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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217N6531999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Hope Creek Generating Station,Unit 1.With ML20210U4721999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Hope Creek Generating Station,Unit 1.With ML20210C4731999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Hope Creek Generating Station,Unit 1.With ML20196A1511999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Hope Creek Generating Station,Unit 1.With ML20206U1571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Hope Creek Generating Station,Unit 1.With ML20205R5901999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Hope Creek Generating Station,Unit 1.With ML20204F7951999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Hope Creek Generating Station,Unit 1.With ML20199E7271998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Hope Creek Generating Station,Unit 1.With LR-N980580, Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With LR-N980544, Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with LR-N980491, Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With LR-N980439, Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With LR-N980401, Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 1 LR-N980354, Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 1 LR-N980302, Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 1 LR-N980247, Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 1 LR-N980196, Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 1 LR-N980104, Monthly Operating Rept for Feb 1998 for Hope Creek Generating Station,Unit 11998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Hope Creek Generating Station,Unit 1 ML20203B6741998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Hope Creek Generation Station,Unit 1 ML20198T3591997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Hope Creek Nuclear Generating Station,Unit 1 ML20203B6841997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 & Jan 1998 for Hope Creek Generation Station,Unit 1,summary of Changes,Tests & Experiments ML20198T4061997-11-30030 November 1997 Revised MOR for Nov 1997 for Hope Creek Nuclear Generating Station,Unit 1.Summary of Changes,Tests,Experiments & Refueling Info,Encl ML20203K3751997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Hcgs,Unit 1 ML20203K3821997-10-31031 October 1997 Revised Monthly Operating Rept for Oct 1997 for Hcgs,Unit 1 ML20199G5591997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Hcgs,Unit 1 ML20199G5931997-09-30030 September 1997 Revised Monthly Operating Rept for Sept 1997 for HCGS, Unit 1 ML20211Q6481997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Hope Creek Generating Station ML20212A5301997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Hope Creek Generating Station,Unit 1,summary of Changes,Tests & Experiments ML20217A1491997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Hope Creek Generating Station,Unit 1 ML20217A6261997-07-31031 July 1997 Revised Monthly Operating Rept for Jul 1997 for Hope Creek Generating Station,Unit 1 LR-N970503, Monthly Operating Rept for Jul 1997 for Hope Creek Generating Plant Unit 11997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Hope Creek Generating Plant Unit 1 ML20149F2921997-06-30030 June 1997 Monthly Operating Rept for June 1997 for HCGS ML20149F3061997-05-31031 May 1997 Revised Monthly Operating Rept for May 1997 for Hope Creek Generating Station.Summary of Changes,Tests & Experiments Encl ML20140H6761997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Hope Creek Generating Station Unit 1.Summary of Changes,Tests & Experiments Implemented in Apr 1997 Included in Rept LR-N970321, Monthly Operating Rept for Apr 1997 for Hope Creek Generating Station1997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Hope Creek Generating Station ML20137X7311997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Hope Creek ML20147F6051997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Hope Creek Generating Station ML20147F6111997-01-31031 January 1997 Revised MOR for Jan 1997 for Hope Creek Generating Station LR-N970110, Monthly Operating Rept for Jan 1997 for Hope Creek Generation Station Unit 11997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Hope Creek Generation Station Unit 1 ML20133M9831996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Hope Creek Generating Station ML20133B7901996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Hope Creek Generation Station Unit 1 LR-N966376, Monthly Operating Rept for Oct 1996 for Hope Creek Generation Station Unit 11996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Hope Creek Generation Station Unit 1 ML20129A8271996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Hope Creek Generation Station Unit 1 ML20134C0941996-08-31031 August 1996 Monthly Operating Rept for Aug 1996 for Hope Creek Generation Station ML20116P0181996-07-31031 July 1996 Monthly Operating Rept for Jul 1996 for Hope Creek Unit 1 ML20117C3331996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Hope Creek Generation Station Unit 1 ML20134C1031996-07-31031 July 1996 Revised Monthly Operating Rept for Jul 1996 Hope Creek Generation Station ML20115E8491996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Hope Creek Generation Station ML20117C3701996-06-30030 June 1996 Revised Monthly Operating Rept for June 1996 for Hope Creek Generating Station ML20116P0381996-06-30030 June 1996 Summary of Changes,Tests & Experiments That Had Been Implemented During June 1996 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F1501999-10-12012 October 1999 Special Rept:On 990929,south Plant Vent (SPV) Range Ng Monitor Was Inoperable.Monitor Was Inoperable for More than 72 H.Caused by Electronic Noise Generated from Noise Suppression Circuit.Replaced Circuit ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217N6531999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Hope Creek Generating Station,Unit 1.With ML20217M0211999-09-20020 September 1999 Part 21 Rept Re Possible Deviation of NLI Dc Power Supply Over Voltage Protection Circuit Actuation.Caused by Electrical Circuit Conditions Unique to Remote Engine Panel. Travelled to Hope Creek to Witness Startup Sequence of DG ML20211N5531999-09-0808 September 1999 Safety Evaluation Supporting Amend 121 to License NPF-57 ML20211B3781999-08-13013 August 1999 Special Rept 99-002:on 990730,NPV Radiation Monitoring Sys Was Declared Inoperable.Caused by Voltage Induced in Detector Output by Power Cable to Low Range Sample Pump. Separated Cables & Secured in Place to Prevent Recurrence ML20210U4721999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8331999-07-26026 July 1999 Safety Evaluation Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given HCGS Design,Operation & History ML20216D8721999-07-26026 July 1999 Review of Submittal in Response to USNRC GL 88-20,Suppl 4: 'Ipeees,' Fire Submittal Screening Review Technical Evaluation Rept:Hope Creek Rev 1:980518 ML20210F3331999-07-22022 July 1999 Safety Evaluation Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3.Finds That Proposed Alternative for RR-B3 Provides Acceptable Level of Quality & Safety & Authorizes Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20210C4731999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8901999-06-30030 June 1999 IPEEEs Technical Evaluation Rept High Winds,Floods & Other External Events ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML20196A1511999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Hope Creek Generating Station,Unit 1.With ML20206Q4731999-05-14014 May 1999 SER Accepting Response to GL 97-05, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206U1571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8451999-04-30030 April 1999 Rev 1, Submittal-Only Screening Review of Hope Creek Unit 1 IPEEE (Seismic Portion). Finalized April 1999 ML20206C8481999-04-22022 April 1999 SER Authorizing Pse&G Proposed Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B Pursuant to 10CFR50.55a(a)(3)(i) LR-N990157, Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced1999-04-12012 April 1999 Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced ML20205R5901999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Hope Creek Generating Station,Unit 1.With ML20205G6051999-03-19019 March 1999 SER Accepting Relief Request Re Acme Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components,Section Xi,Div 1 ML20205F8911999-03-18018 March 1999 Safety Evaluation Authorizing Licensee Requests for Second 10-year Interval for Pumps & Valves IST Program ML20204F7951999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Hope Creek Generating Station,Unit 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20202F6861999-01-26026 January 1999 Engine Sys,Inc Part 21 (10CFR21-0078) Rept Re Degradation of Synchrostat Model ESSB-4AT Speed Switches Resulting in Heat Related Damage to Power Supply Card Components.Caused by Incorrect Sized Resistor.Notification Sent to Customers ML18107A1871998-12-31031 December 1998 PSEG Annual Rept for 1998. ML20199E7271998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Hope Creek Generating Station,Unit 1.With ML18107A1881998-12-31031 December 1998 PECO 1998 Annual Rept. LR-N980580, Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With ML20198N4161998-11-12012 November 1998 MSIV Alternate Leakage Treatment Pathway Seismic Evaluation LR-N980544, Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with ML20155J9861998-10-31031 October 1998 Non-proprietary TR NEDO-32511, Safety Review for HCGS SRVs Tolerance Analyses LR-N980491, Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils LR-N980439, Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With LR-N980401, Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 1 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps LR-N980354, Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 1 ML20236E9491998-06-30030 June 1998 Rev 0 to non-proprietary Rept 24A5392AB, Lattice Dependent MAPLHGR Rept for Hope Creek Generating Station Reload 7 Cycle 8 ML18106A6821998-06-24024 June 1998 Revised Charting Our Future. ML18106A6681998-06-17017 June 1998 Charting the Future. LR-N980302, Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 1 ML20248C7381998-05-22022 May 1998 Rev 0 to Safety Evaluation 98-015, Extension of Allowed Out of Service Time for B Emergency Diesel Generator LR-N980247, Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 1 LR-N980196, Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML18106A5851998-03-0303 March 1998 Emergency Response Graded Exercise,S98-03. Nuclear Business Unit Salem,Hope Creek Emergency Preparedness, 980303 1999-09-08
[Table view] |
Text
- _ . _ _ _ - - - _ - _ . - _ . _ _ - - _ . - - _-- . - . - - - - - _ _ ._ - -- . .--
,M.:
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. AVERAGE DAILY. UNIT POWER LEVEL DOCKET NO.86-354 UNIT Hope Creek Gen. Station DATE 99/97/97' COMPLETED BY H. J en gy4 TELEPHONE (609) 339-5261 uly, 1987
.- MONTH DA1. AVERAGE-DAILY POWER LEVEL DAY- AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1023 997 3 37 906 18 988 .
2 943 3 19 582 20 967 4
977 5 21 984 863 6 22 1015 984 7 23 99 999 8 24 981 753 25 9
987 26 799 10 _
' 920 11 - . . _ _ _ _
27 ___n 992 12 28 968 991 13 29 947 325 14 30 9
15 31
.16 g B1 jog B7 J
p.
OPERATING DATA REPORT DOCKET NO. R6-354' UNIT 3r Hnpn Creek Gen. Sta. ]'
DATE O R /07 / 87 COMPLETED BY H_ aonnen OPERATING ~ STATUS
- 1. REPORTING PERIOD July 1987 GROSS HOURS IN REPORTING PERIOD 744 2.. CURRENTLY AUTHORIZED POWER LEVEL (MWt) 3291--
MAX. DEPEND.. CAPACITY (MWe-Net) 1061*
DESIGN ELECTRICAL RATING (MWe-Net) '1061-
- 3. POWER LEVEL TO WHICH RESTRICTED'(IF ANY) ( MWe-Ne t ) __ Nong_
4.- REASONS FOR RESTRICTION (IF ANY)
THIS YR TO MONTH DATE CUMULATIVE
- 5. NO. OF HOURS REACTOR WAS CRITICAL 7as 6 AA77.6 5165.6
- 6. REACTOR RESERVE SHUTDOWN HOURS n a a
- 7. HOURS GENERATOR ON LINE , 7n5 ? __4852 1 5140 3
- 8. UNIT: RESERVE SHUTDOWN HOURS _
n n n ]
- 9. GROSS THERMAL ENERGY GENERATED (MWH) 7 17n;soa la_mno ans y 1 s . 514. R13 19 ~ GROSS ELECTRICAL ENERGY GENERATED (MWH) 7mn;1n1 a ; AKR 10; __G 169.745
'11. . NET ELECTRICAL ENERGY GENERATED (MWH) A77,7a7 a . 6 6 0 . 9 41 4.946.415
- 12. REACTOR SERVICE FACTOR oa n 45 4 96.1
- 13. REACTOR AVAILABILITY FACTOR oa n on o 46_1
- 14. UNIT SERVICE FACTOR oA_n on a 49 6 c15. UNIT AVAILABILITY FACTOR oa n os a 45 6
- 16. UNIT CAPACITY FACTOR (Using Design MDC) 85.3_ _. RR o 86.2
- 17. . UNIT CAPACITY FACTOR (Using Design MWe) n5.1 _ nn o n6 7
- 18. ' UNIT FORCED OUTAGE RATE R 7 A A aa
- 19. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, & DURATION) :
Surveillance, 9/18/87, 16 days Refueling, 1/31/88, 55 days
- 20. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
N/A
- Estimated Value. Actual value to be determined in August 1987.
__---___--__-__a
OPERATING DATA REPORT UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.86-354 UNIT NAME Hope Creek Gen. Sta.
DATE 08/07/87 COMPLETED BY H. Jensen July 1987 (609)339-5261 REPORT MONTH TELEPHCNE
~
METHOD OF SHUTTING ,
I DOWN THE TYPE REACTOR OR F FORCED DURATION REASON REDUCING CORRECTIVE ACTION /
NO. DATE S SCHEDULED (HOURS) (1) POWER (2) COMMENTS I 8 7/0 3 F 0 B 5 Condensete Demineralized Bypass Operation i Test ;
i 9 7/2 1 F 0 B 5 Reactor Feed Pump Repairs. And Condensate i Demineralized
)
Bypass Operation Test I 10 7/30 F 38.8 H 3 Automatic Scram Incorrect Operation Of an Inverter By an equipment operator in ,
preparation for preventive f maintenance 4
SUMMARY
MONTELY OPERATING
SUMMARY
JULY 1987 l
Hope Creek entered the month operating at 100% reactor power. The' unit operated at essentially full load until July 3 when load was reduced to approximately 60% in order to perform a Condensate .
Demineralized Bypass Operation test. After test completion, power I was restored to 100%. On July 24 power was again reduced for Condensate Demineralized Bypass Operation testing. Reactor Feedwater Pump repairs also took place during this' reduction in power. Full power was restored on July.27.
After completing 150 days consecutive power operation, .an automatic reactor scram occurred on July 30. The' automatic scram was initiated by the incorrect operation of an inverter by an equipment operator in preparation for preventive maintenance on i the inverter. The reactor was started up on July 31 and went critical at 2136 of the same day.
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SUMMARY
OF CHANGES, TESTS, AND EXPERIMENTS l l
FOR THE IIOPE CREEK GENERATING STATION l 1
JULY 1987 1
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. i DfE DescriEt12D 91 DB21sn Chanqg Package HC-KE-002 This DCP added a steel Upending Stand for new fuel containers. The stand allows the i container to be placed in the vertical l position, enabling the fuel bundle to be raised ,
.out of the container. This DCP did not create !
a new safety hazard to the plant nor did it j affect the safe shutdown of the reactor. It did not change the plant effluent releases and ,
did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
4-HMM-86-0704 This DCP was a document-only change to update design drawings to reflect the actual as-built condition of Radwaste Heat Tracing. Updating the design documents did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor. This DCP did not change the plant effluent releases and did not alter the existing environmental impa.t.
Therefore, no unreviewed safety or environmental questions are involved.
4-HME-86-0759 This DCP reterminated wires at the DC Drive Panels so the Centrifuge Metering Pumps "A" and "B" in the Solid Radwaste system would operate as-designed. Reterminating the wires did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor.
This DCP did not change the plant effluent releases and did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
4-BMM-86-0904 This document-only change provided a mechanism for updating design documents to reflect the acceptance Class 2, SA312 Type 304/304H pipe i for use as Reactor Vessel Instrumentation i l
piping. Updating the design documents did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor.
This DCP did not change the plant effluent releases and did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
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DfE Descripi;1on of pagign Change PackAga 4-EMJ-87-0948 A design drawing incorrectly labeled manifolds ,
in the Residual Beat Removal system. This i document-only c)ange corrected the drawing error and did not create a new safety hazard to 1 the plant nor did it affect the safe shutdown l of the reactor. This DCP did not change the plant effluent releases and did not alter the existing environmental impact. Thereforef no unreviewed safety or environmental questions '
are involved.
4-EMJ-86-0951 This document-only change clarified notes on design drawings. The notes were misleading and could have led to misinterpretation of the operating characteristics of the Feedwater system. Clarifying the notes did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor. This DCP did not change the plant effluent releases and did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
4-EMJ-86-0969A This DCP corrected various legends, mimics, and nameplates in the Main Control Room to conform to design documents and to meet NUREG 0700 requirements. These deficiencies were discovered during an as-built walkdown.
Correcting these deficiencies reduced the probability of operator error and did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor.
This DCP did not change the plant effluent releases and did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
4-EME-86-0972 This DCP is a document-only change to identify installed thermocouple as duel element rather than single element. The thermocouple are located in the Residual Heat Removal Heat Exchanger loops. Upgrading the design drawings did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor. This DCP did not change the plant effluent releases and did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
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D.CE. Dggcription gf Design ChaDSR EasliaSR- .j 4-11CJ-86-133 0 This document-only change corrected discrepancies between Nuclear Boiler logic drawings. Upgrading the drawings did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor.
This DCP did not change the' plant effluent !
releases and did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
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Descript12D pf Temporary Modification Saf21Y EYAluat1OD Request 1111B.)_
87-0059 The Temporary Modification Request (TMR) associated with this Safety Evaluation added an Ion Chromatograph to the Balance of Plant Process Sample Panel to assist ,
Chemistry personnel in determining the !
source of the high conductivity and high sulfates in the Reactor Pressure Vessel.
The sample panel has no control functions or automatic actions associated with it and is used solely for chemical monitoring ,
of the Condensate, Feedwater, and Main !
Steam Systems. The addition of the Iron Chromatograph did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor. This TMR did not change the plant effluent releases and did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
87-0061 The Temporary Modification Request (TMR) associated with this Safety Evaluation added a temporary valve and a hose connection to the Solid Redwaste system.
This connection will supply flush water and seal water to the pumps from the Demineralized Water system rather than the Condensate Water s" stem. The modification will prever/ the Solid ,
Radwaste system .;. becoming '
contaminated during t. , test period.
Adding the valve and hose did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor. This TMR did not change the plant effluent releases and did not alter the existing environmental impact.
Therefore, no unreviewed safety or environmental questions are involved.
Safety Eyalpation Description of Temporary Modification Request (TMR) 87-0062 The Temporary Modification Request (TMR) associated with this Safety Evaluation replaced the Centrifuge Discharge Chutes in the Solid Radwaste system with metal flashing chutes with sight glasses. This modification allows observation of centrifuge discharge products during system testing and did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor.
This TMR did not change the plant effluent releases and did not alter the existing environmental impact.
Therefore, no unreviewed safety or environmental questions are involved.
87-0064 The Temporary Modifications Request (TMR) associated with this Safety Evaluation rewired a field terminal box so that it monitors a single tempera'ure c element in the Cooling Tower Basin instead of averaging all 4 temperature monitors.
Prior to the installation of this TMR, a wiring problem and 2 fr:lty elements led to an error of approximately 7' in the Control Room Integrated Display System computer. This TMR eliminated this error until a permanent design change can be implemented and did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor.
It did not change the plant effluent releases and did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
87-0065 The Temporary Modification Request (TMR) associated with this Safety Evaluation installed a temporary compressor to be uced as a backup to a Station Air Compressor during compressor maintenance.
The temporary installation of a backup compressor did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor. This TMR did not change the plant effluent releases and did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
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I Safety Evaluation Description af Deficiency Report (DR) 87-0057 This Deficiency Report identified a pinhole leak in a section- of Service Water piping. The Safety Evaluation authorized the repair of this pipe by welding a plate over the leak area. This plate will remain in place until the next available outage when either a basemetal weld repair will'be performed or the pipe will be replaced. The . pieces of equipment located closest to the leak are j the Safety Auxiliaries cooling System :
Pumps. The pumps have drip-proof motors f and. are mounted on pedestals to protect them during flooding. Therefore this 1 deficiency did not create a new safety hazard to the plant nor did it affect the safe shutdown of the~ reactor. 'It did not change the plant effluent releases and j did not alter the existing environmental impact. Therefore, no unreviewed safety or environmental questions are involved.
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87-0058 This Deficiency Report addresses the degradation of pipe wall thickness in the ;
Service Water piping elbows. immediately downstream of the Safety Auxiliaries Cooling System Heat Exchanger Balancing Valves. The Safety Evaluation authorized the' repair of this pipe by welding a plate over the affected areas. This plate i will remain in place until the next ,
available outage when either a basemetal weld repair will be performed or the pipe will be replaced. The pieces of equipment located closest to the affected areas are the Safety Auxiliaries Cooling System Pumps.
The pumps have drip-proof motors and are mounted on pedestals to protect them during flooding. Therefore this deficiency did not create a new safety hazard to the plant nor did it affect the safe shutdown of the reactor. The deficiency did not change the plant effluent releases and did not alter the existing environmental impact. Therefore, no unreviewe6 safety or environmental questions are involved.
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