ML20213F668

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Monthly Operating Rept for Oct 1986
ML20213F668
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 10/31/1986
From: Lempges T, Roman T
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
NUDOCS 8611140380
Download: ML20213F668 (6)


Text

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te NIAGARA MDHAWK POWER CORPORATION o

NINE MILE POINT NUCLEAR STATION UNIT f1 NARRATIVE OF OPERATING EXPERIENCE The station operated during the month of October 1986 with a Unit Availability Factor of 100.0% and a Net Design Electrical Capacity Factor of 96.6%.

There were no challenges to Electromatic Relief Valves. Reductions in Capacity Factor were due to power reductions for weekly control rod exercising and minor control rod pattern adjust-ments for thermal limit constraints.

CLASS I WORK - MECHANICAL MAINTENANCE - OCTOBER 1986 WR# 102884 Sys. 39, Component EC755, Drain valve off - IV-39-10 Steam Supply IV.

Tightened packing to stop leak.

WR# 102885 Sys. 39, Component EC741. Emergency Condenser Steam

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Line Drain Valve. Tightened Packing to stop leak.

WR# 102895 Sys. 30, Component FW1076.

Blocking Valve to conductivity Element on Common 5th Heater Header. Void per operation.

WR# 013894 Sys. 40, Component Spare, Core Spray Check Valve.

Void per Rocco Longo.

WR# 100118 Sys. 33, Component SWP S-1.

Clean-Up system support S-1.

Inspection hole in plate 13/16" and retorque nut to 150 ft. Ibs.

WR# 100119 Sys. 33, Component A-1.

Clean-Up System Anchor A-1.

Corrective action per attached Telecom.

WR# 103008 Sys. 209, Component 107 Fire door 107.

Replaced closure arm and tightened hinge screws.

WR# 020796 Sys. SEC, Component D-107.

Fire / Security Door D-107.

Adjusted.

WR# 105900 Sys. 39, Component 39-HS-31.

Hydraulic Snubber on Steam Supply to 121 Emergency Condenser.

Replaced snubber component.

WR# 105678 Sys. 05, Component 12.

Emergency Cooling Vent Valve on System 12.

Upon investigation, no leakage. Void, no work required.

WR 105677 Sys. 05, Component 01.

Emergency Cooling Vent on System 11.

Upon investigation, no leakage. Void, no work required.

WR# 105325 Sys. SEC, Component D-196.

Door Closure (Track bay Airlock Exterior) Void. Maintenance has a WR for this work #013995 on hold because of inter-door seal.

WR# 105070 Sys. 29, Component SS26.

Support on Feedwater Recire.

Back to the condenser. Out of spec. Torqued nuts to 150 ft. Ibs.

WR# 105061 Sys. 44, Component

. CRD Serial #71453. Replaced parts. Rebuild CRD.

WR# 105055 Sys. 44, Component

. CRD Serial # 71526.

Replaced parts. Rebuilt CRD.

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CLASS I WORK - ELECTRICAL MAINTENANCE - OCTOBER 1986 WR# 014086 Electrical miscellaneous, ELM-162 MG, Replaced bearing and brush yoke on motor generator.

WR# 102898 Electrical miscellaneous, ELM-162 MG.

Calibrated protective relays.

WR# 105275 Instrument air system, 94-02.

Replaced overcurrent trip device.

WR# 102903 Electrical miscellaneous, ELM-172 MG.

Tested motor generator set.

CLASS I WORK - INSTRUMENTATION AND CONTROLS - OCTOBER 1986 WR# 102898 162 motor generated output voltage tripped open due to low output voltage from generator. Replaced voltage regulator.

WR# 105204 Raise the APRM Rod block line for all APRMS to 104 percent. Changed from 103.5 to 104 percent.

WR# 105205 APRM 18 is reading 100 percent power, GAF is reading 1.04.

Recalibrated 214 in APRM to isolation amp.

WR# 105277 Rx building closed loop cooling temp. control valve does not operate in auto.

Calibrated MVI 70-23A and indicator 70-23C.

WR# 102903 MG se't 172, troubib shoot and replace as necessary.

Replaced voltage regulator.

WR# 105243 Test connection (P6) on CRD accum. 30-27, cap on test connection leaks.

Replaced connector.

WR# 105258 Drywell pressure (accident) 0-75 psi transmitters and indicators - calibrate loops as required. Calibration due.

WR# 105288 Calibrate 112 maint steam rad. monitor.

Recalibrated using N1-ISP-FM7.

WR# 105262 Main steam line rad. monitors 111, 112, 121, 122.

Poor contact on hi cal / local switches.

Burnished contacts.

WR# 112609

  1. 111 main steam rad. monitor is reading low.

Inst.

drift-recalibrated.

WR# 105251 CRD accumulator 42-43 leaking nitrogen. Fitting tightened.

-e OPERATING DATA REPORT DOCKET NO. 50-220 DATE 11/4/86 j

COMPLETED BY T.W. Roman M ecs

/3 TELEPHONE (115)349-2422 OPERATING STATUS Nine Mile Point Unit I Notes

1. Unit Name:
2. Reporting Period:

10/1/86 Thru 10/31/86

3. Licensed Thermal Power (MWt):

1850 640

4. Nameplate Rating (Gross MWe):

620

5. Design Electdcal Rating (Net MWe):

630

6. Maximum Dependable Capacity (Gross MWe):

610

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
9. Power Level To Which Restricted,if Any (Net MWe):
10. Reasons For Restrictions,if Any:

This Month Yr to-Date Cumulatise 745.0 7.296.0 150.121.2

11. Hours in Reporting Period 745.0 4,359.5 105.599.1
12. Number Of Hours Reactor Was Critical
13. Reactor Reserve Shutdown Hours 0.0 0.0 1,204.2
14. Hours Generator On-Line 745.0 4,260.1 102,522.7
15. Unit Reserve Shutdown Hours 0.0 0.0 20.4
16. Gross Thermal Energy Generated (MWH) 1.369.555.0 7,062,630.0 171,553,388.0
17. Gross Electrical Energy Generated (MWH) 459,704,.0 2,335,133.0 56, CO.+,588. 0
18. Net Electrical Energy Generated (MWH) 446,340.0 2,257,557.0 54,919,884.0 100.0 58.4 68.3
19. Unit Service Factor 100.0 58.4 68.3
20. Unit Availability Factor 98.2 30./

60.0 i

21. Unit Capacity Factor (Using MDC Net) 96.6 49.9 59.0
22. Unit Capacity Factor (Using DER Net) 0.0 11.0 15.3
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Each t:
25. If Shut Down At End Of Report Period, Estimated Date of Startup:
26. Units in Test Status t Prior to Commercial Operation):

Forecast Achiesed INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION (4/77i

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AVER 4GE D4lly UN!T P0hCR LEVEL i

DOCKET NO.

50-220 UNIT Nirio Mile pr 1 DATE 11/4/86 CO\\tPLETED By T.W. Roman M Gect TELErilONE -(315)349-2422 af0 NTH OCTOBER DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (5the-Net)

(alwe Net s 601 I7 600 2

60I 601 IS 3

595 19 604 538 4

20 603 598 5

603 21 6

600 604 22 601 7

23 603 601 8

24 602 601 9

25 601 10 600 26 603 II 600 27 602 603 12 2S 604 599 13 604 29 602 14 601 30 60j 15 595 31 16 602 e

INSTRUCTIONS i

On this format.hst the atersee dail' ""5' P"*'"' IC5cl in alENet tiir each day in rise ts;,oity %4. C.

the nearest whole megaw3gg,"

ompute to d

NMP-20524 NIAGARA MOHAWK POWER CORPORATION NIAGARA MOHAWK 300 ERIE BOULEVARD WEST SYR ACUSE,N Y 63202 THOMAS E LEMPGES vre enescent-=uctsan oe=eano.

November 4, 1986 Director Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C.

20555 Attention: Document and Control Desk

Dear Sir:

Submitted herewith is the Report of Operating Statistics and Shutdown for October for the Nine Mile Point Nuclear Station Unit I.

Also included is a narrative report of Operating Experience for October 1986.

Very truly yours, 7

/

/

f/794 A*

Thomas E. Lempges Vice President -

Nuclear Generation TEL/ bas Attachment cc: Director, Office of I&E (10 copies)

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