ML20215D751

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Special Testing Insp Repts 50-327/87-18 & 50-328/87-18 on 870316-27 & 0413-17.Violations Noted:Failure to Ensure Test Procedures & Instruction Contained Necessary Requirements & Performed Per Requirements
ML20215D751
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 05/12/1987
From: Hooks K, Konklin J, Lloyd R, Stein S
NRC OFFICE OF SPECIAL PROJECTS
To:
Shared Package
ML20215D725 List:
References
50-327-87-18, 50-328-87-18, NUDOCS 8706190131
Download: ML20215D751 (17)


See also: IR 05000327/1987018

Text

.

U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF SPECIAL PROJECTS

Report Nos.:

50-327/87-18 and 50-328/87-18

Licensee: Tennessee Valley Authority

,

6N 38A Lookout Place

1101 Market Street

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Chattanooga, Tennessee 37402-2801

Facility Name:

Sequoyah Units 1 and 2

Docket Nos.

50-327 and 50-328

License Nos.

DPR-77 and DPR-79

Inspectors:

5/12/f7

i

E. Konklin, Team Leader

Date Signed-

LAM

es arr

K.

Hooks, Assistant Team Leader

Fat'e Si'gned

afY

Shh7

,

R. L.

yd, Mel:hp6'

ipline Lead

Date Signed

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_

$W2 ] ~

'

%. R. Stein, Electrical Discipline Lead

Date Signed

-1

Consultants:

R. Compton and M. Juister (Mechanical)

i

D. Ford and M. Good (Electrical)

Approved By:

f/fE/T7

/TeamSupport&IntegrationSection

mes E. Konklin, Chief

Difte Signed

SUMMARY

Inspection on March 16-27, 1987 and April 13-17, 1987.

(

Areas Inspected:

This special announced testing inspection was conducted in

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the area of post-modification testing, and included review of test procedures

and test results, observation of work activities associated with functional

<

and surveillance testing, review of system evaluation reports associated with

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the Design Baseline Verification Program (DBVP), and a review of the

separation of electrial circuits.

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"

8706190131 870610

PDR

ADOCK 05000327

G

PDR

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Results:

In the areas inspected, one violation was identified with regard to

the control of post-modification testing.

The examples included in the viola-

tion are discussed in Sections 4 and 5 of the report.

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REPORT DETAILS-

1.

Key Licensee Personnel Contacted

NAME

ORGANIZATION

J. Dorris

Design Basis Verification Program (Electrical)

  • 6T. Flippo

Quality Surveillance Supervisor

  • 6T. Hughes

DNE Principal Electrical Engineer

GN.'Kazanas

Director, Nuclear QA

  • G. Kirk

Compliance Licensing Manager

C. Lagasse

Craft Foreman

9J. LaPoint

Deputy Site Director

  • R. Mooney

Systems Engineer Supervisor

G. Newman

Electrical Craft Superintendent

D. Peters

Modification Supervisor

  • 6M. Purcell

Licensing Engineer

  • sA. Qualls

-Plant Manager'(on detail'to SQN)'

  • H. Rankin

Project Manager

  • M. Sedlacik

Modification Group A Supervisor

  • J. Staub

DNE Electrical Engineering Branch Supervisor .

E. Steinhauser

Design Basis Verification Program (Mechanical)

  • R. Stockton

Modification Group A Engineering Supervisor

Other licensee employees were contacted, including supervisors, operators,

shift engineers, electricians, and maintenance personnel.

The NRC

resident inspection staff was represented at both exit meetings.

  • Present at exit meeting on March 27, 1987.

9 Present at exit meeting on April 17, 1987.

2.

Followup on Previously Identified Items

The inspectors reviewed two unresolved items at the request of the

resident inspector,

a.

(Closed) 327,328/86-08-08: This item concerned WP 12365, which was

issued to replace Cable 2V2451A to 2-FCV-68-333, for ampacity con-

siderations.

The cable was routed from the Reactor MOV Board 2Al-A,

Panel 9D to Penetration 15 at Azimuth 101 on the 693 level.

FCR 5142

was written to correct cable routing cards since the work plan

required the cable to change trays.

The tray change was not speci-

fied on the routing cards that were prepared to support the work

plan.

The installation was inspected by the NRC inspectors in the

480 Board Room 2A and the Unit 2. Mechanical Equipment Room in the

Auxiliary Building. The cable was routed from Tray HT-A, Node 126 to

Tray HU-A, Node 123 in the Mechanical Equipment Room and then from

.HU-A, Node 122 back to Tray HP-A, Node 127.where'it connects with

Tray HT-A in the 480 Board Room 2A.

The trays were separated by

about 12 inches vertically and the cable routing was appropriate.

No

deficiencies were noted. This unresolved item is closed.

f

b.

(0 pen) 327,328/86-49-06: This open item concerned potential cable

tension and tension on cable terminations in the control room because

of long vertical runs of Flamemastic coated bundled cables in the

cable spreading room. The inspectors found no problems with the 68

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cables that were inspected in the risers of control room panels. All

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cables had adequate slack, and the terminal lug to wire connections

were not under tension.

During the inspection, it was found that TVA

is conducting an independent review of an employee concern in this

area. Therefore, this item was not closed by the inspectors.

1

3.

Scope of Inspection

The inspection team reviewed selected documents which specified test

requirements, including seven surveillance instructions (sis), ten

maintenance requests (MRs), four workplans (WPs), and two technical

instructions (tis). The inspectors also observed testing activities and

verified the reporting of test results for a total of twelve functional

tests, ten surveillance tests and two instrument calibration tests.

In

addition, two safety-related cable pulls and the makeup of six Raychem

splices were observed.

In conjunction with the above test inspection activities, the inspectors

also reviewed sixteen system evaluation reports generated by TVA as part

of the Design Baseline Verification Program (DBVP), and inspected a sample

of 75 cables in the control room and the auxiliary building for potential

secondary bridging violations. The results of the system evaluation

report review are discussed in Section 6 of this report.

The inspection

of cables for secondary bridging is discussed in Section 7.

4.

Electrical Inspection Results

The NRC inspectors monitored the performance of selected plant functional

and surveillance tests in the areas of electrical and instrumentation

modifications.

Sequoyahworkrequestpackages(WRs)providethebasic

criteria for the component or system modifications and functional testing.

Surveillance tests are generally accomplished in accordance with appli-

cable surveillance instructions. Tests asse sated with five WRs were

observed. The review of the WRs concentrav.d on the functional testing

aspects of the packages.

In addition, functional tests associated with

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selected modification workplans (WPs) and maintenance requests (MRs) were

reviewed and observed.

The observation of functional testing by the NRC inspectors indicated that

weaknesses exist in the licensee's testing program.

Based upon the

deficiencies observed, the NRC inspectors concluded that Sequoyah func-

tional testing associated with MR/WR work activities lacked sufficient

controls to assure that modified components are tested for full perform-

ance of their intended functions.

In the foliowing sections a brief

description of each test is provided along with the inspectors' observa-

tions regarding the adequacy of associated test documentation, test

performance and test results evaluation.

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a.

Functional Testing of CVCS Valves.

WRs B217164 and B217156 details instructions for the functional test

of Chemical and Volume Control System (CVCS) Letdown Isolation Valves

2-FCV-62-69A and 2-FCV-62-70A.

Testing of these components was

required because of the modification of existing system circuits

to facilitate the replacement of Raychem splice materials. Addi-

tionally, surveillance testing of valve stroke and timing was per-

formed in accordance with Sequoyah Surveillance Instruction (SI)

166.6.

The functional tests were performed by operating the valves from

Local Control Stations 1361-8 and 1365-B.

Indicating lights were

observed to verify valve travel to the " fully open" and " fully

closed" positions.

The inspectors' review of the above WRs verified that functional

testing had been performed in accordance with requirements.

Valve

positioning and confirmation of associated relay pickup were accom-

plished as specified in the WR test instructions.

Surveillance

testing was accomplished through remote signal initiation from the

indicating switches located in the control room.

Test results

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indicated that timing and valve stroke data were in compliance with

the criteria specified in SI 166.6

No deficiencies were identified during performance of this test.

However, the inspectors noted that over 50 percent of the indicating

lights located in Local Control Stations 1361-B and 1365-B were

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broken, missing or burned out.

To perform the functional test, the

cognizant engineer provided the required indicating lights by remov-

ing bulbs from other local control stations in the area. Although

this method of replacement accommodated the needs of the specific

test, it is poor test practice.

Faulty or missing bulbs should be

replaced with new bulbs to assure adequate indication at all control

stations.

b.

Functional Testing of Containment Isolation Valves.

WRs B219442 and 8219444 provided instructions for the functional

testing of solenoid-operated Containment Vacuum Relief Isolation

Valves 2-FSV-30-46A and 2-FSV-30-468.

Testing of these components

was required because of the modification of existing system circuits

to facilitate replacement of Raychem splice materials.

Functional

and surveillance tests were performed by the cognizant engineer and a

reactor operator using the remote indicating switches located in the

control room.

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During the observation of the functional test the inspectors identi-

fied the following concerns:

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1.

The WR package contained formal instructions which detailed the

steps required for successful completion of the functional

test.

Several handwritten changes had been made to the approved

test package; specifically, the annotation of splice and test

instructions without signatures, initials or subsequent approvals

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as required by Sequoyah Procedure SQM-2 " Maintenance Management

System."

2.

Step 1 of the functional test instruction for each of the two

containment vacuum relief isolation valves incorrectly speci-

fied that the valve solenoid actuator should be de-energized

when the valve is placed in the fully closed position. The NRC

inspector's review of applicable TVA Schematic 45N630-10 indi-

cated that the solenoid should energize at valve closure.

Consequently, the test instruction provided information which

conflicted with approved design documents and which was techni-

cally incorrect.

3.

Following completion of the functional test, the inspector

reviewed the test instruction and schematic with the cognizant

engineer and discussed the conflict noted above.

The cognizant

engineer later modified the approved test instructions by elimi-

nating portions of Steps 1 and 2 in order to reflect actual test

results. This action is contrary to the requirements of the

controlling procedure, SQM-2, and indicates a lack of

familiarity with plant administrative requirements.

These examples of changes to approved test packages without required

reviews, inclusion of incorrect requirements in a test instruction,

and after-the-fact changes to a test instruction to reflect the test

results, indicate a lack of test control as required by Criterion XI

of 10 CFR 50 Appendix B (50-327/87-18-01; 50-328/87-18-01).

c.

Functional Testing of CVCS Isolation Valve 2-FCV-62-91A.

WR 219655 details instructions for the functional test of valve

2-FCV-62-91A. Testing of this component was required because of

modification of existing system circuits to facilitate the replace-

ment of Raychem splice materials.

No deficiencies were observed in

this area.

d.

Inspection of Damper Covers for the Fifth Vital Battery.

WP 10968 included the manufacture and installation of two ventilation

damper covers associated with the installation of the fifth Vital

Battery.

No deficiencies were noted.

e.

Phase Testing and Motor Bump Tests for the Component Cooling System

Swing Pump.

WP 12337 covered the replacement of cables from the switchgear to the

component cooling swing pump for both the normal and alternate power

supplies.

Inspectors observed the phase testing at the normal /

alternate power transfer switch, lead makeup, and the motor bump test

at the swing pump. The motor had been decoupled from the pump as a

precaution to prevent potential reverse rotation of the pump during

the motor bump tests should the wiring be in error. The following

concerns were identified by the inspectors:

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1.

Phase checking of the normal supply to the motor could not

initially be accomplished since the transfer switch normal

supply breaker would not close.

The breaker mechanism would not

engage with the handle. The breaker was finally closed by

manipulating the interlock mechanism behind the breaker. A

review of WR B127722, which was posted on the breaker, indicated

that repair of the breaker mechanism was a priority one work

request that had been outstanding for six months.

During phase checking of the alternate transfer supply, the

alternate transfer switch breaker could not be closed without

immediately tripping.

Investigation revealed that the remote

switches were misaligned.

This also occurred during attempts to

shut the alternate supply breaker at the 480 VAC switchboard.

The apparent cause was that the test procedure in the work-

plan was not detailed enough to specify a proper switch align-

ment prior to shutting off the alternate supply breaker and the

transfer switch breaker. The test discrepancy was not recorded

by test personnel.

2.

During motor bump tests the swing pump motor was inadvertently

started and ran for approximately 20 seconds until it was

secured by test personnel with the local control pushbuttons at

the motor. The inadvertent start of the decoupled motor threw

potentially contaminated grease from the coupling outside the

contamination zone onto two personnel observing the test.

Although no personnel were injured, the potential for personnel

injury existed because of the close proximity of personnel to

the motor / pump coupling. The apparent cause was that the test

procedure was inadequate.

No other deficiencies were noted.

The examples of inadequate procedural requirements, and a failure to

record a test discrepancy, discussed above, are considered to be

further examples of a lack of proper test control, as designated in

Section 4.b above.

f.

Calibration of Upper Head Injection System Level Setpoint Switches.

WP 12385 involved removing level switch channel modules from the

control room, conducting a channel calibration in the instrument

shop, replacing the modules and then conducting a "zero" and " span"

adjustment in the system.

The calibration was conducted on two BLH

Electronics Tranducer Indicators (Model 450). Transducer input was

simulated with a Precision Calibrator Model 625, Serial 435659, and

power supply checes were done using a Fluke 8600A digital multimeter

Serial Number 432927. All test instruments were in calibration.

Power supply checks were also observed. The module was warmed up but

did not stabilize, indicating a problem with the module.

The power

supply leads and cables were checked by test personnel, but no

problem was foun,i. The calibration was later run satisfactorily on

the same module. A loose cable was suspected, however, no root cause

of the problem wis dets mined and the problem was not logged on the

work plan. No otaer deficiencies were noted.

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g.

Functional Testing of Safety Injection Valves.

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The inspectors observed. functional and stroke timing tests on Boron

Injection Tank Isolation Valves 2-FCV-63-25, 2-FCV-63-26,.2-FCV-63-39

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and 2-FCV-63-40. The functional tests were completed under

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Maintenance _ Request Packages B219665 through B219668. Stroke timing

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tests were conducted using SI 166.4.

The functional test was con-

trolled from the Control Room and involved mid-positioning each

valve, applying power to the valve and ensuring it did not move,

cycling the valve from the local control station and observing proper

operation, and then performing the stroke timing test from the

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control room. The Senior Reactor Operator decided to complete the

test one valve at a time since the valves were the only normally-

closed valves between the charging pumps and the reactor vessel. The

following was observed by the NRC inspectors during the testing:

1.

Three of the four Boron Injection Tank isolation valves were

energized prior to placing the valves in the mid-position. This

was contrary to the signature-verified steps in the functional

test procedure.

3

2.

The Senior Reactor Operator operated one valve with a hold order

tag still attached to the valve control switch in the Control

Room.

3.

Steps in the functional test procedure were not signed off as

each step was completed, which may have contributed to the

procedural violations identified above.

These examples of failure to follow procedures are considered to be

further examples of a lack of test control, as designated in Section

4.b above.

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h.

Installation of Raychem Splices at Penetration No. 37.

4

Raychem splices were installed on four conductors of Cable 2V55998-

under MR 8217399.

The splices were installed at Penetration No. 37

(inboard containment penetration). The conductors had been pre-

viously prepared for splicing by a different work package.

During

installation, a butt connector was installed on the wrong lead for

one conductor but was promptly recognized by the electrician and a

quality control inspector. Work was stopped while a new connector

was obtained. After certification of the new connector by the

quality control inspector, the job was satisfactorily completed. No

deficiencies were noted.

1.

Functional and Stroke Timing Test of Reactor Building Instrument

Room Air Conditioning Isolation Valve.

A functional and stroke timing test of the Reactor Building Instru-

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ment Room Air Condition Isolation Valve, 2-FCV-31C-232, was conducted

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under WR B212284. Two-way radio communication between the Control

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Room and the remote station during the test was marginal and resulted

in having to. stroke the valve three times in order to properly time

the valve for the test.

No deficiencies were noted.

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j.

Observation of Spent fuel Pump Motor Bump Test.

WP 12424 replaced the power cable to the Spent Fuel Cooling System

Pump because of ampacity considerations. At the time of this inspec-

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tion, the new cable had been routed in the raceway but had not yet

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been terminated at the motor.

The motor bump test was conducted

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with the original power cable to determine correct motor rotation

to assure proper phase connection when the new cable is connected to

the motor. This was being done because the test procedure called

for a motor bump test or for observation'of a permanent rotation

indicator on the motor and pump assembly, and test personnel were

unaware that an indicator existed. However, during setup for the

test, the test engineer found a permanent direction arrow on the

pump which made the motor bump test unnecessary.

No deficiencies

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were identified.

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k.

Functional and Stroke Time Test of the Upper Head Injection Test

Line Isolation Valve.

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A functional and stroke time test of the Upper Head Injection Test

Line Isolation Valve, 2-FCV-87-8 was conducted under WR B217159. The

functional test and stroke timing test were conducted satisfactorily,

except that signature steps were not signed off as each step was

completed. All steps were signed off after the entire test had been

done.

No deficiencies were noted.

1.

Functional and Stroke Time Test of the Containment Standpipe

Isolation Valve.

A functional and stroke timing test of the Containment Standpipe

Isolation Valve 2-FCV-26-240 was conducted under WR B219647. Motor

leads were meggered prior to the functional test. The tests were

specified because of replacement of the Raychem splices on the motor

leads. The functional test involved hand cranking the valve to the

mid-position, applying power to the valve and ensuring that it did

not move, cycling the valve from the local control station, and then

performing the stroke timing test from the local control station.

During the testing, the inspectors identified the following discrep-

ancies:

1.

The indicator dial on the valve was used to mid-position the

valve; however, the indicator dial on the valve was misaligned

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by about 180 degrees.

Consequently, the dial indicated about 65

percent when open, through "0" to about 63 percent when shut.

The functional test procedure did not specify what indication to

use when mid-positioning the valve.

2.

Valve indicator lights on the local control panel (Box 2921

Train A) did not work when power was applied to the valve.

Investigation by the Auxiliary Unit Operator found that more

than half of the bulbs on that panel were missing or broken.

Bulbs from other valves were scavenged to complete the test.

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This is a further example of the poor test practice noted in

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Paragraph 4'a above.

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3.

The functional test procedure did not specify how to check that

the valve was full open after it had been stroked from the local

control panel.

The test had separate acceptance criteria for

" valve goes full open."

The above cases of inadequate procedural requirements for determining

valve mid-position and for checking the valve full-open position are

considered to be further examples of lack of proper test control, as

designated in Section 4.b above.

During observation of the test the inspectors noted improper thread

engagement on four body to bonnet bolts on the safety-related valve,

and one missing limit switch cover. A number of installation dis-

crepancies were also noted on other modifications associated with

recent valve work.

Some specific deficiencies noted included loose

fittings on Cables 2M24-668, 2M24-678, 2M24-68B, 2M24-728, and

2M24-758 to the Containment LOCA H2 Detector at the 734 level; and,

in the 690 level pipe chase, loose or missing conduit straps between

Valves 2-FCV-26-240, 2-FCV-62-63 and 2-FCV-77-10; loose conduit

.'

connectors on Valves 2-FCV-63-156, 2-FCV-77-10, 2-FCV-63-8, 2-FCV-63-40,

2-FCV-70-85, 2-FCV-72-41, 2-FCV-43-69, 2-FCV-63-44, and 2-FCV-26-240;

a conduit run partially blocking a handwheel on Valve 2-FCV-70-92;

broken flexible conduit on Valve 2-FCV-26-245, missing LB box covers

near Valve 2-FCV-77-20, near a Boron Injection Tank, and on cable to

2-TIS-63-36; missing bolts on a safety-related transmitter (2-PT-63-35)

body to mounting plate, and on the transmitter mounting plate to Wall

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Bracket 2-L-346; and missing hangers on rigid conduit to Valve

2-FCV-26-240.

These discrepancies were brought to the attention of-

appropriate licensee personnel.

m.

Cable Installation.

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The inspectors observed the in-process installation of safety-related

cable 2PL4957A. The installation was specified by WP 12392 to

facilitate the replacement of an existing cable from the 480V

Shutdown Board 2Al-A to the 480V control / auxiliary building Vent

Board 2Al-1. The inspectors monitored installation work activities

and reviewed the controlling installation procedure, M&Al 4, and the

associated cable pull tension calculations provided in the work plan.

No deficiencies were identified in this area.

5.

Mechanical Inspection Results

During the two week inspection only a few mechanical tests were performed.

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The inspection team was able to observe three mechanical tests,

a.

Operability Test of Boric Acid Transfer Pump 2A-A

The inspectors witnessed the performance of Surveillance Instruction

304 on Boric Acid Transfer Pump (BATP) 2A-A after maintenance had

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been performed.

This safety-related pump is included in the

Inservice Test (IST) program governed by ASME Section XI which

requires verification of continued operability after maintenance

activities. The test involved duplicating system conditions pre-

viously documented when the pump was known to be operating properly

and verifying that pump. characteristics were the same as before

(within tolerances). The inspectors identified the following

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concerns:

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1.

Suction and discharge gauges for the pump, which was already

running when the test began, were not functioning.

In fact,

gauges for two of the other three BATP's (running) were also

inoperable.

On Pump 1A-A, the suction and discharge gauges

indicated a differential pressure that 'did not meet the opera-

bility requirements of the IST program, however, this pump was

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not being tested at the time.

It was not clear whether Pump.

1A-A was " operable" or " inoperable." To meet the accuracy

requirements of ASME Section XI, temporary gauges were installed

on Pump 2A-A to perform the test.

In summary, although operable

gauges and lines were used to conduct the. test, there was no

indication of pump suction and discharge pressures available to

plant staff during normal operations.

2.

In investigating the gauge concern, the inspectors noted that

each BATP had two sets of suction and discharge pressure gauges;

a labeled set at a panel six feet from the pump and another set

immediately off the suction and discharge piping.

For Pump 1B-8

the nearer gauges had been removed and the tubing capped.

Flow

Diagram 47W809-5 in the control room showed additional gauges

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installed on Unit 2 only, per Temporary Alteration Change Form

(TACF) 84-200262, although TACF 84-20062 was no longer listed in

the Shift Engineer's TACF log.

The gauges were not shown

installed for any BATPs on the as-constructed system flow

diagram. Also noted was that the piping class boundary designa-

tions on the flow diagram were inconsistent in that the boric

acid tanks are indicated as Safety Class "C" in some cases and

as Class "D" in others.

3.

Because the test resulted in a low differential pressure in

the " action" range of the IST' program, the pump was declared

.

inoperable.

The deficiency log attached to the completed test

report showed that the initial valve lineup was inadequate and

that a procedure change would be issued and the test redone.

It

appears that the test, which was run in accordance with an

established SI that has been used on a quarterly basis for

several years, may be invalid because the procedure was incor-

rect. This raises a concern as to whether previous pump

operability tests to the same procedure have been valid.

4.

One of the pump parameters verified during the operability

tests was vibration of pump bearing housings.

The inspector

noted that readings were taken on Pump 2A-A at locations dif-

ferent from those shown on the sketch in the SI. The discre-

pancy between field markings and procedure sketches was pointed

out to licensee personnel.

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As a result of this discrepancy, the inspectors reviewed sis and

verified target markings on 17 additional safety-related pumps

involved in the IST program. Technical Instruction (TI) 96.1,

" Vibration Monitoring-Pumps and Motors," states that, for

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repeatability, the pickup location should be marked on each

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bearing cap with a paint stick. The inspectors found no paint

marks on the two Unit 2 Motor Driven Auxiliary Feedwater (AFW)

Pumps, Unit 2 Turbine Driven AFW Pump 2AS, or on the top of Unit

1 Turbine Driven AFW Pump 1AS.

RHR Pump 188 had no markings at

the south and east orientations as shown in the SI sketch.

1

Conversely, SI-37 for the Component Cooling Pumps did not

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contain a sketch showing pickup locations although pumps were

marked in the field.

5.

To obtain suction and discharge pressure readings on the tem-

porary gauges for the test, the instrument mechanic had to

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do extensive cleanout of boric acid crystals from the instrument

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tubing. This involved the " rodding" of tubing, and disassembly

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of additional tubing joints and of a bolted flange. None of the

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additional activities were described on any work requests

associated with the test or gauge installation / removal process,

4

and no inspections or second party verifications of joint makeup

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were performed,

b.

Review of Previous SI Test Records

The inspectors reviewed surveillance test results for the BAT Pumps

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(SI-304) f rom February 1985 through September 1986 and for the

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Component Cooling Pumps (SI-46) from April 1986 through July 1986.

With the exception of one test, the data and evaluations appeared to

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be in accordance with procedure and Code requirements. The one

discrepancy noted involved the SI-304 test en September 12, 1986 for

BATP 1B-B, which showed a suction pressure tf 2.5 psi while the

minimum allowable was 4.3 psi. The out of specification reading was

not noted by the test personnel, and apparently no evaluation or

corrective action was performed. This is considered to be an

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isolated occurrence.

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c.

Functional Testing of Diesel Generator (DG) Room Exhaust Fan Low

Flow Switches

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The NRC inspectors witnessed the performance of the functional test

on six fans in three of the DG rooms. During the first test on

DG 28-B, a step verifying that red lights on the fan breaker were

energized was signed off when in fact the panel lights were burned

out.

A subsequent search by test personnel to obtain bulbs from

other panels indicated that approximately 50 percent of the panel

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lights were missing or burned out.

These local lights indicate the

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energized or de-energized status of plant equipment,

d.

Monthly Functional Testing of Diesel Generator 2A-A

The part of this test, which was observed by the inspection team,

indicated that DG 2A-A had a load dropping problem.

Discussions

with test personnel revealed that load dropping was related to the

-10-

.

rate at which loads.were picked up.

By the end of the NRC.inspec-

tion, TVA had not yet determined what corrective action was neces-

sary.

The examples of inadequate test conditions, inadequate test procedure

requirements, discrepancies in test documentation, and failure to follow

procedures discussed in Section 5.a above, are considered to be further

examples of lack of proper test control, as designated in Section 4.b

above.

6.

Design Baseline Verification Program (DBVP) Post Modification Test Review

The DBVP post-modification test review was initiated by TVA to review

Sequoyah modifications which had been performed since plant licensing.

The TVA review was limited to those modifications that were'within the

boundaries of 37 FSAR Chapter 15 systems required to shutdown the reactor

All applicable engineer-

or to mitigate the conseq)uences of.an. accident.and field change notices (FCNs)

ing change notices (ECNs

plant licensing were reviewed by TVA for Unit 2 and Unit 1/2 common

systems to verify the adequacy of post-modification-testing. The NRC

inspection team reviewed sixteen of the DBVP system evaluation reports

(SYSTERS) to determine whether an adequate-screening of ECNs and WPs had

been accomplished by TVA. The inspectors identified isolated deficien-

cies, which were discussed in detail with licensee personnel during the

inspection and were provided to licensee management during the exit

meeting. The overall conclusion of the NRC inspectors in this area was

that the licensee had applied the review criteria in a reasonable manner

in determining testing requirements for previous modifications.

7.

Separation of Electrical Circuits

a.

In response to questions raised during the previous NRC Safety

Systems Outage Modifications Installation Inspection (SS0MI), the

team inspected the routing of cables in a number of Flamemastic

coated cable bundles which contained both essential and nonessential

circuits.

The Sequoyah FSAR, in Section 8.3.1.4.3, states, in part... " Cables

for nonessential circuits may be run on cable trays.with those for

essential circuits with the following restrictions. When nonessen-

tial cable is routed in a tray with essential (GSPS) cables, that

cable or any cable in the same circuit has not been subsequently

routed onto another tray containing a different division of separa-

tion of essential cables." For the purpose of this report, the FSAR

requirement which prohibits the routing of any nonessential circuit

into raceways containing both divisions of essential circuits will be

referred to as " secondary bridging."

During the previous SS0MI inspection, it had been determined that

free-air cable installations are not controlled by the computer

generated routing scheme established for plant design.

Consequently,

the bundling of essential and nonessential cables in this manner

represented a potential for inadvertent secondary bridging.

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,

..

.

. - - - . . --

..

..

.

_ _ _ . . . . . . - . . .

. . . . - . . .

..

.. -- . . . .

. . ,

- - - - -

During this inspection, the inspectors identified a' sample of. .

nondivisional cables in the Units 1 and 2 spreading rooms which were

bundled with divisional cables. The nondivisional cables were then

identified above the fire barrier in the control room panel risers.

The inspectors then checked the computer generated routing of each .

identified nondivisional cable to ensure that it was not routed with

,

'

a redundant division in other parts of the plant. A total'of 68.

cables in the control room and seven cables from various locations in

the auxiliary building were selected. The cables are identified in

,

Table I.

The licensee had performed a similar effort just prior to

1

this NRC inspection and sampled 165 nonsafety cables bundled with

safety cables in the spreading rooms. Of the 75 cables in the NRC

sample, 31 overlapped TVA's sample.

A review of the-computer routing records for the cables selected

indicated that none were routed across' safety divisions. An audit.of

the routing list for the 165 cables identified by TVA also indicated

-

no routings across divisional boundaries.

However, two instances of

misrouted cables were identified with the cables. selected by the NRC

in the Auxiliary. Building. These two examples, which are discussed

below, call into question the accuracy'of.the cable routing lists:

1.

Safety-related Conduit IPP673B had three cables that' exited the

i

conduit and were then routed into divisional Tray LM-B and one

essential cable that was routed into nonessential Tray EAZ.- The

,

cable ran about 4 feet in Tray EAZ and then entered divisional

i

Conduit IV2943B. A review of the routing record for the cables

and conduit indicated that all four cables, IPP664B, IV2944B,

IV2963B, and IV29438, should have been routed in divisional Tray

LM-B.

Cable IV2943B should have been routed in divisional Tray

LM-B rather than non-essential Tray EAZ.

Sequoyah DNE personnel

verified the installation with NRC inspectors and indicated that

a Condition Adverse to Quality Report (CAQR) would be prepared

to document and correct the misrouting by moving the cable into

the appropriate divisional tray.

,

!

2.

Nonsafety-related Conduit FE-4832 had three cables exiting.the

conduit. After exiting the conduit, two of the cables were

i

routed into divisional Tray NJ-A, and one cable was routed into

j

non-essential Tray JAM. A review of the conduit and cable

j

routing records indicated that all three cables, FE4968, FE4969,

!

and V1004 should have been routed in nondivisional Tray JAM.

i

j

Since the two misrouted cables entered the Flamemastic bundle in

divisional Tray NJ-A, finding'the true routing of the cables was'

not possible. Sequoyah DNE-staff verified the misrouting with

the NRC inspectors.- The NRC inspectors were informed that a.

CAQR would be written to document and evaluate the misrouting.

Since the route for the two cables in Tray NJ-A was unknown,

the potential exists for secondary bridging by these cables.

1

In summary, the question of secondary bridging at Sequoyah will

require further evaluation by the licensee and NRC personnel. The

routing deficiencies identified during this inspection indicate a

3

potential for inadvertent problems in this area.

l

(

4

-12-

i

1

.

b.

During the entrance meeting with the licensee the NRC inspectors

raised questions concerning the use of Flamemastic 77 as an approved

fire barrier for protection of safety-related circuits from inter-

nally generated fires.

In response to these questions the licensee

stated that, with one exception, Flamemastic 77 had not been used for

this purpose. The exception is the annulus area where cables leaving

various electrical penetrations are dispersed into cable trays or

conduits for routing through the shield wall to other areas of the

plant.

This exception is found in TVA Design Criteria SQN-DC-V-12.2,

Section 4.2.9, which states in part... "Where it is impracticable to

provide enclosed trays, then the cables shall be coated with Flame-

mastic 77 or its equivalent."

During evaluation of Sequoyah FSAR requirements pertaining to elec-

trical separation the inspectors noted NRC Question 8.20 and a TVA

response which relate to this issue.

The NRC question states:

"Several places in Section 8.3.1.4.2 the use of fire resistant

coating materials such as 'Flamemastic 71A' is proposed as an

1

alternative to the use of solid barriers.

This is not an

1

'

acceptable alternative and we will require the use of adequate

solid barriers that will not permit the transfer of sufficient

heat energy between trays to raise the temperature of the cables

contained in the redundant tray above their safe temperature

rating."

TVA's response to the NRR question was as follows:

1

" Fire resistant coating material such as 'Flamemastic 71A' in

!

lieu of solid barriers has not been used.

Subparagraph

j

8.3.1.4.2 has been revised to delete this reference."

1

The NRC inspectors discussed this issue with TVA personnel in an

attempt to determine to what extent Section 4.2.9 of the design

criteria had been used at Sequoyah.

The discussions indicated that

design drawings for the annulus area specify the installation of tray

1

covers, and that no Flamemastic was used in lieu of solid barriers

j

in the annulus area. Additionally, the licensee provided two Quality

Information Requests (QIRs), SQN-EEB-86145 and SQN-EEB-86172, which

j

detail the walkdown of plant cable trays, including the annulus area,

I

to assure that tray covers have been installed. Based upon this

information the NRC inspectors concluded that, while portions of the

design criteria make provision for use of cable coating in lieu of

solid barriers, it does not appear that this provision was exercised

in field installations.

Based on the conflict which exists between the Sequoyah FSAR and the

TVA design criteria the inspectors concluded that the provision for

use of Flamemastic cable coating, as specified in Section 4.2.9 of

Sequoyah Design Criteria SQN-DC-V-12.2, does not provide an acceptable

alternative for protection of safety-related circuits and appears to

permit installations which violate FSAR requirements.

c.

The Sequoyah FSAR, in Section 8.3, establishes separation criteria

for independence of safety-related equipment and circuits. These

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_-

.

.

criteria are delineated in SQN-DC-V-12.2, titled " Separation of

Electric Equipment and Wiring." Specific criteria are provided for

physical separation of cable trays in order to protect the enclosed

safety-related circuits. However, the FSAR provides no criteria for

physical separation of conduits which contain safety-related circuits

and, while this subject is referenced in Section 4.2.2.2 of the

Design Criteria, no specific details are provided.

During the

inspection of installed components, the NRC inspectors observed

several installations in which the physical separation between

redundant divisional cable trays and conduits was less than the FSAR

)

specified distances for cable tray.

As an example, Division A

l

Conduit 2M-3240-A was installed less than 1 inch from Division B

uncovered Cable Tray MS-B.

Based upon the examination of field

installations, the inspectors expressed concern that the lack of

i

criteria for separation of safety-related conduits does not meet the

intent of Section 8.3 of the FSAR, in that protection and independ-

ence of redundant circuits may be compromised.

The concerns identified above regarding the potential for secondary

bridging, the potential use of Flamemastic as an alternative to solid

barriers, and the lack of criteria for separation of safety-related

conduits, will require further review by NRC (Unresolved Item

50-327/87-18-01;50-328/87-18-01).

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a

l

TABLE I

SECONDARY BRIDGING CABLE SAMPLE

Control Room / Spreading Rooms

Panel 1-M-23B:

1M1597

1M1596

IV3521

IM1585

IV1595

1M1598

1M1599

ISR906

i

1A3690

1A3716

IM1587

ISR914

1M1586

1M1589

iM1588

l

Panel 1-M-23A:

1V3521

IV3522

IV3520

1A3688

IV3523

1M1590

PL3858

1M1584

1M1581

1M1591

IM1580

3

Panel 0-M-27B Riser 1:

2FE89

2FE74

SR210

2TCT1

'

PL3931

2FE97

2PL1994

2FE65

2FE73

2TCT2

2PL1894

2TCT3

2FE96

2FEP'

2PL1794

2FE66

PL3921

2FE90

2A4380

2FE81

,

Panel 0-M-278 Riser 2:

2M202

2M200

Panel 0-M-27B Riser 3:

2PL3646

1PM3191

1PL3646

1PM3227

2PL3661

IPM2491

2PM2411

1PM2256

2PM2271

2PM3122

1PM3217

2PM3257

2PM3182

2V5787

Panel 2-M-4 Riser B:

2A2581

2A2580

2SR694

2C222

2SR693

Panel 2-M-5 Riser B:

2SR695

Auxiliary Building

IV2944B

IV2963B

IV2943B

IPP664B

FE4968

FE4969

V1004

TI-1