significance determination process (SDP) and the best

available information at the time of the Significance and Enforcement Review Panel on February

21, 2024. Enclosure 2 contains a detailed risk evaluation with the basis of our preliminary

significance determination. We are considering escalated enforcement for the apparent violation

consistent with our Enforcement Policy, which can be found at http://www.nrc.gov/about-

nrc/regulatory/enforcement/enforce-pol.html. Because we have not made a final determination,

no notice of violation is being issued at this time. Please be aware that further NRC review may

prompt us to modify the number and characterization of the apparent violation.

On February 15, 2024, you informed the NRC that you completed an evaluation of the risk

impact of the 1B DG failure to run on September 19, 2023. The NRC was not able to review

your evaluation prior to completing the preliminary determination enclosed in this letter but will

review it and consider your position as we make our final decision on this matter. The NRCs

evaluation is subject to several uncertainties which could affect the outcome of the significance

determination. Therefore, before we make a final decision, we request you provide any

additional information that you feel would be beneficial in our evaluation of the significance of

the finding. Specifically requested is any additional information or perspectives that address

mitigation of the dominant accident sequences given the potential for the delayed onset of

station blackout plant conditions and any additional information or perspectives regarding the

ability to repower containment hydrogen igniters when assessing the potential for large early

release frequency.

March 19, 2024

J. Barstow

2

On February 28, 2024, you informed the NRC that you completed a Level 1 Evaluation (Root

Cause Assessment, RCA) Report (RCAR) to determine the causal factors which resulted in the

1B DG failure to run on September 19, 2023. The NRC was not able to review your RCAR prior

to completing the preliminary determination enclosed in this letter but will review it and consider

your position as we make our final decision on this matter.

The NRCs SDP is designed to encourage an open dialogue between your staff and the NRC;

however, the dialogue nor the written information you provide should affect the timeliness of our

final determination.

Before we make a final decision on this matter, we are providing you with an opportunity to (1)

request a Regulatory Conference where you can present to the NRC your perspective on the

facts and assumptions the NRC used to arrive at the finding and assess its significance, or (2)

submit your position on the finding to the NRC in writing. If you request a Regulatory

Conference, it should be held within 40 days of the receipt of this letter, and we encourage you

to submit supporting documentation at least one week prior to the conference in an effort to

make the conference more efficient and effective. If a Regulatory Conference is held, it will be

open for public observation. If you decide to submit only a written response, such submittal

should be sent to the NRC within 40 days of your receipt of this letter.

If you choose to send a response, please include your perspective of the significance of the

finding along with the related facts and assumptions used to reach your determination.

Additionally, your response should be clearly marked as a "Response to Apparent Violation;

(EA-24-008)" and should include for the apparent violation: (1) the reason for the apparent

violation or, if contested, the basis for disputing the apparent violation; (2) the corrective steps

that have been taken and the results achieved; (3) the corrective steps that will be taken; and

(4) the date when full compliance will be achieved. Your response should be submitted under

oath or affirmation and may reference or include previously docketed correspondence if the

correspondence adequately addresses the required response. Additionally, your response

should be sent to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Center,

Washington, DC 20555-0001 with a copy to Mr. Louis McKown, U.S. Nuclear Regulatory

Commission, Region II, within 40 days of the date of this letter. If an adequate response is not

received within the time specified or an extension of time has not been granted by the NRC, the

NRC will proceed with its enforcement decision or schedule a Regulatory Conference.

If you decline to request a Regulatory Conference or to submit a written response, you

relinquish your right to appeal the final SDP determination, in that by not doing either, you fail to

meet the appeal requirements stated in the Prerequisite and Limitation sections of Attachment 2

of NRC Inspection Manual Chapter 0609.

Please contact Mr. Louis McKown via phone at 404-997-4545, and in writing, within 10 days

from the issue date of this letter to notify the NRC of your intentions. If we have not heard from

you within 10 days, we will continue with our significance determination and enforcement

decision. The final resolution of this matter will be conveyed in separate correspondence.

For administrative purposes, this inspection report provides an update to the apparent violation

documented in NRC inspection report 05000327/2023004 AND 05000328/2023004, dated

February 12, 2024 (Agency Documents Access and Management System (ADAMS) Accession

Number ML24040A073).

J. Barstow

3

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Gregory F. Suber, Deputy Director

Division of Reactor Projects

Docket Nos. 05000327 and 05000328

License Nos. DPR-77 and DPR-79

Enclosures:

1. Inspection Report

2. UNIT 1 B-EDG DETAILED RISK EVALUATION

cc w/ encl: Distribution via LISTSERV

Signed by Suber, Gregory

on 03/19/24

ML24066A197

SUNSI Review

Non-Sensitive

Sensitive

Publicly Available

Non-Publicly Available

OFFICE

RII/DRP

RII/DRP

RII/DRP

RII/DRP

RII/EICS

HQ/NRR/DRO

NAME

S. Ninh

D. Hardage

S. Sandal

L. McKown

M. Kowal

R. Felts

DATE

3/7/2024

3/7/2024

3/7/2024

3/7/2024

3/7/2024

3/13/2024

OFFICE

HQ/NRR/DRA

HQ/OE

RII/DRP

NAME

M. Franovich

D. Bradley

G. Suber

DATE

3/16/2024

3/12/2024

3/19/2024

Enclosure 1

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000327 and 05000328

License Numbers:

DPR-77 and DPR-79

Report Numbers:

05000327/2024090 and 05000328/2024090

Enterprise Identifier:

I-2024-090-0002

Licensee:

Tennessee Valley Authority

Facility:

Sequoyah, Units 1 and 2

Location:

Soddy Daisy, TN 37379

Inspection Dates:

February 05, 2024 to February 27, 2024

Inspectors:

D. Hardage, Senior Resident Inspector

S. Ninh, Senior Project Engineer

A. Price, Resident Inspector

S. Sandal, Senior Reactor Analyst

Approved By:

Gregory F. Suber, Deputy Director

Division of Reactor Projects

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting a NRC inspection at Sequoyah, Units 1 and 2, in accordance with

the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for

overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to establish and implement adequate maintenance procedures on the 1B Diesel

Generator

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Preliminary greater-than-Green

AV 05000327,05000328/2023004-01

Open

EA-24-008

[H.12] - Avoid

Complacency

71111.15

A self-revealed apparent violation (AV) of Technical Specification (TS) 5.4.1,

Procedures, was identified. The licensees procedures for maintenance on the 1B Diesel

Generator (DG) were not adequately prescribed and/or accomplished in accordance with

documented instructions and procedures of a type appropriate to the circumstances.

Specifically, the licensee failed to adequately establish and implement maintenance

instructions and practices that reasonably ensured the reliability, availability, and operability of

the 1B DG. The 1B DG failed on September 19, 2023, during a surveillance run due to a

piston failure that required the DG to be placed in an emergency shutdown condition. The

most probable direct cause of the failure was an improperly tightened rocker arm adjustment

screw locknut which resulted in severe damage to the associated power pack.

Additional Tracking Items

None.

3

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

INSPECTION RESULTS

Failure to establish and implement adequate maintenance procedures on the 1B Diesel

Generator

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Preliminary greater-than-Green

AV 05000327,05000328/2023004-01

Open

EA-24-008

[H.12] - Avoid

Complacency

71111.15

A self-revealed AV of TS 5.4.1, Procedures, was identified. The licensees procedures for

maintenance on the 1B DG were not adequately prescribed and/or accomplished in

accordance with documented instructions and procedures of a type appropriate to the

circumstances. Specifically, the licensee failed to adequately establish and implement

maintenance instructions and practices that reasonably ensured the reliability, availability,

and operability of the 1B DG. The 1B DG failed on September 19, 2023, during a surveillance

run due to a piston failure that required the DG to be placed in an emergency shutdown

condition. The most probable direct cause of the failure was an improperly tightened rocker

arm adjustment screw locknut which resulted in severe damage to the associated power

pack.

Description: On September 19, 2023, Sequoyah was performing a scheduled 24-hour run of

the 1B DG. 1B DG was started at 1121 and at approximately 1544, operations received

multiple Main Control Room and local annunciator alarms including high crankcase pressure

followed by low jacket water level. The operator performed an emergency stop of the 1B DG

in accordance with the annunciator response procedure.

The onsite Class 1E AC electrical distribution system supplies electrical power to two power

trains shared between the two units. The AC sources for the shared loads are distributed

across both units shutdown boards. However, the impacts of an inoperable offsite power or

DG on the opposite units shutdown board differ from the impacts of an inoperable offsite or

DG on an associated units shutdown board, due to the loads powered from the respective

board.

Sequoyah Units 1 and 2 entered LCO 3.8.1 Condition B for one Train B DG inoperable.

Sequoyah Units 1 and 2 TS 3.8.1 requires four DGs capable of supplying the onsite Class 1E

AC Electrical Power Distribution System, to be operable in Modes 1-4; if a DG is inoperable, it

shall be returned to operable status within 7 days or in accordance with the Risk-Informed

Completion Time Program. The DGs must demonstrate the capability to run continuously at

4

full load for at least 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in order to ensure that they can support safety-related plant

equipment independently of offsite electrical power sources.

10 CFR Part 50.73(a)(2)(i)(B) requires a Licensee Event Report (LER) for any operation or

condition which was prohibited by the plants TS except when the TS is administrative nature.

As part of the failure investigation, inspection of the 1B2 engine discovered water leaking into

cylinder #14. The 1B DG is comprised of two diesel engines identified as 1B1 and 1B2

coupled to a common electrical generator. Further inspection showed an approximately 3-

inch diameter hole in the piston associated with 1B2 engine cylinder #14. The cylinder #14

exhaust valve bridge adjusting screw locknut nut associated with one pair of the exhaust

valves was found loose on top of the head along with valve spring retainer pieces. This

condition is consistent with the exhaust valve falling into the cylinder during operation and

causing damage to the piston/cylinder head.

Sequoyah had performed the four-year preventive maintenance procedure, PM 063604820,

on the 1B DG in January 2023. This maintenance, in part, directs the technicians to check/set

the exhaust valve lash settings, which requires the loosening and retightening the exhaust

valve bridge adjuster locknut. Table 5.9.7 Top Timing Table shows the lash setting performed

and initialed for each cylinder. Knowledgeable craft interviewed early, and later causal

analyses provided differing understandings of expectations for execution of the valve lash

verification and rocker arm locknut adjustments. These were established as skill of the craft

using terms such as tighten vice obtaining readily attainable specified values consistent with

MMTP-104, Guidelines and Methodology for Assembling and Tensioning Threaded Connections,

Revision 13.

The failure of the 1B DG resulted from the loss of proper lash adjustment of the rear valve

bridge on cylinder #14. During operation of the 1B DG following maintenance, the exhaust

valve bridge adjuster locknut on cylinder #14 separated from the adjustment screw, indicating

that the locknut was not adequately tightened. The separated locknut allowed the adjuster

screw to loosen, significantly increasing the clearance between the rocker arm and the valve

bridge. As the adjustment screw loosened further, the valve bridge spring no longer

compressed resulting in a loss of the spherical spring seat mating with the cylinder head. This

ultimately resulted in a complete loss of retention of the exhaust valve, which then fell into the

cylinder causing the observed cylinder damage and loss of jacket water cooling as the loose

exhaust valve was struck by the piston head during each stroke.

Corrective Actions: The 1B DG was emergency stopped and Sequoyah units 1 and 2

entered LCO 3.8.1 Condition B for one Train B DG inoperable. Sequoyah technicians

performed corrective maintenance on the 1B DG which included the replacement of impacted

power packs followed by post maintenance and operability testing including a new 24-hour

run. In subsequent maintenance outages on the remaining station DGs, Sequoyah staff

ensured all exhaust valve rocker arm adjusting screw locknuts were torqued in accordance

with vendor recommendations. The licensee ordered a failure analysis of the failed cylinder to

be completed and ensured that the latest vendor recommendations for exhaust valve bridge

lash adjustment were incorporated into the station's 4-, 6-, and 12-year preventive

maintenance instructions consistent with MMTP-104.

Corrective Action References: CRs 1881328, 1882753, 1900849

5

Performance Assessment:

Performance Deficiency: The inspectors determined that the licensee's failure to adequately

establish and implement maintenance instructions and practices was a performance

deficiency reasonably within their ability to foresee and prevent. Specifically, during

performance of exhaust valve lash adjustment in accordance with maintenance instruction

PM 063604820, appropriate tightening of the exhaust valve bridge adjuster locknut on DG

1B2 cylinder #14 was not performed. This resulted in the loss of retention of the exhaust

valve while in service causing damage to the associated cylinder and loss of jacket water

cooling.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Equipment Performance attribute of the Mitigating

Systems cornerstone and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the failure to properly implement adequate

maintenance instructions and practices contributed to the failure of the 1B DG.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The

inspectors reviewed IMC 0609, Attachment 4, Initial Characterization of Findings, and

determined that the finding affects the Mitigating Systems cornerstone. The inspectors

screened the performance deficiency using Exhibit 2 of Appendix A and determined a

detailed risk evaluation was required because the degraded condition represented a loss of

the Probabilistic Risk Assessment (PRA) function of one train of a multi-train TS system for

greater than its TS allowed outage time.

A Region II Senior Reactor Analyst performed a detailed risk evaluation. The finding was

determined to be preliminarily greater-than-Green. The preliminary risk estimate was

obtained by performing a run time failure conditional analysis of the B-train emergency diesel

generator (EDG) using a 246-day exposure period evaluated over eight run intervals. The

dominant Standardized Plant Analysis Risk (SPAR) model sequences were associated with

fire initiating events that involved impact to the normal offsite power supply, unavailability of

the A-train EDG, resulting in station blackout (SBO) plant conditions, followed by a reactor

coolant pump seal failure or turbine-driven auxiliary feedwater pump failure. Because the B-

train EDG would have been expected to operate for some period at nominal failure likelihood

prior to onset of SBO conditions, additional analysis of the impact of the delayed SBO on the

mitigation of the dominant accident sequences will be necessary before reaching a final

determination of significance. Additional evaluation would also be necessary prior to making

any determination of the estimated increase in large early release frequency due to the

delayed onset of SBO and the potential for repowering the containment hydrogen igniters

from Diverse and Flexible Coping Strategy (FLEX) diesel generator sources. See Enclosure 2

UNIT 1 B-EDG DETAILED RISK EVALUATION, for a summary of the basis for the

preliminary risk determination.

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the

possibility of mistakes, latent issues, and inherent risk, even while expecting successful

outcomes. Individuals implement appropriate error reduction tools. In this case and as

associated with this finding, the licensee failed to ensure that error reduction tools such as

specified values appropriate to the situation were implemented in lieu of skill of the craft

during the performance of PM 063604820.

6

Enforcement:

Violation: Sequoyah Unit 1 TS 5.4.1 requires, in part, that written procedures shall be

established, implemented, and maintained for the applicable activities recommended in

Appendix A of Regulatory Guide (RG) 1.33, Quality Assurance Program Requirements

(Operation), Revision 2. Appendix A to RG 1.33, Section 9.a, states that maintenance that

can affect the performance of safety-related equipment should be performed in accordance

with written procedures, documented instructions, or drawings appropriate to the

circumstances.

Sequoyah PM 063604820 is a preventive maintenance procedure that includes instructions

for the adjustment of the safety-related DG exhaust valve bridge adjuster locknut, an activity

that can affect the performance of DGs safety-related function.

Sequoyah Units 1 and 2 TS 3.8.1 requires, in part, four DGs capable of supplying the onsite

Class 1E AC Electrical Power Distribution System, to be operable in Modes 1 through 4; if a

DG is inoperable, it shall be returned to operable status within 7 days or in accordance with

the Risk-Informed Completion Time Program.

Contrary to the above, on January 25, 2023, the licensee failed to establish, implement, and

maintain a procedure appropriate to the circumstances of the 1B DG maintenance as

required in TS 5.4.1, resulting in the licensees failure to meet the DG operability

requirements in TS 3.8.1. Specifically, the licensee failed to establish, implement, and

maintain appropriate preventive maintenance instructions under PM 063604820 to properly

tighten the rear exhaust valve bridge adjuster locknut on the 1B DG cylinder #14, leading to

the failure of the DG on September 19, 2023, during a surveillance test.

Hence, further, contrary to the above, from January 25, 2023, through September 29, 2023,

the licensee failed to provide four operable DGs capable of supplying the onsite Class 1E AC

Electrical Power Distribution System. Specifically, given performance of the inadequate

preventive maintenance activity in January 2023, the 1B DG was unable to support design-

basis events.

Enforcement Action: This violation is being treated as an apparent violation pending a final

significance (enforcement) determination.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On February 27, 2024, the inspectors presented the NRC inspection results to Mr. Tom

Marshall, Site Vice President, and other members of the licensee staff.

7

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.15

Corrective

Action

Documents

1881328

Unit 1 received

unexpected alarms

resulting in emergency

stopping 1B DG

09/19/2023

71111.15

Corrective

Action

Documents

1882753

Perform inspection of

locking nuts on the rocker

assembly for 2B diesel

generator

09/26/2023

71111.15

Corrective

Action

Documents

1900849

EDG engine 1B2 exhaust

valve failure

01/02/2024

71111.15

Miscellaneous

SQN-0-24-008 R0

PRA Evaluation

Response

02/15/2024

Enclosure 2

UNIT 1 B-EDG DETAILED RISK EVALUATION

OVERALL RISK SUMMARY

The Sequoyah Unit 1 B-train emergency diesel generator (EDG) was rendered inoperable due

to significant damage to the #14-cylinder assembly during a surveillance test on September 19,

2023. A conditional risk evaluation using a 246-day exposure period preliminarily estimated an

increase in Core Damage Frequency (delta-CDF) of 2.68E-05/year for Unit 1 and 2.10E-05/year

for Unit 2. The Standardized Plant Analysis Risk (SPAR) model dominant sequences were

associated with station blackout (SBO) scenarios that did not include consideration of the

reactor decay heat removal and Reactor Coolant System (RCS) cooldown that would occur as

the result of the delayed onset nature of SBO plant conditions following the initial loss of offsite

power. Additional evaluation of the impact of the delayed onset of SBO conditions will be

necessary to refine the preliminary risk estimates before making a final significance

determination.

EXPOSURE TIME

The component run time failure approach discussed in Section 2.5 of Volume 1 of the Risk

Assessment Standardization Project (RASP) Manual was used to evaluate the condition

exposure time. The run history of the B-train EDG prior to the failure in September 2023 was

used to determine the number of intervals of accumulated operation for its 24-hour Probabilistic

Risk Assessment (PRA) mission time (condition inception time unknown but the degradation

was assumed to progress only during operation of the EDG). The final time interval included the

B-train EDG repair time after the failure was identified during the surveillance test. A total

exposure time of 246 days divided into eight run intervals, including repair time, was used for

the analysis.

RISK ANALYSIS/CONSIDERATIONS

Assumptions

1.

The condition was assumed to only continue to degrade when the EDG was operated and

not when in a standby status. Consequently, the component run time failure approach

discussed in Section 2.5 of Volume 1 of the RASP manual was used to evaluate the

condition exposure time. Based on the run history of the B-train EDG, a condition exposure

period of 246 days, divided into eight separate run intervals, and including repair time, was

used for the analysis. To explore the sensitivity of the evaluation method, a sensitivity case

will be performed that does not divide the 246-day exposure period into separate time

intervals.

2.

No repair credit for the failure of the B-train EDG was included in the analysis.

3.

Diverse and Flexible Coping Strategies (FLEX) mitigating strategies and equipment were

credited in the analysis using a 24-hour PRA mission time. FLEX equipment reliability was

modeled using information contained in PWROG-18042-NP, Revision 1, FLEX Equipment

Data Collection and Analysis, (ADAMS ML22123A259). A sensitivity case with no FLEX

credit was also performed.

Systems Analysis Program for Hands-On Integrated Reliability Evaluations (SAPHIRE) software

Version 8.2.9 and Sequoyah SPAR model Version 8.82 were used for the evaluation.

2

1.

The SPAR model was modified to account for the FLEX implementation strategy at

Sequoyah. A new SBO-ELAP event tree and top events were created with the following key

characteristics:

A top event for the FLEX 480V Diesel Generator (DG) sets which do not require

deployment and are in enclosures on the auxiliary building roof was created to query

the ability to power the battery chargers following Extended Loss of AC Power

(ELAP) declaration. Success of the 480V FLEX DGs would extend battery availability

for remainder of sequences.

A top event was created for powering the 6.9kV shut down boards from the 3 MW

6.9kV FLEX DGs which are permanently installed and located in a separate building

from the EDGs. Success of the 6.9kV FLEX DGs provides the ability to power in-

plant equipment like Motor-Drive Auxiliary Feedwater (MDAFW) and Safety Injection

(SI) pumps (in addition to FLEX mitigating equipment). The 6.9kV FLEX DGs can be

used to power the battery chargers should the 480V FLEX DGs fail. DC load

shedding at Sequoyah does not impact the ability to power components such as the

MDAFW pumps or SI pumps from the 6.9kV FLEX DGs. The corresponding top

events were modified to reflect the availability of safety-related components for

mitigation given the success of the 6.9kV FLEX DGs.

2.

The approach discussed in Section 2.5 of the RASP manual was used to evaluate the

condition exposure time. The run history of the B EDG prior to the failure in September

2023 was used to determine the number of intervals of accumulated operation of the EDG

for the 24-hour PRA mission time (condition inception time unknown but the engine

degradation mechanism was assumed to only progress during operation of the EDG). The

final 10 days being considered in the exposure time includes the EDG repair time after the

failure occurred.

The fault tree logic for the B-train EDG was modified to split the fail-to-run basic

event into two separate components so that adjustments could be made to credit

EDG operation prior to failure. The SAPHIRE convolution mapping tool was then

used to update model convolution events using the new fault tree logic.

For the conditional case, the model was adjusted using change set

1BEXT_EDG_FTR which set event EPS-DGN-FR-1B to TRUE so that the FTR

common cause change would be calculated by SAPHIRE. The change set also set

the new basic event EPS-DGN-FR-1BEXT to 1.0 so the failure would show up in

cutsets for post-processing adjustment made for credited EDG run time.

For each time interval, the mission time for basic events EPS-DGN-FR-1BT2 and

EPS-DGN-FR-1BEXT were adjusted to reflect the estimated run time before failure

and each time interval also included ET post-processing to look for B EDG FTR

basic event EPS-DGN-FR-1BEXT in the cutsets and substitute the appropriate

recovery terms based on credited EDG operation.

3

3.

For each time interval, event tree post-processing rules were used to substitute the

appropriate recovery terms based on credited EDG operation. This had the effect of

crediting some amount of time of 1B EDG operation prior to its failure when estimating the

likelihood of non-recovery of power sources to the shutdown boards. As an example, if the

EDG would be expected to operate for approximately six hours (at nominal failure

likelihood) prior to failure due to the performance deficiency, the one- and four-hour non-

recovery terms for Loss of Offsite Power (LOOP) recovery would be adjusted to seven and

ten hours respectively.

4.

A conditional case was performed for every interval bin and the results were summed to

determine the overall risk estimate.

5.

The following SPAR model event sequences were used in evaluating the nominal and

conditional cases:

INTERNAL EVENTS

FIRE

SEISMIC

HIGH WINDS

TORNADO

INTERNAL FLOODING

EXTERNAL FLOODING

6.

SAPHIRE condition assessments were performed using the event tree direct solve method

where cutset results were gathered for sequences other than internal events. Conditional

case change set 1B_EDG_FTR was used to evaluate the change in risk that could be

attributed to the EDG failure for each time interval being evaluated over 236 days of the

exposure period. The final 10 days of repair time was estimated by performing a condition

assessment with the 1B EDG Test and Maintenance basic event (EPS-DGN-TM-1B) set to

TRUE for the conditional case.

7.

SAPHIRE condition assessments were also performed using the ECA module to generate

dominant sequence and cutset reports. Conditional case change set 1B_EDG_FTR was

used in the condition assessments.

4

CALCULATIONS

Best Estimate:

Interval

Exposure

(days)

Fire

-CDP

Int. Evnt

-CDP

Hi-Wind

-CDP

Seismic

-CDP

Int. Flood

-CDP

Tornado

-CDP

Ext. Flood

-CDP

1

26

1.49E-06

8.72E-07

3.26E-07

1.99E-08

9.19E-09

3.12E-09

9.26E-10

2

24

1.40E-06

8.17E-07

3.03E-07

1.84E-08

8.55E-09

2.87E-09

8.55E-10

3

38

2.24E-06

1.31E-06

4.83E-07

2.92E-08

1.35E-08

4.55E-09

1.35E-09

4

28

1.67E-06

9.78E-07

3.58E-07

2.15E-08

9.90E-09

3.34E-09

9.97E-10

5

28

1.68E-06

9.93E-07

3.61E-07

2.15E-08

9.90E-09

3.34E-09

9.97E-10

6

35

2.13E-06

1.26E-06

4.55E-07

2.68E-08

1.25E-08

4.18E-09

1.25E-09

7

29

1.79E-06

1.07E-06

3.81E-07

2.22E-08

1.03E-08

3.46E-09

1.03E-09

8

28

1.75E-06

1.07E-06

3.72E-07

2.15E-08

9.97E-09

3.34E-09

9.97E-10

Repair

10

5.69E-07

3.64E-07

9.99E-08

5.21E-09

3.23E-09

7.67E-10

2.19E-10

Total

246

1.47E-05

8.74E-06

3.14E-06

1.86E-07

8.71E-08

2.90E-08

8.62E-09

SAPHIRE condition assessments were performed using the direct solve method and conditional

case change set 1B_EDG_FTR. The overall estimated increase in risk was a change in Core

Damage Probability (delta-CDP) of 2.68E-05. FIRE sequences were determined to be strongly

dominant in the results with INTERNAL EVENTS and HIGH WINDS also significant sequence

contributors. SAPHIRE ECA condition assessments were performed to generate dominant

sequence and cutset reports.

Dominant FIRE cutsets were associated with fire initiating events in the shutdown board rooms

resulting in a LOOP. The LOOP is accompanied by common mode failure of the A-train

emergency diesel generator leading to an SBO with Reactor Coolant Pump (RCP) seal failure

resulting in core damage.

Dominant INTERNAL EVENT and HIGH WIND cutsets were associated with weather-related

LOOP with common mode failure of the A-train emergency diesel generator leading to an SBO

with either RCP seal failure (INTERNAL EVENT) or random failure of the turbine-driven auxiliary

feedwater pump to run (HIGH WIND).

Sensitivity 1 - No Time Intervals

To explore the sensitivity of the analysis results due to application of the run time treatment of

exposure time, this sensitivity will determine the estimated increase in risk-based on the full

exposure period without the use of time intervals or post-processing to adjust power recovery

terms.

5

SAPHIRE condition assessments were performed using the direct solve method and conditional

case change set 1B_EDG_FTR for the full 246-day exposure period.

Exposure

(days)

Fire

-CDP

Int. Evnt

-CDP

Hi-Wind

-CDP

Seismic

-CDP

Int. Flood

-CDP

Tornado

-CDP

Ext. Flood

-CDP

246

1.93E-05

1.23E-05

3.64E-06

1.82E-07

8.71E-08

2.90E-08

8.76E-09

The overall estimated increase in risk was a delta-CDP of 3.55E-05.

As expected, the sensitivity results were higher without consideration of the run history of the B

EDG or consideration for the increased time that would have been available to potentially

recover power sources for the affected safety bus. The higher estimate would not have been

sufficient to alter the overall conclusions of the analysis. The use of the run time failure

methodology was determined to be the most appropriate treatment of exposure time for the

analysis.

Sensitivity 2 - Use of SAPHIRE ECA vs. Direct Solve Method

Because SAPHIRE ECA was used to generate reports for the dominant sequence cutsets, the

information was readily available to assess the impact of the use of SAPHIRE ECA on the

quantification of results.

SAPHIRE ECA condition assessments were performed for the full exposure period (no run

intervals used) with the B EDG FTR basic event set to TRUE for the conditional case.

Exposure

(days)

Fire

-CDP

Int. Evnt

-CDP

Hi-Wind

-CDP

Seismic

-CDP

Int. Flood

-CDP

Tornado

-CDP

Ext. Flood

-CDP

246

2.05E-05

1.23E-05

3.86E-06

4.73E-07

9.76E-08

3.07E-08

8.33E-09

The overall estimated increase in risk was a delta-CDP of 3.73E-05.

The analyst noted that the analysis results were slightly higher than the use of no time intervals

in Sensitivity 1, but more significantly higher than the best estimate using the run time failure

approach. As with Sensitivity 1, the higher estimate would not have been sufficient to alter the

overall conclusions of the analysis.

Sensitivity 3 - No FLEX

To evaluate the sensitivity of analysis results with respect to crediting of FLEX mitigation

strategies, the basic event for operator failure to enter ELAP procedures was set to 1.0 for both

the nominal and conditional cases.

FLX-XHE-XE-ELAP = 1.0

SAPHIRE ECA condition assessments were performed for the full exposure period (no run

intervals used) with the B EDG FTR basic event set to TRUE for the conditional case.

6

Exposure

(days)

Fire

-CDP

Int. Evnt

-CDP

Hi-Wind

-CDP

Seismic

-CDP

Int. Flood

-CDP

Tornado

-CDP

Ext. Flood

-CDP

246

2.89E-05

1.83E-05

5.48E-06

5.47E-07

1.08E-07

4.85E-08

1.70E-08

The overall estimated increase in risk was a delta-CDP of 5.34E-05.

Although the analysis results demonstrated some sensitivity with respect to the crediting of the

FLEX, its importance in the risk estimate was tempered by dominant cutsets that involved early

failure of the Turbine-Drive Auxiliary Feedwater (TDAFW) pump or RCP seal failures where

FLEX mitigation is not credited in the base SPAR model based on the assumption that the SBO

occurs at the time of the LOOP. Although not a strongly influential factor, inclusion of FLEX

mitigation was determined to be most appropriate to the circumstances and was considered in

the best estimate case.

CROSS-UNIT IMPACT

Because the EDGs have the capability of supplying power to the other units associated

shutdown boards, the impact of the performance deficiency on Unit 2 was assessed. The fail-to-

run basic event for the 2B EDG (EPS-DGN-FR-2B) was used as a surrogate for the cross-unit

impact and set to TRUE because the SPAR model is a Unit 1 model. An ECA condition

assessment over the entire 246-day exposure period was performed using FIRE sequences.

FIRE sequences were selected because they were the most dominant in the analysis results.

The condition analysis for Unit 2 yielded an estimated delta-CDP of 1.61E-05 vs. the Unit 1

delta-CDP of 2.05E-05 for un-binned FIRE sequences. The analyst noted that the Unit 2 risk

estimate for FIRE sequences was approximately 79% of the Unit 1 results. Applying that level of

reduction to the overall binned Unit 1 results (as a representative impact to Unit 2) would

produce an estimated delta-CDP of 2.10E-05 for Unit 2.

LICENSEE EVALUATION

The licensee provided the NRC with an evaluation of the estimated increase in risk of the Unit 1

B-train EDG failure on February 15, 2024. The licensees evaluation included an analysis of the

impact of delayed onset of SBO conditions on mitigation of the key accident sequences

including those associated with RCP seal failure and TDAFW pump failure. Additional NRC

review of the licensees evaluation will be performed prior to reaching a final decision regarding

the significance of the finding.

7

DELTA CDF FOR EXPOSURE TIME

The overall preliminary results are summarized below:

EVENT SEQUENCE

Best

Estimate

Sensitivity #1

No Intervals

Sensitivity #2

SAPHIRE ECA

Sensitivity #3

No FLEX ECA

FIRE

1.47E-05

1.93E-05

2.05E-05

2.89E-05

INTERNAL EVENTS

8.74E-06

1.23E-05

1.23E-05

1.83E-05

HIGH WINDS

3.14E-06

3.64E-06

3.86E-06

5.48E-06

SEISMIC

1.86E-07

1.82E-07

4.73E-07

5.47E-07

INTERNAL FLOODING

3.23E-09

8.71E-08

9.76E-08

1.08E-07

TORNADO

2.90E-08

2.90E-08

3.07E-08

4.85E-08

EXTERNAL FLOODING

8.62E-09

8.76E-09

8.33E-09

1.70E-08

TOTAL

2.68E-05

3.55E-05

3.73E-05

5.34E-05

Considering that SAPHIRE calculates the difference in Core Damage Probability over a given

exposure time, and that changes in CDF over the same period are numerically equivalent, the

change in CDF due to the finding would be on the order of 2.68E-05/year for Unit 1.

EXTERNAL EVENTS CONSIDERATIONS

Internal event risk estimates were greater than 1E-07, therefore all other external event

sequences were evaluated in the risk assessment.

LARGE EARLY RELEASE FREQUENCY IMPACT

The finding was evaluated in accordance with IMC 0609, Appendix H, Containment Integrity

Significance Determination Process, as a Type A finding. The dominant sequences in the

analysis are LOOP sequences and not Steam Generator Tube Rupture (SGTR) or Interfacing

System Loss of Coolant Accident (ISLOCA). The 6.9KV FLEX DGs can power the hydrogen

igniters through the 480V shutdown power distribution system. Additionally, the 480V FLEX

DGs can also be aligned to provide power to the hydrogen igniter supply transformers, if

required. The ability to restore power to the hydrogen igniters from FLEX equipment reduces the

likelihood of containment failure for SBO scenarios. For a LOOP/SBO sequence to represent

large early release frequency (LERF), core damage and containment failure must occur early in

the sequence and prior to the implementation of the site emergency plan for evacuation. The

analyst determined that additional evaluation would be warranted prior to making any

determination of delta-LERF risk. Specifically, the dominant cutsets would be reviewed to

determine if they represent a loss of secondary heat removal and failure of the FLEX DGs

simultaneously with an early failure of other mitigating equipment.

CONCLUSIONS/RECOMMENDATIONS

The preliminary estimated risk increase (delta-CDF) over the nominal case for the inoperability

of the Unit 1 B-train EDG was 2.68E-05/year (Unit 1) and 2.10E-05/year for Unit 2 (due to the

cross-unit impact). The dominant SPAR model sequences were associated with fire initiating

events that involved impact to the normal offsite power supply, unavailability of the A-train EDG

due to random failure or fire damage, resulting in station blackout (SBO) plant conditions,

followed by a reactor coolant pump seal failure or

8

turbine-driven auxiliary feedwater pump failure. Because the B-train EDG would have been

expected to operate for some period at nominal failure likelihood prior to onset of SBO

conditions, additional analysis of the impact of the delayed SBO on the potential mitigation of

the dominant accident sequences will be necessary before reaching a final determination of

significance. Accordingly, the finding is best characterized as preliminary greater-than-Green.