ML20236B289

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Insp Rept 50-482/87-15 on 870601-0704.Violations Noted. Major Areas Inspected:Plant Status,Operational Safety Verification,Review of LERs,10CFR21 Rept Followup,Onsite Event Followup & Physical Security Verification
ML20236B289
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 07/10/1987
From: Bruce Bartlett, Cummins J, Hunter D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20236B276 List:
References
50-482-87-15, NUDOCS 8707290041
Download: ML20236B289 (14)


See also: IR 05000482/1987015

Text

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APPENDIX B  ;

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U. S. NUCLEAR REGULATORY COMMISSION

REGION IV

NRC Inspection Report: 50-482/87-15 LP: NPF-42

Docket: 50-482

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Licensee: Wolf Creek Nuclear Operating Corporation (WCNOC)

P. O. Box 411  ;

Burlington, Kansas 66839

Facility Name: Wolf Creek Generating Station (WCGS)

Inspection At: Wolf Creek Site, Coffey County, Burlington, Kansas

Inspection Conducted: June 1 to July 4, 1987

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Inepectors: M4Nd '

b'li444AxC6 0

' . /E. Cummins, Senior 1[esident Inspector, Date

perations

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(B. L. Bartlett, Residentm4

M4A

Reactor Inspector,

?-m-97

Date

Operations

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Approved: 7!20 /I 7

D. R. Hunter, Chief, Reactor Project Section B Date

Reactor Projects Branch

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8707290041 870722

PDR ADOCK 050DO482

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Inspection Sunmary

Inspection Conducted June 1 through July 4, 1987 (Report 50-482/87-15)

Areas Inspected: Routine, unannounced inspection including plant status,

operational safety verification, monthly surveillance ~ observation, monthly

maintenance observation, review of licensee event reports (LERs),10 CFR Part 21

report followup, onsite event followup, physical security verification,

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radiological protection, battery bank surveillance, independent reactor

l coolant system (RCS) leak rate measurement, and engineered safety features

(ESF)walkdown.

Results: Within the 12 areas inspected, two violations were identified '

(failure to comply with TS, paragraph 5; and-failure to perform a containment

purge system surveillance, paragraph 4). Two unresolved items are identified

in paragraphs 3.c and 5.

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DETAILS

1. Persons' Contacted

Principal Licensee Personnel

  • G. D. Boyer, Plant Manager
  • 0. L. Maynard, Manager, Licensing
  • C. M. Estes, Superintendent of Operations
  • M. D. Rich, Superintendent of Maintenance
  • M. G. Williams, Superintendent of Regulatory, Quality, and Administrative

Services

  • W. J. Rudolph, QA Manager-WCGS
  • A. A. Freitag, Manager, Nuclear Plant Engineering (NPE)

M. Nichols, Plant Support Superintendent

G. Pendergrass, Licensing

  • W. M. Lindsay, Supervisor, Quality Systems
  • C. J. Hoch, QA Technologist
  • K Petersen, Supervisor Licensing

E. Lehmann, NSE Engineer

  • J. Allen, NSE Engineer

The NRC inspectors also contacted other members of the licensee's staff

during the inspection period to discuss identified issues.

  • Denotes those personnel in attendance at the exit meeting held on July 9,

1987.

2. Plant Status

The plant operated in Mode 1 during the inspection period, except during

the time period described below:

On June 29, 1987, the reactor tripped from approximately 92 percent power,

when Main Feedi amp "A" tripped and the steam generator water levels

reached the Lo-Lo level reactor trip setpoint. The plant was returned to

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power operations in Mode 1 on July 1, 1987.

3. Operational Safety Verification

The NRC inspectors verified that the facility is being operated safely and

in conformance with regulatory requirements by direct observation of

licensee facilities, tours of the facility, interviews and discussions

with licensee personnel, independent verification of safety system status

and simiting conditions for operations, and reviewing facility records.

The NRC inspectors, by observation of randomly selected activities and

interview of personnel verified that physical security, radiation

protection, and fire protection activities were controlled.

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By observing accessible components for correct valve position and i

electrical breaker position, and by observing control room indication, the-

NRC inspectors confirmed the operability'of selected. portions of

safety-related systems. The NRC> inspectors also visually inspected safety

components for leakage, physical damage, and other impairments that could

prevent them from performing their designed functions. l

Selected NRC inspector observations are discussed below:

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On June 8,1987, at 3:20 p.m. (CDT) the licensee made a verbal report

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to the NRC duty officer per 10 CFR 50.72-(b)(1)(ii) concerning a leak

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rate test on the containment personnel airlock. The NRC inspector

reviewed Defect / Deficiency Report'(DDR)87-054 and LER 482/87-023 I

which stated that on June 1,- 1987, the personnel ~ airlock barrel 1

leakage test (STS PE-014A) failed to meet its ' leakage criteria. 'l

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At the time of the test, the leak rate was beyond the range of the

test instrumentation to measure and it was not until June 5, 1987,

that the leak rate was verified to be greater than 0.6 La by-

calculation.

At the time PE-014A failed, the shift supervisor (SS) was  ;

informed c a test deficiency as required by procedure; however, j

since'the was not informed that the leak rate was greater than '

O.6 La, the SS only entered TS 3.6.1.3 for an inoperable airlock,

failing to realize that he should have also entered TS 3.6.1.1

because of a lack of containment integrity. Because of a combination

of circumstances, the requirements:of TS 3.6.1.1 were incidentally'

complied with. The NRC inspector concluded that the licensee had

complied with the applicable TS requirement by chance rather than by

design. .

b. On June 14, 1987, at approximately 11:18 a.m. CDT licensee security

personnel reported to the control room that a loud rushing noise.was

coming from the hydrogen (H 2 ) skid. The H2 skid is located s

approximately 1000 feet north of the control room-and outside of the

protected area barrier (PAB).

H2 fires are not normally visible during daylight; however, the shift

supervisor (SS) could see a heat wave effect when viewing the skid on

the security cameras. The SS called out'the site fire brigade and

the City of Burlington Fire Department and then entered 0FF-Normal

Procedure OFN 00-016, " Fire Response."

The H2 bottles were sprayed with water to cool them and then the

affected bottle was isolated, terminating the H2 leak. Thw SS did

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not declare a Notification of Unusual Event (NOVE) because with the ,

wind out of the east, the release of flammable gas did not.present a  !

general hazard to other personnel or.the plant.  !

Due' to the high summer temperatures, the site fire brigade leader was

overcome with heat exhaustion and spent the night in the hospital; j

however, he returned to work the next day. 4

c. During a review of environmental qualification (EQ) of certain

equipment, the licensee's staff determined that the main steam

isolation valve (MSIV) nitrogen (N )2 accumulator pressure switches

were not properly EQ qualified. The switches are Barksdale

, Model BDB1T-A65SS. These switches were temporarily removed from the

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MSIV electr' al circuit pending further engineering review.

Engineering review determined that if these switches shorted to '

ground, a second ground would be-required to; affect MSIV operability

since it was a DC circuit. -The licensee is'considering the

desirability of future modifications to'these pressure switches

either to qualify them fully or to ensure that their failure would ';

not affect the rest of the valve in any'way. This will remain an

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unresolved item pending NRC issurance of enforcement guidance

(482/8715-03). 1

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d. On June 24, 1987, during a routine tour of the control room on i

backshift, the NRC inspector observed the supervising operator (50)

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studying a textbook while on duty. When questioned, the 50 stated

that the textbook was directly job related since' he _was taking the .,

course to satisfy NRC requirements for a shift technical advisor and' 1

studying was approved by his management. The NRC inspector informed {

, the 50 that NRC did not agree that studying was directly job related l

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but the NRC inspector would contact Region IV for guidance. On .

June 26, 1987, in a telecon Region IV informed the licensee that I

studying course textbooks while'on shift would not be in accordance .!

with Regulatory Guide 1.114, Revision 1, " Guidance On Being Operator i

At the Controls Of a Nuclear Power Plant." l

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l No violations or deviations were identified.

4. Monthly Surveillance Observation

The NRC inspectors observed selected portions of the performance of

surveillance testing and/or reviewed completed surveillance test

procedures to verify that surveillance activities were performed in

accordance with TS requirements and administrative procedures. The NRC

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inspectors considered the following elements while' inspecting surveillance

activities: .;

o Testing was being accomplished by qualified personnel in accordance

with an approved procedure. i

o The surveillance procedure conformed to TS requirements.

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o Required test instrumentation was calibrated,

o Technical Specification limiting conditions for operation (LCO) were

satisfied.

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o Test data was accurate and complete. Where appropriate, the NRC

inspectors performed independent calculations of selected test data

to verify their accuracy.

o The performance of the surveillance procedure conformed to applicable

administrative procedures,

o The surveillance was performed within the required. frequency and the

test results met the required limits.

Surveillance witnessed and/or reviewed by the NRC inspectors are listed

below:

l STS CR001, Revision 5, " Shift Logs for Modes 1, 2, and 3,"' performed on

May 31, 1987.

STS BB001, Revision 4, "RCS Water Inventory Balance," performed April 1

and 25, 1986, and May 9, 1987.

STS IC-640A, Revision 4 " Slave Relay Test K640A Train A Motor Driven

Auxiliary Feedwater Pump Start," performed on June 17, 1987.

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Selected NRC inspector observations are discussed below:

On July 1, 1987, the licensee determined that required TS

Surveillance 4.3.3.11 was not being adequately performed due to

Surveillance Procedure STS IC-275B, Revision 4, " Analog Channel  ;

Operational Test Containment Purge System Radiation Monitor GT RE-33,"

l which the licensee. c,ad established to accomplish this surveillance, was

l inadequate. Performance of STS IC-275B between October 1985 and

l October 1986 and December 1986 and July 1987 failed to demonstrate that

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automatic isolation of the containment purge pathway occurred when I

radiation monitor (GT RE-33) indicated measured levels above the Alarm / Trip

Setpoint as required by TS Surveillance 4.3.3.11. Between October and

December 1986, during refueling outage, the required surveillance was done

by Surveillance Procedure STS GP001, Revision 5, " Containment Penetration

Integrity Verification." Up to July 20, 1985, STS IC-275B contained

adequate instructions for verifying that the containment purge pathway was

isolated. Revision 3 to STS IC-2758, deleted these instructions from the

STS. The instructions were deleted as 'a part of the corrective action to

WCGS Defect / Deficiency Report No,85-105 which reported that Surveillance

STS 1C-275B, as it was then written, provided a flow path from containment

through the containment purge system to the environment without specifying

that this action required a release permit. .However, an alternata method

of demonstrating that the containment purge pathway automatically isolated

on a radiation monitor measured level above the Alarm / Trip Setpoint, as

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required by TS, was not provided. This is the third reported instance

where the licensee has failed to perform a TS required surveillance (see

NRC Violations 482/8541-03 and 482/8534-02) and is, therefore, an apparent

violation (482/8715-02), even though the licensee identified the problem.

5. Monthly Maintenance Observation

The NRC inspector observed maintenance activities performed on

safety-related systems and components to verify that these activities were

conducted in accordance with approved procedures, Technical

Specifications, and applicable industry codes and standards. The

following elements were considered by the NRC inspector during the

observation and/or review of the maintenance activities:

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o LCOs were met and, where applicable, redundant components were

operable.

o Activities complied with adequate administrative controls,

o Where required, adequate, approved, and up-to-date procedures were

used. .

o Craftsmen were qualified to accomplish the designated task and

technical expertise (i.e., engineering, health physics, operations)

was made available when appropriate.

o Replacement parts and materials being used were properly certified,

o Required radiological controls were implemented,

o Fire prevention controls were implemented where appropriate.

o Required alignments and surveillance to verify post maintenance

operability were performed.

l 0 Quality control hold points and/or checklists were used when

l appropriate and quality control personnel observed designated work

activities.

Selected portions of the maintenance activities accomplished on the work

requests (WR) listed below were observed and related documentation

reviewed by the NRC inspector:

No. Activity

WR 00702-87 Line No. 027 downstream of EJ-V033, below minimum wall

thickness

WR 02158-87 Hydro pressure may not have been adequate for repair

performed on WR 10370-85

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Selected NRC inspector observations are discussed below: J

During a routine review of WRs on June 23, 1987, the NRC inspector 4

developed questions concerning WR 02158-87. This WR had been written to )

resolve a quality first allegation concerning the test equipment I

configuration for a hydrostatic test. Licensee personnel stated that the j

analysis for WR 02158-87 had just been completed and due to test equipment  !

configuration that the hydrostatic pressure test performed for WR 10370-85 )

could not be verified to meet the code requirement.

WR 10370-85 was written to repair EF137-HBC?4 which is a section of I

safety-related, ASME Code Class 3, piping located immediately downstream )

of Valve EF V090. On September 8,1985, a small amount of water was  !

observed to be leaking from under the insulation and the repair was I

started on November 15, 1986. During the repair effort, the pipe was j

opened up and internal inspections revealed wall thinning due to erosion '

I caused by flow through a throttled butterfly valve. At that time, a base

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metal repair returning the minimum wall thickness to greater than

0.320 inches and a hard surface deposit was performed. As required by the l

code for through-wall repairs, a hydrostatic pressure test was performed; )

however, as stated above this test was later found to have been performed

at approximately 215 aounds instead of the required 224 pounds or greater.

In discussions with tle licensee, the NRC inspector became aware that the

licensee was apparently unaware of the TS surveillance requirement of

4.0.5.

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In a telecon on June 23, 1987, NRC gave verbal permission to WCN0C to

i delay performing a new pressure test, to meet code, until the next

refueling outage since the pressure test could not be performed without

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shutting down the unit. On June 24, 1987, the licensee informed the NRC

inspector that they had identified two other sections of safety-related

piping where code exemptions would be requested. Line Number EF-080-HBC-24

immediately downstream of Valve EF V058 and Line EJ032-HBC-18 immediately

downstream of Valve EJ V033 were below minimum wall thickness due to

erosion and would be repaired as required by the code; however, they could

not be tested per the code with the unit in Mode 1. Verbal permission was

given by NRC later that afternoon in a telecon~to wait until the refueling

outage to test or replace the piping.

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Valve EF V058 is the essential service water discharge valve from the

"A" train component cooling water heat exchanger, while Valve EF V090

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performs the same function on "B" train and has the same configuration as

EF V058. The licensee was unable to adequately explain their lack of

timely action to identify the wall erosion below EF V058 once the wall

erosion below EF V090 was identified.

This failure to comply with TS 4.0.5 and to notify the commission in

accordance with 10 CFR Part 50.55a(g)(5)(iii) is an apparent violation

(482/8715-01).

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When asked about TS 4.0.5, the licensee stated that they considered the

components fully operable, since they had not failed, even though the

components no longer met code.  ;

The question of whether the licensee should declare a component inoperable

immediately upon determination that it fails to meet ASME Code will remain

an unresolved item pending further NRC review (482/8715-04).

6. Review of Licensee Event Reports (LER) l

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During this inspection period, the NRC inspectors performed followup on  !

Wolf Creek LERs. The LERs were reviewed to ensure. j

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o Corrective action stated in the report has been properly completed or

work is in progress.

o Response to the event was adequate.

o Response to the event met license conditions, commitments, or other i

applicable regulatory requirements. l

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o The information contained in the report satisfied applicable i'

reporting requirements.

o Generic issues were identified.

The LERs discussed below were reviewed and closed:

LER 86-028-001: TS Violation-Due to RHR Inoperability j

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This LER was discussed in NRC Inspection Report 50-482/86-13 and concerns

the closure of one valve in one train of residual heat removal (RHR)

causing all of RHR to be inoperable. The licensee has written procedures

to define actions to be taken if the RHR system temperature increases

during a plant heatup due to checkvalve back leakage. This LER was made

required reading for licensed operators and to reduce the problem of

checkvalve back leakage, the time :: pan that the reactor coolant system is

maintained at lower pressures during startups is being reduced. This LER

is closed.

LER 86-034: Inoperable Containment Isolation Valve

During a containtaent isolation valve local leak rate test (LLRT), it was

discovered that tha total leak rate through one valve was greater than the

TS limit of 0.6 La due to a mispositioned handwheel. The inner containment

isolation valve was operable throughout the time that the outer.

containment isolation valve was mispositioned. This LER is discussed

further in paragraph 4. This LER is closed.

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LER 85-082: Engineered Safety Features (ESF) Actuation-Partial Loss of

Off-Site Power l

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Failure of a potential transformer in the 69 KV offsite power system j

caused the loss of offsite power to the 4160 V ESF Bus, NB01. Per design  !

Emergency Diesel Generator "A" started and picked up the ESF loads as they

were sequenced onto the NB01 bus. All ESF components functioned per

design and the plant continued to operate in Mode 1 at 100 percent power

during the event and the subsequent restoration. This LER is closed.

LER 86-062: Control Room Ventilation Isolation Signal (CRVIS)

Power leads to a chlorine monitor were lifted as a part of an isolation i

, clearance order. Lifting the power leads caused an unanticipated ESF

l actuation (CRVIS) which'is required to be reported to the NRC. -To prevent j

a reoccurrence, the licensee changed the administrative procedure for '

l clearance order control to include a step reminding personnel to conduct a

thorough review prior to removing equipment from service to identify

potential ESF actuations. This LER is closed, j

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7. 10 CFR Part 21 Report Followup j

The NRC inspector, by review of documents and discussions with licensee

personnel, verified that the 10 CFR Part 21 reports discussed below had

been reviewed and appropriately acted on by the licensee.

(Closed) P21-1987-87-18: Inoperability Due to Retainer Nut Problems With

Discs in Main Steam Line Check Valves

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The licensee determined that there were not any components supplied by  !

Schutte & Koerting Co. used at WCGS. ~WCGS does not use the dual check l

valve design in the main steam isolation valves (MSIV) that were reported  ;

in the Part 21. Anchor Darling dual disc gate valves were used at WCGS. l

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This information was documented in WCGS Industry Technical Information

Review and Evaluation (ITIP) No. 00359.

(Closed) P21-1987-87-20: 6" Model C Valve and Mercury Check-Devises

Failed to Open ]

The licensee has determined that WCGS did not use the Automatic Sprinkler

Corp. Model "C" Valver reported by this Part 21 to have a problem. This

information was documented in WCGS ITIP No. 00361.

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(Closed) P21-1987-87-38: After Being Energized for a Long Period a 130 V

DC Relay in the DG Control Circuit Failed to Drop Out Af ter Being

De-Energized

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The emergency diesel generators at WCGS were supplied by Colt Industries.

WCGS does not use the emergency diesel generators or the Square D Company

Class 8501, Type KPD13 relay reported in this Part 21 as having a problem.

This information was documented in WCGS ITIP No. 00389.

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8. Onsite Event Followup

The NRC inspectors performed onsite followup of nonemergency events that

occurred during this report period. The NRC inspectors reviewed control

room logs and discussed the events with cognizant personnel. The NRC

inspectors verified the licensee had responded to the events in accordance

with procedures and had notified the NRC and other agencies as required in

a timely fashion. The events that occurred during this report period are

listed in the table below. The NRC inspectors will review the LER for

each of these event and will report any findings in a subsequent NRC'

inspection report.

Date Event * Plant Status Cause 1

6/15/87 CRVIS Mode 1 Blown Fuse

(100 percent)

6/23/87 CPIS/CRVIS Mode 1 Technician Error

(100 percent)

6/29/87 Rx Trip Mode 1 Main Feed Pump Trip

(92 percent)

  • Event  !

CRVIS - Control room ventilation isolation

CPIS - Containment purge isolation

Selected NRC inspector observations are discussed belowf j

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The reactor trip which occurred on June 29, 1987, was caused by "A" main i

feedwater pump tripping which caused a reactor trip on Lo-Lo steam

generator water level. All ESF features equipment operated as designed.

Both NRC resident inspectors were in the control room during the trip and >

verified that operator actions were timely, well coordinated, and

appropriate to the circumstances. The NRC inspectors.will follow up and

review the LER for this event.

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No violations or deviations were identified.

9. Physical Security Verification

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The NRC inspectors verified that the facility physical security plan (PSP)

was being complied with by direct observation of licensee facilities and

security personnel.

The NRC inspectors by observation of randomly selected activities verified

that search equipment was operable, that the protected area barriers and

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vital area barriers were well maintained, that access control procedures

were followed and that appropriate compensatory measures were followed

when equipment was inoperable.

No violations or deviations were identified. H

10. Radiological Protection

By performing the following activities, the NRC' inspectors verified that J

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radiologically related activities were _ controlled in accordance with the

licensee's procedures and regulatory requirements:

o Reviewed documents such as active radiation work ~ permits and the- I

health physics shift turnover log.  ;

o Observed personnel activities in the radiologically ' controlled

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area (RCA)suchas: j

. Use of the required dosimetry equipment. -;

. " Frisking out" of the RCA. l

. Wearing of appropriate anti-contamination clothing where

required. .

o Inspected postings of radiation and contaminated areas.

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o Discussed activities with radiation workers and health physics ,

supervisors. l

No violations or deviations were identified.

11. Independent Reactor Coolant System Leak Rate Measurement

The NRC inspector verified the adequacy of the licensee's calculational

technique to determine the RCS leak rate and independently verified that

the RCS leak rates were within the TS limits. Using the Computer-

Program RCSLK9 supplied by NRC, the NRC inspector updated the plant

parameter list to reflect Wolf Creek specific numbers and then taking data-

from leak rate. surveillance previously performed by the licensee ran the

RCSLK9 program. Comparing the results of the RCSLK9 program to the  !

licensee's surveillance, the difference was less than 0.2 gpm.

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No violations or deviations were identified.

12. Battery Bank Surveillance u

On June 19, 1987, the licensee's staff was performing a routine review of

surveillance procedures and discovered that STS MT-019, Revision4, "125 V

DC Class 1E Quarterly Battery Inspection," performed on November 8,1986, ,

failed to meet its TS criteria, yet, the associated action statement was

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not entered. The licensee's review showed that when STS MT-019 was  !

performed on November 8,1986, that the average compensated specific 1

gravity for Battery Bank NK11 was 1.199 and for NK13 was 1.205 which were

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below the TS limit of greater than 1.205 for all connected cells. -

TS 3.8.2.2 requires that as a minimum 125-volt Battery Bank NK11 and NK13 q

and its associated full capacity chargers NK21 and NK23 or Battery i

Bank NK12 and NK14 and their chargers be operable in Modes 5 and 6. On

November 8 and 10, 1986, at 12:25 a.m. (CST) refueling commenced and the j

unit entered Mode 6. Since TS 3.8.2.2 allows one train of vital DC to be i

inoperable in Modes 5 and 6, there was not a TS violation at that time;

however, on November 16, 1986, at 11:19 a.m. the licensee deenergized

Bus NB02 making B train vital DC sources inoperable and should have ,

entered the action statement to TS 3.8.2.2, which among other things l

prohibited core alternations. On November 17, 1986, at 3:05 a.m. Bus NB02

was reenergized.

Further licensee review has shown that while Battery Banks NK11 and NK13

were at all times capable of performing their design functions, it  ;

was not until January 10, 1987, that STS MT-019 was reperformed proving  :

that the battery banks were fully operable. On December 11, 1986, the

unit entered Mode 4 with battery banks inoperable in violation of TS.

This violation of TS was identified by the licensee corrective actions j

have been taken to prevent recurrence, and it was not a violation that i

could reasonably be expected to have been prevented by the licensee's

corrective action for a previously identified violation. However, similar

violations have been previously cited. -Violation 482/8628-01 issued

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December 22, 1986, stated that on November 24, 1986, STS MT-016,

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Revision 3 " Standby Diesel Generator Inspection," performed on

! November 1,1986, was noted to have not been signed off by the test

performer, the supervisor, or the quality control supervisor / lead as

required. Violation 482/8632-01 issued March 13, 1987, stated that on

,l December 5, 1986, STS MT-019 performed October 16, 1985, was noted to have

I average specific gravity out-of-limits which the reviews failed to

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identify or take corrective action. While these violations were

identified after STS MT-019 was performed on November 8,1986, their

corrective actions would not have corrected this violation. This failure

to properly review completed STSs and identify out-of-specification data

shows a lack of attention to detail. The NRC inspectors will continue to

follow the licensee's corrective actions to verify their adequacy to

ensure that surveillance performed in the future are adequately reviewed.

13. Engineered Safety Features System (ESF) Walkdown

The NRC inspectors verified the operability of ESF systems by walking down

selected accessible portions of the systems. The NRC inspector verified

valves and electrical circuit breakers were in the required position,

power was available, and valves were locked where required. The NRC

inspectors also inspected system components for damage or other conditions

that could degrade system performance.

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The ESF system walked down during this inspection period and the documents

utilized by the NRC inspectors during the walkdown are listed below:

System Documents

Auxiliary Feedwater System (AL) Drawing M12AL01(Q), Revision 0, " Piping

and Instrumentation Diagram Auxiliary

Feedwater System"

Checklist (CKL) AL120, Revision 10

" Auxiliary Feedwater Normal Lineup"

SYS AL-120, Revision 6, " Feeding Steam-

Generators With a Motor Driven or Steam

Driven Auxiliary feedwater Pump"

No violations or deviations were identified.

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14. Unresolved Item  !

Unresolved items are matters about which more information is required in

order to ascertain whether they are acceptable items, items of

I noncompliance, or deviations. Two unresolved items disclosed during the

inspection are discussed in paragraphs 3.c and 5.

15. Exit Meeting

The NRC inspectors met with licensee personnel to discuss the scope and

findings of this inspection on July 9, 1987.

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