ML20235R909

From kanterella
Jump to navigation Jump to search
Special Rept 89-003:on 890201-02,RCS Sample Data Indicated Specific Activity Exceeded 0.8 Uci/Ml I-131 Limit.Caused by Normal Increase in Iodine Activity After Power Reduction. Isotopic Analysis Continued Until Restoration Complete
ML20235R909
Person / Time
Site: Rancho Seco
Issue date: 02/27/1989
From: Keuter D
SACRAMENTO MUNICIPAL UTILITY DISTRICT
To: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
89-03, AGM-NPP-89-062, GL-85-02, NUDOCS 8903030474
Download: ML20235R909 (6)


Text

,.

i 1 $SMUD SACRAMENTO MUNICIPAL UTILITY DIS 1RICT C 6201 S Street. P.o. Boo ?.3830, Sacramento CA 95852 1830,(916) 452 3211 AN ELECTRIC SYSTEM SERVING THE HEART OF CALIFORNIA i

AGM/NPP 89-062 Feburary 27, 1989 U. S. Nuclear Regulatory Commission Attn:

J. B. Martin, Regional Administrator j

Region V 1450 Maria Lane, Suite 210 Halnut Creek, CA 94596 i

Docket No. 50-312 l

Rancho Seco Nuclear Generating Station License No. DPR-54 l

SPECIAL REPORT NUMBER 89-03:

FAILURE TO HAINTAIN SPECIFIC ACTIVITY OF THE PRIMARY SYSTEM HITHIN ADMINISTRATIVE LIMITS

Dear Mr. Martin:

I The specific activity of the primary system exceeded the administrative limits specified in Rancho Seco Administrative Procedure RSAP-0222 and as committed to in our response to Generic Letter 85-02.

The Sacramento Municipal Utility District hereby submits Special Report No. 89-03 in accordance with Rancho Seco adminir.trative controls.

Members of your staff with questions requiring additional information or clarification may contact Mr. Jim Clark at (209) 333-2935, extension 4378.

l Sincerely, V

n Dan R. Keuter Assistant General Manager Nuclear Power Production Attachment cc w/atch:

A. D'Angelo, NRC, Rancho Seco Document Control Desk, Washington DC 8903030474 090227 N

PDR ADOCK 05000312 S

PNU

)(

l RANCHO SECo NUCLEAR GENERATING STATloN O 1444o Twin Cities Road, Herald, CA 95638-9799;(209) 333 2935

i l

SPECIAL REPORT NUMBER 89-03 Failure to Maintain Specific Activity of the Primary System Within Administrative Limits Date of OccurleAtt i

February 1 - 2, 1989 Plant Conditions at Time of Occurrence l

Hot to Cold Shutdown.

l l

Identification of Occurrence The specific activity of the primary system exceeded administrative l

limits as specified in Rancho Seco Administrative Procedure RSAP-0222, i

l Rancho Seco Chemistry Control Commitment.

The procedure requires the j

l submission of a Special Report if the specific activity of the primary coolant is either greater than 0.8 pCi/mi I-131 or 43/E pCi/ml.

Description of Occurrence l

For the period from approximately 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> on February 1 to 1015 hours0.0117 days <br />0.282 hours <br />0.00168 weeks <br />3.862075e-4 months <br /> on February 2, while in a hot then cold shutdown condition, Reactor Coolant System sample data indicated that specific activity was above 0.8 pCi/ml I-131; the 43/E limit was not exceeded.

It is normal for t

iodine activity to increase for a short period of time after a power reduction.

The District had committed to the 0.8 pCi/ml I-131 limit via letter dated June 11, 1985, in response to Generic Letter 8S-02.

I Corrective Action Taken In accordance with RSAP-0222, on detection of the unusual condition, isotopic analysis continued until restoration of specific activity to within limits.

The analysis performed on February 2 at 1015 hours0.0117 days <br />0.282 hours <br />0.00168 weeks <br />3.862075e-4 months <br /> j

indicated that specific activity was below 0.8 pCi/ml I-131.

Per RSAP-0222 the following information i: attached:

Primary coolant specific activity and time duration when the activity exceeded 0.8 pCi/ml I-131 (Attachment 1).

Reactor power history starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the first sample in which the limit was exceeded (Attachment 1).

Cleanup flow history starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the first sample in which the limit was exceeded (Attachment 2).

I

i SPECIAL REPORT NUMBER 89-03 Failure to Maintain Specific Activity of the Primary System Nithin Administrative Limits Corrective Action Taken (Continued)

History of degassing operations, if any, starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the first sample in which the limit was exceeded.

(No data is l

attached for this item because degassing operations were not performed during the period I-131 specific activity exceeded the limit.)

Fuel burnup by core region (Attachment 3).

\\

SPECIAL REPORT 89-03 Failure to Maintain Specific Activity of the Primary System Hithin Administrative Limits POWER LEVEL PARAMETER DATE/ TIME

(% Full Power)

VALUE I-131 28-Jan-89 00:25 92.0 0.142 pC1/ml l

l 29-Jan-89 01:15 92.0 0.14 pCi/mi 30-Jan-89 00:05 92.0 0.147 pCi/ml 31-Jan-89 00:10 92.0 0.157 pCi/ml 01-Feb-89 00:05 40.0 0.218 pCi/ml 01-Feb-89 05:00 0.0 1.75 pCi/ml 01-Feb-89 08:30 0.0 1.72 pCi/ml

-)

01-Feb-89 11:00 0.0 1.69 pCi/ml 02-Feb-89 02:10 0.0 1.47 pCi/mi l

02-Feb-89 10:15 0.0 0.655 pCi/ml l

l l

l 1

l l

l

__---.-__-___.t__

SPECIAL REPORT 89-03 Failure to Maintain Specific Activity of the Primary System Hithin Administrative Limits PARAMETER DATE/ TIME VALUE LETOOWN 27-Jan-89 01:45 75 GPM FLOH 28-Jan-89 00:25 75 GPM 29-Jan-89 01:15 75 GPM 30-Jan-89 00:05 75 GPH 31-Jan-89 00:10 75 GPM 01-Feb-89 00:05 75 GPM

\\

02-Feb-89 02:10 55 GPM 03-Feb-89 01:50 55 GPM 04-Feb-89 01:10 55 T?M 04-Feb-89 01:10 55 GPM

SPECIAL REPORT 89-03 i

Failure to Maintain Specific Activity of.the Primary System Within Administrative Limits BURNUP BATCH #

  1. OF ASSEMBLIES (HHD/HTU) lE 1

21,983 SC 8

29,746 68 16 30,013 l

7 32 26,093 I

8A 24 19,584 8B' 40 19,132 9

56 8,104 CORE AVERAGE - 18,442 HHD/HTU i

_ _ _ _ _ _ _ -. _ _ _ _