ML20212R359

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SALP Repts 50-454/87-01 & 50-455/87-01 for Nov 1985 - Oct 1986
ML20212R359
Person / Time
Site: Byron  
Issue date: 01/21/1987
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20212R346 List:
References
50-454-87-01, 50-454-87-1, 50-455-87-01, 50-455-87-1, NUDOCS 8702020612
Download: ML20212R359 (35)


See also: IR 05000454/1987001

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SALP 6

SALP BOARD REPORT

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

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SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

50-454/87001; 50-455/87001

Inspection Report No.

Commonwealth Edison Company

Name of Licensee

Byron Station Units 1 and 2

Name of Facility

.,

November 1, 1985 through October 31, 1986

Assessment Period

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8702020612 870121

PDR

ADOCK 05000454

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BYRON STATION

TABLE OF CONTENTS

Page No.

I.

INTRODUCTION

1

II. CRITERIA

2

III. SUMMARY OF RESULTS

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IV. PERFORMANCE ANALYSIS

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A.

Plant Operations

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B.

Radiological Controls

6

C.

Maintenance

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D.

Surveillance

11

E.

Fire Protection

12

F.

Emergency Preparedness

13

G.

Security

15

H.

Outages

17

1.

Quality Programs;and Administrative Controls

Affecting Quality

18

J.

Licensing Activities

20

K.

Training and Qualification Effectiveness

22

L.

Preoperational Testing

23

M.

Construction

26

V.

SUPPORTING DATA AND SUMMARIES

28

A.

Licensee Activities

28

B.

Inspection Activities

28

C.

Investigations and Allegations Review

30

D.

Escalated Enforcement Actions

30

E.

Licensee Conferences Held During Assessment Period

31

F.

Confirmatory Action Letters (CALs)

31

G.

Review of Licensee Event Reports, Construction

Deficiency Reports, and 10 CFR 21 Defect Reports

Submitted by the Licensee

32

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H.

Licensing Activities

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1.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance based upon this

information. SALP is supplemental to normal regulatory processes used to

ensure compliance to NRC rules and regulations. SALP is intended to be

sufficiently diagnostic to provide a rational basis for allocating NRC

resources and to provide meaningful guidance to the licensee's management.

to promote' quality and safety of plant construction and operation.

An NRC SALP Board, composed of staff members listed below, met on

January 8, 1987, to review the collection of performance observations

and data to assess the licensee's performance in accordance with the

guidance in NRC Manual Chapter 0516, " Systematic Assessment of Licensee

Performance." A summary of the guidance and evaluation criteria is

provided in Section II of this report.

This report is the SALP Boards's assessment of the licensee's safety

performance at Byron Station Units 1 and 2 for the period November 1,

1985, through October 31, 1986.

SALP Board for Byron Station Units 1 and 2:

J. A. Hind, Director, Division of Radiation Safety and Safeguards

C. E. Norelius, Director, Division of Reactor Projects

C. J. Paperiello, Director, Division of Reactor Safety

R. F. Warnick, Chief, Reactor Projects Branch 1

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J. M. Hinds, Jr., Senior Resident Inspector, Byron

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S. A. Varga, Project Director, NRR Division of PWR Licensing A

L. N. 01shan, Project Manager, NRR Division of PWR Licensing A

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II. CRITERIA

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The licensee performance is assessed in selected functional areas

depending whether the facility is in a construction, preoperational

or operating phase. Each functional area normally represents areas

significant to nuclear safety and the environment, and are normal

programmatic areas.

Some functional areas may not be assessed because

of little or no licensee activities or lack of meaningful observations.

Special areas may be added to highlight significant observations.

One or more of the following evaluation criteria were used in assessing

each functional area.

1.

Management involvement in assuring quality

2.

Approach to resolution of technical issues from a safety standpoint

3.

Responsiveness to NRC initiatives

4.

Enforcement history

5.

Operational and Construction events (including response to analysis

of, and corrective actions for)

6.

Staffing (including management)

However, the SALP Board is not limited to these criteria and others may

be used where appropriate.

Based upon the SALP Board assessment each functional area evaluated is

classified into one of three performance categories. The definition

of these performance categories is:

Category 1:

Reduced NRC attention may be appropriate.

Licensee

management attention and involvement are aggressive and oriented toward

nuclear safety; licensee resources are ample and effectively used so

that a high level of performance with respect to operational safety

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and/or construction quality is being achieved.

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Category 2:

NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and

are reasonably effective so that satisfactory performance with respect

to operational safety and/or construction quality is being achieved.

Category 3: Both NRC and licensee attention should be increased.

' Licensee management attention or involvement is acceptable and considers

nuclear safety, but weaknesses are evident; licensee resources appear to

be strained or not effectively used so that minimally satisfactory

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performance with . respect to operational safety and/or construction

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quality is being achieved.

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III. SUMMARY OF RESULTS

A total of 13 Functional Areas were rated in this SALP.

Licensee

performance in four areas improved from Category 3 to Category 2 so

that there were no Category 3's assigned in this SALP. Two Functional

Areas sustained Category 1 performance and five areas remained at

Category 2.

The Functional Area of Training and Qualification

Effectiveness had not been used in prior assessments and was rated a

Category 2.

As noted below, the Functional Area of Construction which

was also rated Category 2 is the combination of construction Functional

Areas used in prior assessments. These areas were combined due to

limited activity and inspection in this assessment period.

Rating Last

Rating This

Functional Area

Period

Period

Trend

A.

Plant Operations

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2

improving

B.

Radiological Controls

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2

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C.

Maintenance

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2

D.

Surveillance

2

2

E.

Fire Protection

2

2

F.

Emergency Preparedness

1

1

G.

Security

3

2

improving

H.

Outages

1 (initial fuel load) 1

1.

Quality Programs and

Administrative Controls

Affecting Quality

2

2

J.

Licensing Activities

2

2

K.

Training and Qualification

2

Effectiveness

L.

Preoperational Testing

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M.

Construction

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Not rated as a separate functional area in previous SALPs.

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Construction during this assessment period includes the functional areas

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of Containment and Other Safety-Related Structures, Piping Systems and

Supports, Instrumentation and Control Systems, and Electrical Power Supply

and Distribution, which all received Category 2 ratings during the last

SALP assessment.

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IV. PERFORMANCE ANALYSIS

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A.

Plant Operations

1.

Analysis

Licensee activities in this functional area were observed in

portions of 14 inspections conducted by resident inspectors.

Due to the large amount of activity expected for Unit 1

startup and Unit 2 completion and licensing and due to the

Category 3 rating assigned in the last SALP, a third resident

inspector was assigned to the station. The operations

inspections focused on overall plant performance, operating

events, personnel errors, shift crew performance during normal

and off-normal conditions, shift relief and turnover activities,

control room discipline, and adherence to operating procedures.

The inspections included a review of logs and records, interviews

with plant personnel, and followup of significant operating events

to ascertain that the facility was operated in conformance with

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the Technical Specifications and administrative procedures.

The licensee's enforcement performance indicated minor and

isolated programmatic failures. One Severity Level V and four

Severity Level IV violations were identified.

In addition, the

licensee identified three violations of minor significance for

which, in accordance with 10 CFR Part 2, Appendix C, Notices

of Violation were not issued.

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From a review of the Licensee Event Reports (LERs) issued

during the assessment period, it was determined that the number

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of events involving personnel errors continues to represent

a significant portion of the total at 16 of 39. Licensed

operators were involved in 5 of the 16 personnel errors.

The Region has continuously reviewed the Unit 1 LERs and

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found them to be of an improved quality based on the 10 CFR

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50.73 requirements due primarily to a licensee LER improvement

program initiated in February 1986.

Features of the

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improvement program included additional training of all

personnel involved in LER preparation; increased supervisory

review,

i.e., supervisor listed as contact; designating

" Lead Reviewers"; format changes; LER writers guide and review

check list changes; and implementation of a diagnostic flow

chart to aid in root cause determination.

Improvement was also noted in the area of reactor trips.

During this period Unit 1 experienced six trips (two during

the last eight months of the assessment period) compared

with 31 during SALP 5.

Of these, two could be attributed to

operations; one was due to a personnel error, and the other

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to a defective procedure.

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Periodic management meetings between RIII and Byron Plant

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management, initiated during the previous SALP period by

Region III as a result of the high number of Unit 1 operating

events and personnel errors, continued through most of this

assessment period. As a result of concerns expressed by the

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NRC, the licensee developed and implemented an effective

improvement program in operations (and in other areas discussed

in later sections of this report).

The NRC has noted increased

licensee management involvement, increased responsiveness to

NRC concerns, and improvement in this functional area. Because

of improved plant performance and management involvement and

responsiveness, the periodic management meetings to review Unit

1 performance were terminated in mid-1986.

Examples of effective management involvement are: (1) a one

page daily status bulletin for all plant employees which

highlights the plant status, the critical work scheduled for

the day, and other significant information; (2) a monthly

report of performance indicators to measure performance trends,

and department goals; and (3) special attention to eliminate

nuisance alarm annunciators in the control room which resulted

in a " black board" at the beginning of 1986.

The effectiveness of station management's influence and

resulting operator implementation in the operations control

areas continues to be demonstrated by a high level of control

room discipline. Personnel access controls are enforced,

operators are cognizant and alert to plant conditions, and a

high level of professionalism is demonstrated at all times.

Although the activity level in the control areas has increased

with Unit 2 pre-operational testing and readiness for licensing

activity, the licensed operators and shift managers have met

the challenge and continue to maintain controlled areas free

from distracting or prohibited activity. However, one recently

noted control room distraction is the background noise caused

)

by the intercom speakers in the control room. The NRC

continues to view the licensed operators at Byron Station

as a highly professional, well trained, collectively motivated,

high quality operating team.

The Byron staff is stable and well organized and continues

to be a licensee strength with the only personnel turnovers

resulting from promotions and internal transfers, which have

added to management effectiveness. Qualifications and

experience levels within the staff have shown improvement

through the addition of licensed operators and continued

on-shift experience.

Staffing levels continue to be high

to ensure qualified and experienced operators are available

as Unit 2 approaches the Startup Test phase.

The licensee has continued to treat Technical Specification

interpretations with a conservative approach to technical

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safety issues.

Responsiveness to NRC concerns has been

thorough and overall the licensee was cooperative.

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2.

Conclusion

The licensee is rated Category 2 with an improving trend in

this area. The licensee was rated a Category 3 in this area

in the last SALP. The improved rating is based on significant

reduction in the number of events and in the overall improvement

of plant operations.

3.

Board Recommendation

None.

B.

Radiological Controls

1.

Analysis

Twelve inspections were conducted during this assessment period

by region based inspectors.

Inspection effort was increased

in response to poor licensee performance during the previous

assessment period. The resident inspector also reviewed this

area during routine inspections.

No violations were identified. This represents a significant

improvement over the previous assessment period when seven

violations were identified, including an aggregate of problems

cited in a Severity Level III violation which resulted in a

civil penalty.

Management involvement and control in assuring quality was

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much improved during this assessment period.

In response to

previously identified problems, licensee management committed

to aggressively identify and correct radiation protection

program weaknesses by developing a radiation protection.

improvement program. The positive effects of this strong

management involvement and support of the radiation protection

program resulted in significant improvements in that program.

An improving trend of positive management involvement was

observed during the assessment period, in particular concerning

staff emphasis on procedural adherence and increased

disciplinary action for procedural violations. Corporate

management involvement has also improved as evidenced by

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corporate investigation of several radiological occurrence

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reports. Chemistry group management provides satisfactory

oversight of laboratory operations and stays well aware of

plant chemistry conditions.

$taffing was generally adequate during the period.

Considerable

turnover was experienced with the replacement of the Radiation

Chemistry Supervisor (RCS) who was reassigned, the lead health

physicist, who transferred to the corporate offices, and two

staff health physicists who left. The RCS supervisor was

replaced by the Assistant Technical Staff Supervisor and the

lead health physicist was replaced by an experienced health

physicist with equivalent qualifications from another licensee

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nuclear plant. The Radiation Protection Manager (RPM) role

held by the former RCS was assumed by the new lead health

physicist. One staff health physicist was replaced and the

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other's duties have been assumed by contract professional

health physicists (five) hired to supplement the staff until

it acquires more experience. Staff qualifications in health

physics and chemistry meet current ANSI standards although

operational experience is low, which is not atypical for new

plants. The licensee's policy of rotation between chemistry

and health physics assignments limits radiological control

technician's (RCT) proficiency in the laboratory. RCT

experience is partially compensated by assignment of ANSI

qualified foreman to each shift. The weakness in the generic

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Ceco plant organization change (last assessment period) that

placed two intermediate management positions between the RPM

and the plant manager has been mitigated by regularly scheduled

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meetings between the two.

The licensee's responsiveness to NRC initiatives has generally

improved during this assessment period. Weaknesses concerning

radiological evaluations, airborne release calculations,

procedural adherence, RCT training, and radiation protection

awareness of workers were improved during this assessment

period. The licensee's reporting of incidents to the NRC was

better than required. However, the licensee has been slow to

determine the cause of anomalous readings of the monitor on

the waste gas decay tank effluent line.

The licensee's approach to resolution of radiological technical

issues has been adequate. Total personnel radiation exposure

for 1986 through August was approximately 45 person rems

reflecting good exposure control program design and

implementation during the early operation of the plant. The

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licensee's ALARA program is well organized but appears to

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require increased resource allocation to effectively complete

the work required prior to the Unit I refueling / maintenance

outage and the Unit 2 startup.

Several noteworthy ALARA

activities requiring further implementation include, ALARA

awareness sessions with each department, Unit 1 outage

preparations and discussions of planned jobs with each work

group, shielding and mock-ups for radiologically significant

outage jobs, and completion of the plant photo file. A design

change implemented during this assessment period to min %ize

neutron streaming near the personnel batch has not been as

successful as anticipated; further design analysis and

shielding attempts are planned. Solid radwaste shipments were

average for a PWR during the assessment period. There were

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no problems with transportation of radioactive material or

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radwaste during the assessment period.

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Licensee control of radioactive effluents has improved.

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One minor unplanned release occurred early in the assessment

period whereas five occurred during the previous period.

Gaseous effluents continued in the average range for U.S.

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pressurized water reactors.

Liquid effluents continued the

decline noted at tht end of the previous assessment period

and are also currently in the average range.

Licensee chemistry / radiochemistry performance has generally

improved. The chemistry group naintains very good awareness

of plant water chemistry through extensive sampling and

handling of key chemistry variables. Chemistry controls have

been generally satisfactory except for dissolved oxygen levels

in the primary water storage tank which consistently exceed

the Westinghouse 100 ppb guidelines. The licensee is

continuing to investigate the cause of the problem. Meanwhile

reactor coolant oxygen levels are being controlled within

limits by hydrogen addition.

The plant makes extensive use of in-line monitoring on the

secondary system including an ion chromatograph on the steam

generator blowdown.

Effective use is made of state-of-the-art

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instrumentation in the chemistry laboratory and counting

room. The station performed well in its first confirmatory

measurements split sample comparison with the NRC mobile

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laboratory by achieving 49 agreements in 50 comparisons.

Basic chemistry QA/QC programs have been established to

monitor instrument performance and technical performance

in the laboratory and counting room. Twice yearly testing

with unknown chemistry samples have indicated improving RCT

capabilities. Considerable improvement is needed in the

organization of QC data to make it more useful for routine QA

assessments and the scope of RCT testing needs to be expanded

to include more analyses. A corporate interlaboratory

comparison program currently under development for radiological

and nonradiological analyses is partially in place.

2.

Conclusion

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The licensee is rated Category 2 in this area. The licensee

was rated Category 3 in this area in the last SALP. The

improved rating in this area is attributed to strong management

involvement which continued throughout the SALP period.

3.

Board Recommendation

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None.

C.

Maintenance

1.

Analysis

Examination of this functional area consisted of two

inspections conducted by region based inspectors and portions

of thirteen inspections by resident inspectors.

Inspection

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effort by resident inspectors was increased with the assignment

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of a third resident inspector.

The inspections by resident

inspectors included a review and observation of the maintenance

programs, staffing, staff training, and records. Selected

preventative and corrective maintenance and system modifications

were observed to verify that these activities were completed

in accordance with Technical Specifications and the licensee's

quality assurance program requirements and administrative

procedures.

Followup inspections were performed on significant

equipment problems.

Discussions were held with craftsmen,

maintenance supervision, and plant management. One of the

Regional inspections was conducted to review the operational

maintenance program for Unit 1 and the other was conducted to

verify operational readiness in this area for Unit 2.

Four violations were identified, including two Severity Level

IV and one Severity Level V violations which represented

isolated failures by the licensee's programs. One Severity

Level III violation was issued after the SALP period for an

event that occurred within the period. This event was of

safety significance and was indicative of programmatic

failures of personnel to accomplish maintenance and quality

assurance programs as they were written.

In July 1986,

an inoperable Pressurizer Code Safety Valve was installed,

placed into service, and failed to function as required. The

violations resulted from inadequate administrative controls and

personnel errors in that after a Code Safety Valve was taken

out of service in 1985 for repair, the valve disc was removed

and only partial maintenance was performed. Subsequently,

because of improper segregation, identification, and test

documentation, the valve with the missing valve disc was

inadvertently placed back into service without being tested.

It was only after the valve actuated at a lower pressure than

intended that plant personnel became aware of problems with

the valve. The root cause of these violations was personnel

errors by a mechanical maintenance supervisor, a technician,

and a QC inspector. Also, after the July 1986 incident, the

replacement Pressurizer Code Safety Valves were tested and

accepted based on a lift setting of 2485 psig

3% rather than

1% as required by the Technical Specifications. One of the

replacement valves was actually set outside the i 1% Technical

Specifications limit. These violations are considered

significant and demonstrate weaknesses in the mainterance

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program. However, once licensee management became aware of

the Pressurizer Code Safety Valve problem, the licensee took

prompt and extensive corrective action at both the station and

corporate levels. The licensee's immediate corrective actions

included, among other things, meetings with appropriate

departments and stressing that test documentation must match

equipment being tested; revising test procedures to clearly

identify equipment; installing segregation cages for defective

components; and requiring Quality Assurance to independently

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verify proper disposition of nonconforming conditions. The

long term corrective actions included a broad look at all

maintenance activities by licensee management as well as an

evaluttion requested by the licensee of the Byron maintenance

program and activities by a team from the Institute of Nuclear

Power Operations (INPO). A licensee site task force performed

a review of the findings by INP0 and management and developed

a maintenance improvement program. The improvement progam has

been initiated and corrective actions are being implemented.

Overall, maintenance work performed was generally technically

sound, thorough, and timely. Records were generally complete,

well maintained, and available.

However, the NRC believes

that during the first part of the SALP assessment period,

appropriate management attention including accurate and timely

resolution of maintenance items was a weakness as evidenced

by the Code Safety Valve event discussed above. Subsequently,

management involvement in assuring quality in the maintenance

area has improved. Upon identifying areas requiring additional

management oversight, the licensee has generally provided

technically sound resolutions with good consideration of the

safety issues involved.

A review of cause codes for LERs shows 10 of 39 were

attributable to malfunctions. However, malfunctions include

the results of lightning and ice forming as well as radiation

monitor spurious signals causing ventilation realignments. No

maintenance program weaknesses were identified by LERs; however,

the licensee is including in the Maintenance Improvement

Program provisions for a preventative maintenance program which

assesses equipment failures.

The maintenance organization is adequately manned in all

positions with well-trained,* increasingly experienced personnel

who have demonstrated a growing measure of pride in their

workmanship.

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Inspections in the maintenance area have provided the NP.C with

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a reasonable level of confidence in the administration of an

overall sound program with adequately documented procedures

and records. The maintenance program (both corrective and

preventative) appeared to be adequate and properly implemented

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based on these inspections.

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2.

Conclusions

The licensee is rated Category 2 in this area. The licensee

was rated Category 2 in this area in the last SALP.

3.

Board Recommendation

None.

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D.

Surveillance

1.

Analysis

This functional area was examined in two inspections conducted

by region based inspectors and portions of thirteen inspections

conducted by resident inspectors.

Inspection effort by

resident inspectors was increased with the assignment of a

third resident inspector based, in part, on the Category 3

rating given this functional area in the last SALP.

Implementation of the surveillance program was reviewed and

inspectors verified that testing was. performed in accordance

with approved procedures, that test instrumentation was

calibrated, that limiting conditions for operation were met,

that removal and restoration of the affected components were

accomplished, that test results conformed with Technical

Specifications and procedure requirements and were reviewed by

personnel other than the individual directing the test, and

that any deficiencies identified during the testing were

reviewed and resolved by appropriate management personnel.

Work was generally timely, thorough, and technically sound.

Records were generally complete, well maintained, and available.

Seven violations were identified for which Notices of Violation

were issued, five Severity Level IVs and two Severity Level Vs.

In addition, the licensee identified three violations for

which, in accordance with 10 CFR Part 2, Appendix C, Notices

of Violation were not issued. These violations represented

minor and isolated failures of the licensee's programs;

however, the total number indicates that there were areas

in need of program refinements and more attention to details.

Six Severity Level IV violations were identified in the last

SALP period.

During this assessment period the licensee reported 6 incidents

of missed or inadequately performed surveillances compared with

18 in the previous SALP. Of these, 5 were attributed to

personnel error, and 1 to defective procedures. Some of the

missed surveillances have resulted in violation of license

conditions, Technical Specifications, or NRC regulations;

however, performance in this functional area has shown a

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significant improvement in total incident occurrences when

considering the thousands of surveillances conducted.'

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Management involvement in this functional area was consistent

throughout the period. The licensee developed the Conduct

of Operations Improvement Program (COIP) during the last

assessment period and has continued to focus on implementation.

A feature of the COIP was to eliminate missed surveillances.

Based on NRC inspection findings over the current assessment

period it appeared that the program was technically sound and

has provided acceptable technical resolutions from a safety

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Management involvement in reducing the numbers of surveillance

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incidents has demonstrated a greater level of effectiveness

than the previous assessment period as the reduced number

indicates.

The licensee has demonstrated a willingness to

address this issue in response to NRC concerns expressed in

the monthly management meetings discussed in Section IV.A.,

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Operations. The licensee continues to devote resources to

the resolution of the problem through efforts in the areas

of monitoring the surveillance system records, increasing

awareness of the operating staff in surveillance scheduling,

improving surveillance scheduling, increasing technical staff

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awareness and interaction with the operating staff, and

continuing to monitor and improve the corrective action items

designed to eliminate the problem. A review of the events

during this period indicated that these changes were effective

and resulted in improvements in this functional area.

2.

Conclusion

The licensee is rated Category 2 in this area. The licensee

was rated a Category 3 in this area in the last SALP. The

improved rating is based on the significant reduction in missed

or inadequately performed surveillance.

3.

Board Recomendation

None.

E.

Fire Protection

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1.

Analysis

During the assessment period, two inspections were conducted

by regional based inspectors. Areas reviewed included the

close out of open items from previous Appendix R inspections,

verification of the adequacy of the routine fire protection

program implementation, and continued NRC review of Unit 2

compliance with 10 CFR 50, Appendix R.

Portions of 19

inspections performed by resident inspectors observed fire

protection related activities in the plant. One Severity

Level IV violation was identified concerning two examples of

failure to properly control flammable materials in proximity

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to safety-related equipment (Inspection Report No. 455/86031).

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This violation indicated a reduction in licensee personnel's

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attention to fire protection precautions which merits

management attention.

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Housekeeping and the administration of fire protection programs

were generally found adequate through the assessment period.

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Increased management attention to housekeeping was necessitated

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during this assessment period by the construction activities

of Unit 2 in addition to Unit 1 startup test activities. While

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management was effective in maintaining high levels of

cleanliness, a significant number of shortcomings were

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highlighted to management by the NRC staff based on tours

of the plant. Housekeeping was at a greatly improved level

at the end of the assessment period and further improvements

in the painting of the plant were in progress.

During the Appendix R inspection, a review of the systems

required for safe shutdown including alternate shutdown

capability, a procedural review, and protection for associated

circuits was conducted. Within the majority of areas examined,

the licensee met Appendix R requirements; however, five new

items were identified.

Items such as areas with inadequate

emergency lighting and an Auxiliary Feedwater start switch

cable requiring relocation, although of some significance,

were not materially different from the types of items generally

discovered in Appendix R inspections. Subsequently, the

licensee initiated corrective action for certain of these

items prior to the departure of the inspectors from the site,

while the other items are currently being evaluated by the

licensee.

Management attention and the staffing of fire protection

activities were adequate. The training of fire protection

related individuals was appropriate and the overall level of

resources devoted to this area was sufficient to adequately

meet the needs.

2.

Conclusion

The licensee is rated Category 2 in this area. The licensee

was rated Category 2 in this area in the last SALP.

3.

Board Recommendation

None.

F.

Emeroency preparedness

1.

Analysis

Two inspections were conducted during the assessment period to

evaluate the following aspects of the licensee's emergency

preparedness program: actions on previously identified items;

emergency plan activations; emergency detection and

'

classification; protective action decision-making; notifich*, tons

and communications; shift staffing and augmentation; knowledge

and performance of duties (training); independent audits of

l

emergency preparedness; and changes to the emergency

preparedness program. One of the inspections was an evaluation

of the licensee's annual emergency preparedness exercise

and the other was a routine inspection of the emergency

preparedness program.

l

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"

No violations of NRC requirements were identified during the

inspections.

Management involvement and control in assuring quality in

the emergency preparedness program was demonstrated through

decision-making that has consistently been at a level that

ensures adequate management review and control. Corporate

management is frequently involved in site activities, audits,

and inspections and associated records are generally complete

and readily available. The licensee has provided timely and

sound resolutions to NRC concerns as evidenced by the closure

of all eight open items created during 1985.

Similarly, the

licensee implemented all eight of the improvement items

recommended during 1985, including one that required corporate

assistance.

The licensee demonstrated a high level of proficiency during

the emergency preparedness exercise. Emergency response

organization positions were well defined, authority and

responsibilities specified, and personnel were capable of

implementing their assigned tasks. Staffing to implement

routine daily operations was also well defined and adequate.

The licensee has maintained a prioritized roster of adequate

numbers of qualified personnel to fill the key positions in

the emergency organization. Semiannual off-hours drills have

successfully demonstrated the capability to augment on-shift

staff in a timely manner.

The training program is well defined and implemented with

dedicated resources and included the use of a simulator.

The adequacy of the training program was demonstrated by

individual performances during exercises and walkthrough

interviews.

!

Records of five actual emergency plan activations during this

assessment period indicated that all five had been properly

classified. The NRC and State of Illinois were notified of

these emergency declarations in a timely manner.

Followup

notifications were also completed within adequate time periods

after significant event changes or event termination.

2.

Conclusion

The licensee is rated Category 1 in this area. The licensee

was rated Category 1 in this area in the last SALP.

3.

Board Recommendation

Reduce inspection in this area to the minimum inspection

program.

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G.

Security

1.

Analysis

Three routine and three reactive security inspections and one

Material Control and Accountability inspection pertaining to

Unit I were conducted by regional based inspectors during this

assessment period; three preoperational inspections (two

security and one Material Control and Accountability) regarding

Unit 2 were also conducted by regional based inspectors. The

resident inspectors also made periodic inspections of security

activities assessing routine program implementation and

providing initial responses to security events.

Two violations were identified, a Severity Level III violation

for failure to control access into a vital area (Inspection

Report No. 454/85054) and a Severity Level IV violation for

failure to report a security incident to the NRC within the

time limits required by 10 CFR 73.71(c) (Inspection Report

.

No. 454/85054). The failure to control access led to 2 of

the 3 elements of access control for the affected vital area

being inadequate such that an individual could have gained

unauthorized, undetected access. A civil penalty in the amount

of $50,000 was issued.

In addition, the violation continued

for 26 days before identification by a member of the plant

security force. Once identified, the incident was not reported

to the NRC within the time limits required by 10 CFR 73.71(c).

The above Severity Level III violation, and prior poor

performance in the area of security during the previous SALP

period raised concerns regarding the effectiveness of the Byron

security program. To improve performance in the area of access

control to protected and vital areas, the licensee committed

to implementing a security Performance Improvement Program

,

!

(PIP) as part of the licensee's Conduct of Operations

Improvement Program, focusing on three major areas: (a)

upgrading security education to station personnel and

construction workers; (b) monitoring compliance with security

rules; and (c) actions to improve the effectiveness of security

equipment. The licensee's successful implementation of the

PIP in the first quarter of the assessment period resulted in

improved performance as shown by a significant decrease in

safeguard event reports and irregularity reports. The PIP

also resulted in improved communications between security and

plant operations, and heightened plant security awareness.

During the assessment period, the resident inspector at Byron

received allegations of security violation coverup, fitness

for duty concerns, and security staff shortages. Only the

latter allegation was substantiated; however, there were no

violations of NRC requirements identified.

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Management involvement in assuring quality increased

significantly during the assessment period. The licensee's

Senior Corporate Security Administrators developed and

conducted a training program for all CECO Quality Assurance

(QA) inspectors. The goal of the program was to provide

QA inspectors with an increased security knowledge to provide

improved program effectiveness. The licensee's security

contractor developed and implemented an internal audit

program. The audits conducted to date were thorough,

comprehensive, well documented, and effective in uncoverirg

weaknesses in the security system, procedures and practices.

Security management was responsive to NRC initiatives as

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demonstrated by their full support of the PIP and the

i

successful implementation of Unit 2 security program. Senior

plant management became directly involved in the development

of an increased security awareness in the implementation of

the PIP. Corporate security continues its involvement in

site activities through the presence of the Senior Security

Administrator assigned to the site.

The violations identified during the previous assessment

period were indicative of a significant programmatic breakdown.

Corrective actions had not been successful in preventing

recurrence. The continuation of similar problems necessitated

the formulation of the PIP. The Severity Level III violation

identified during this assessment period occurred during the

developmental stage of the PIP. The results of the PIP

achieved the goals of preventing recurrence of access cortrol

problems and improving performance.

i

The licensee's approach to the resolution of technical issues

'

was viable and generally successful.

In the previous assessment

period, the licensee had not been successful in achieving results

in the security computer system reliability, which involved both

l

l

software and hardware problems. During this assessment period,

l

the computer redundancy problem was resolved; however, the

'

licensee continues to experience unplanned and planned outages.

The licensee is continuing their analysis of this problem.

l

The licensee's staffing levels are adequate to fulfill security

!

plan commitments; however, in June / July 1986, there existed a

I

temporary shortage of personnel because of the additional

l

compensatory posts caused by Unit 2 security construction

requirements necessitating excessive overtime. Positions

within the security organization are identified and authority

,

!

and responsib111 ties are well defined. Major progress was

achieved in stabilizing the contract security force. Contract

security management is providing consistent support and

oversight of the security force. Training policies and

procedures have ensured that all security personnel are trained

and qualified to perform assigned security related tasks or

duties.

~

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There were two security events reported to the NRC under

73.71(c) during the assessment period. These reports were

accurate; however, one of the two was late, resulting in a

Severity Level IV violation. The first event occurred in the

beginning of the assessment period and involved the vital area

access control problem which resulted in a Severity Level III

violation discussed above. The second event pertained to a

guard allegedly sleeping while performing compensatory measures.

The licensee properly analyzed the two events and initiated

appropriate corrective action.

2.

Conclusion

The licensee is rated Category 2 with an improving trend in

this area. The licensee was rated Category 3 in this area in

the last SALP. The improved rating is based on the licensee

security staff's effectiveness in reversing a trend of repeated

access control violations and in establishing an effective

security operation.

3.

Board Recommendation

None.

H.

Outages

1.

Analysis

Three major outages occurred during this assessment period;

there were no refueling outage activities. This functional

area was examined in portions of five inspections conducted

by resident inspectors. Activities covered included reviews

of outage management, including scheduling of parallel path

and non parallel path work.

One Severity Level IV violation was identified for failure to

perform surveillance testing on a containment isolation valve

following maintenance, due to the use of blanket out-of-services

during an outage (Inspection Report No. 454/85048). This

violation was identified by the licensee in an LER and

corrective actions were taken to prevent recurrence.

Management involvement has increased in this area with the

establishment of an Assistant Superintendent - Work Planning

position in the production department. This individual

coordinates the outage schedule and planning functions in

one location; monitors outage performance against planned

schedule; and identifies critical path areas for increased

management attention. A 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> outage schedule is continually

updated to take advantage of any unplanned outage.

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The licensee has increased staffing in this area and has

transferred personnel with operating experience to the outage

group in preparation for the Unit I refueling outage scheduled

for February 1987.

The licensee has taken conservative positions with regard to

scheduling to ensure that redundant trains of safety related

equipment are not worked on at the same time. No significant

initiatives were identified by the NRC in this area.

The licensee has developed computerized out-of-service lists,

by component, and has computerized lists of work surveillances

performed to assist operations department personnel in

determining that all activities are completed prior to

entering the next operational mode.

An additional indication of adequate outage performance is

plant performance during a return to operations. Unit 1

performed well in this regard providing increased assurance

in the licensee's ability to manage outages.

2.

Conclusion

The licensee is rated Category 1 in this area. The licensee

was rated Category 1 in the similar functional area of " Initial

Fuel Load," during the last SALP period.

3.

Board Recommendation

Inspection effort in this area should be maintained during

the approaching first refueling of Unit I which will include

extensive maintenance work,

i

I.

Quality programs and Administrative Controls Affecting Quality

1.

Analysis

Examination of this functional area consisted of four

inspections by regional based inspectors and, as part of

the routine inspection program, portions of 12 inspections

by the resident inspectors. One of these inspections was

conducted on the operational QA program for Unit I and two

were conducted to verify operational readiness in this area

for Unit 2.

Specific areas examined during the inspections

~

included quality assurance program implementation; organization

and administration; procedures; corrective action; document

control; design changes and modifications; equipment calibration

and control; receipt, storage and handling of material; audits;

and procurement. Another inspection was conducted to review

allegations received from QC inspectors for an electrical

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contractor.

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One Severity Level V violation was identified, an isolated

failure to protect plant equipment.

The Severity Level III violation involving a Code Safety

Valve discussed in Section IV.C., Maintenance, resulted from

significant failures in maintenance and quality assurance

programs. Management response to this event was prompt and

thorough and involvement in periodic meetings was good.

Management's approach to resolving technical issues was

conservative, sound, and responsive to NRC initiatives for

improving performance, reducing LERs, housekeeping, and

professionalism.

The inspection of allegations concerning deficiencies in the

Quality Assurance Program of the electrical contractor

commenced during this assessment period. Although the number

and severity level of potential violations identified during

t

the inspection have not been determined, meetings have been

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held with the licensee on issues identified during this

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inspection. Multiple examples of apparent violations of

i

10 CFR Part 21 and 10 CFR Part 50, Appendix B, were identified.

They demonstrated Commonwealth Edison Company's failure to

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exercise adequate oversight and control of their electrical

1

!

contractor to whom they had delegated the establishment and

execution of a quality assurance program in the electrical

area. This occurred in spite of the fact that inspector

concerns had been brought to the attention of the Commonwealth

Edison Company Quality Assurance organization. Deficiencies

identified during this inspection were primarily caused by the

i

lack of performance by those involved with the construction

phase.

l

Two team inspections were conducted during this assessment

period, an inspection by the NRC Nondestructive Examination

(NDE) van team and an inspection by the NRC Office of

Inspection and Enforcement (including consultants) to ensure

that applicabla corrective actions from the Byron Unit 1

Integrated Design Inspection (IDI) and the Independent Design

Reviews (IDR) of Byron Unit I and Clinton Power Station were

being correctly implemented. Although specific items requiring

correction were identified by these inspections, no violations

were identified.

In addition, followup inspections were made

of the NRC Construction Assessment Team (CAT) findings

identified in the last SALP period and found that the licensee

had adequately resolved the issues involved in the three

>

l

violations that were cited by the CAT.

l

Meetings were held periodically between NRC staff and plant

l

management to assess operation of the plant.

Licensee

i

management involvement in the implementation of the quality

assurance program is evident. Audits and surveillances are

being conducted, deficiencies are being identified, and

corrective actions are solving the problems. Quality programs

and the administrative controls affecting quality appear to

be increasingly effective. Plant operation has improved and

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operating events have been reduced as evidenced by the number

of LERs declining from 135 to 39 in this assessment period

and the number of reactor trips dropping from 31 to 6.

Administrative programs for control of procedures, deviations,

modifications, and for response to events and NRC Bulletins

and Information Notices are established and functioning well

with few failures.

Areas in operations where controls

affecting quality were not adequate were identified by the

events involving the Code Safety Valve, and by NRC reviews of

preoperational test results acceptances by the licensee's

Project Engineering Department.

In spite of these,

administrative controls affecting quality have improved overall

4

including enhanced plant features for human factors and the

initiation at the end of the assessment period of a " Plan for

Error-Free Operation".

The " Byron Station Plan for Error-Free Operation of Unit 1

and 2" establishes a Corporate / Station Special Review Committee

to review station performance. The membership of the committee

encompasses corporate and Byron management as well as

bargaining union personnel. The committee is charged with

meeting monthly or more often as necessary and has a list of

topics to be addressed at least semi-annually. The list of

topics touches on all the major areas of plant operations.

The plant features instituted for " human factors" includes

the color codin'g of piping systems, electrical cables and

document cover sheets for Unit 1 and Unit 2.

The licensee has

also established a control board free of caution color lights

under normal plant conditions and has committed to maintaining

a " blackboard", that is a control panel free of nuisance

(repetitive and non-significant) alarms. The licensee has

added other improvements aimed at eliminating human error and

is showing initiative in this area.

2.

Conclusion

The licensee is rated Category 2 in this area. The licensee

was rated a Category 2 in this area in the last SALP.

3.

Board Recommendation

None.

I

J.

Licensing

1.

Analysis

During the assessment period there was a significant level of

licensing activity, especially toward the end of the period.

l

The low power license for Unit 2, and a supporting SER

supplement, were prepared for issuance on October 31, 1986.

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(Incompleteness of the plant delayed issuance of the license

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until November 6, 1986.)

Management involvement and control in assuring quality was

sati sfactory. The licensee's decision-making was usually at a

level that ensures adequate management review. The submittals

needed to support licensing of Unit 2 were almost always

timely, thorough, and technically sound. However, as a result

of the extensive effort involved in licensing Unit 2, some

of the more routine items were not submitted en a timely

basis.

The licensee's overall approach to resolution of technical

issues from a safety standpoint was satisfactory. The licensee

understood the technical issues and responses were generally

sound and thorough. Conservatism was generally exhibited.

Licensee responsiveness to NRC initiatives was good.

In the

weeks prior to the issuance of the Unit 2 low power license,

the licensee responded to many NRC initiatives in a timely

manner and proposed resolutions that were acceptable to the

staff.

In nearly all other instances throughout the rating

period, licensee responses to NRC initiatives were timely,

1

technically sound, thorough, and found acceptable by the NRC.

Plant staffing is amp?e. Key positions are identified and

responsibilities and authorities are well defined. The staff

that will startup Unit 2 has extensive experience on Unit 1;

'

shift advisors, which were needed on Unit 1, are not needed

on Unit 2.

It is anticipated that the well-trained and

experienced Unit 1 staff will provide a smooth startup of

Unit 2 and continued smooth operation of both units.

!

Both the Immediate Notifications and the Licensee Event Reports

suggest, for the most part, that the Licensee took appropriate

action with regard to the reported events.

It was noted,

however, that there were 3 Immediate Notifications of

inoperability of the process computer, with subsequent loss

of emergency assessment, over a 4 day period with no followup

,

report on causes or measures taken to correct deficiencies.

i

This and five late reports lead us to conclude that the

licensee's licensing activities need more management attention.

!

2.

Conclusion

The licensee is rated Category 2 in this area. The licensee

i

was rated a Category 2 in this area in the last SALP.

,

3.

Board Recommendation

1

None.

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K.

Training and Qualification Effectiveness

1.

Analysis

Operator licensing examiners have evaluated training and

qualification effectiveness on senior reactor operator (SRO)

and reactor operator (RO) licensing candidates during

examinations administered during this assessment period.

No violations were identified.

Examinations were administered to 25 SRO candidates and

29 RO candidates. Of these, 19 SR0 candidates and

22 RO candidates passed the examination. This pass rate

is comparable to the national average.

Generic concerns identified by the examiners included the

candidates reluctance to initiate entry into Byron Emergency

Operating Procedures during steam and feed line breaks that

did not cause automatic safety injection or reactor trip

signals. Candidates demonstrated unfamiliarity with xenon

poisoning affects during reactor startup following a trip.

During remote shutdown panel operation candidates were unable

to effectively make a transition to the Emergency Operating

Procedures for a steam line break. The candidates usage

and follow through with Technical Specifications and

administrative procedures was often superficial and incomplete.

As each generic concern was identified over this assessment

period, a discussion was held at length with the plant manager

i

and training staff. The results of which were evidenced in

l

later examinations. This indicated that the concerns

l

identified early in the examination process had been corrected

i

through enhanced training in this area.

l

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Another identified concern was the partial adherence and

compliance with administrative procedures and Technical

Specifications. These difficulties were traced to the teaching

philosophies at the Production Training Center classrooms.

The instructors were not requiring the candidates to review

all of the Technical Specifications due to their understanding

that the NRC examinations did not cover the full spectrum of

understanding and adherence to the action statements, and as

,

a result, this philosophy manifested itself in the area of

Technical Specifications and administrative procedures during

the oral examination phase.

Candidates in general were

competent and sensitive to the Technical Specifications

procedures and action statements and addressed them promptly

during the simulator examinations, indicating that this concern

had been specifically addressed.

However, this indicates a

weakness in training in that candidates may be taught based

on the perceived content of the NRC licensing exam and not

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on the comprehensive tasks which should be included in the

task analysis of all duties required by a licensed individual

to accomplish his job.

The operational unfamiliarity regarding the use of the remote

shut down panel with malfunctions was exhibited during

examinations conducted at the end of this assessment period.

Discussions with the plant manager and training staff resulted

in the licensee's commitment that all candidates in the future

will undergo an enhanced training class to identify and

procedurally respond to malfunctions on the remote shut down

panel.

The generic concerns that were identified as training

weaknesses were in the most part corrected by the licensce.

The ongoing enhanced training program committed to by the

licensee should have a long term beneficial effect to all

candidates. The licensee had received INP0 accreditation

for their non-licensed operator, reactor operator, and senior

reactor operator programs.

Staffing (including management) appears to be adequate and

qualification of training personnel was satisfactory.

Management involvement is required to assure timely and full

INPO accreditation in the remaining seven areas.

The effectiveness of the training received by the Byron staff

is evident in the improved performance observed in the areas

of plant operations, radiological controls, surveillances,

security, and LER report content. Another indicator of the

effectiveness of training and qualification is the personnel

awareness that the plant staff has of their impact on plant

performance.

For example, the I&C technicians take pride in

the fact that they have not been responsible for a plant trip

since late 1985.

2.

Conclusions

,

The licensee is rated Category 2 in this function.1 area.

a

The licensee was not rated in this area in the last SALP.

3.

Board Recommendation

None.

L.

Preoperational Testing

1.

Analysis

This functional area was examined for Unit 2 in four

inspections conducted by region based inspectors and portions

of six inspections conducted by resident inspectors. The

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inspection effort included:

review of administrative controls,

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review of preoperational test procedures, witnessing of

preoperational test performance, detailed reviews of

preoperational test results, verifications of preoperational

test results and reviews of startup test procedures. At the

end of this assessment period, Unit 2 preoperational testing

was almost completed while Unit 2 fuel loading and startup

testing had not yet begun. Unit 1 preoperational and startup

testing were completed prior to this assessment period.

Early in the assessment period, an inspection was conducted

to determine the effectiveness of implementing in the Unit 2

preoperational test program the lessons learned during the

conduct of the Unit 1 preoperational tests.

It was determined

that the licensee had identified Unit 1 test shortcomings and

other lessons learned and was taking action to improve the Unit

2 tests.

In light of the licensee's improvement program and

based on the use of Unit 1 procedures to develop Unit 2

procedures, the NRC reduced inspections of the test procedures.

In the previous assessment period, 7 violations consisting

of 3 Severity Level IV, 3 Severity Level V items, and one item

for which a severity level is yet to be determined (pending

consideration for escalated enforcement action) were identified

over a rating period of 18 months.

In this assessment period,

8 violations consisting of 1 Severity Level IV item, 6 Severity

Level V items and one unresolved item for which a severity level

is yet to be determined (pending consideration for potential

escalated enforcement action) were identified over a rating

period of 12 months. This indicates that the enforcement

history has not changed significantly from the previous SALP

period.

The six Severity Level V violations were judged to have little

safety significance; however, three of the Severity Level V

violations appeared to be indicative of a weakness regarding

administrative aspects of the testing program and indicate

the need for licensee management to exercise more influence

to ensure that administrative requirements are appropriately

followed during the Unit 2 startup testing program. The

Severity Level IV violation concerns the Safety Injection Flow

Balance preoperational test which was written and approved

with inappropriate acceptance criteria in that the test required

several safety-related pumps to equal or exceed the head versus

flow performance curves from the vendor's shop tests (Inspection

Report No. 455/85045). The unresolved item concerns the

inadequate technical evaluation for a preoperational test

deficiency (Inspection Report No. 455/86041).

4

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Inspection Reports Nos. 455/86034 and 455/86041, which documented

three of the seven violations mentioned above and the unresolved

item, were issued subseauent to the assessment period. These

violations are addressed in this report because they reflect on

performance during this assessment period.

Failure to perform an adequate test results evaluation was

identified as a weakness in SALP Reports 4 and 5.

The

unresolved item discussed above represents a continuing

weakness in this area. The test deficiency was written for a

reactor containment fan cooler preoperational test because

the fan flows did not meet the minimum flow requirements of

the FSAR. The Project Engineering Department (PED) evaluated

the deficiency and, based on the evaluation, PED decided that

'

the flows were acceptable regarding low fan speed capacity.

An NRC review of the tu;hnical justification found that it

.

did not provide an adequate technical basis to support this

conclusion. At the end of the assessment period, it was unclear

whether or not the reactor containment fan coolers were capable

of performing the intended safety-related function. This

cannot be resolved until completion of further testing and/or

evaluation. Although preoperational testing is essentially

complete, strong management attention regarding adequate test

results evaluations for Unit 2 startup testing is needed as

evidenced by a weakness being identified in this area for three

,

successive SALP assessment periods.

,

An item which was originally identified during the SAlp 5

assessment period was not addressed in the SALP 5 report

because an investigation by the Office of Investigation (01)

was still in progress at that time. This item consisted of

,

PED approving the results of a Unit I startup test, Reactor

Coolant System Flow Coastdown, which did not meet FSAR

requirements since the measured core flow coastdown data decayed

faster than assumed in the FSAR. Westinghouse performed a new

,

safety analysis which provided revised flow coastdown acceptance

criteria. The flow coastdown test was approved based on the new

acceptance criteria; however, the Byron low power license

required that NRC approval be obtained prior to changing

acceptance criteria and NRC approval was not obtained. The OI

investigation has been completed and subsequent to this SALP

period, an Enforcement Conference was conducted and escalated

,

enforcement is under review regarding this item.

Based on inspector observation, conduct of Unit 2 preoperational

tests improved significantly over Unit I test performance.

Staffing (including management) appears to be adequate and

qualification of test personnel was satisfactory. Management

involvement in the development of the Unit 2 startup procedures

was evident based on the quality of the startup testing

procedures. The NRC's review of the Unit 2 startup test

procedures is complete and no violations or significant

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concerns were identified. Since four of the violations in

this functional area were conteined in reports issued after

the end of the assessment period, the licensee has not yet

responded to these; however, in general, the licensee is

responsive to specific violations and concerns.

j

2.

Conclusion

The licensee is rated Category 2 in this area. The licensee

was rated Category 2 in this area in the last SALP.

3.

Board Recommendation

There is one area, test results evaluations, that appears to

be a pervasive weakness in that it was identified during three

successive SALP periods. Based on this, the board recommends

additional management attention in the area of test results

evaluations for Unit 2 startup tests with special emphasis on

Project Engineering Department's involvement in the test

.

evaluation process.

M.

Construction

1.

Analysis

Construction work at the Byron Station was essentially complete

except in the electrical area; therefore, inspection activities

were limited. This section is a consolidation of several

areas that were addressed separately in previous SALP reports.

Examination of construction was based on the results of 10

inspections by region based inspectors. Areas examined

included: containment structural integrity testing -and welding;

verification of as-built conditions associated with structural

installations, piping systems and onsite design activities;

observation of completed work involved with heating,

ventilating and air conditioning (HVAC) systems and hangers;

observation and review of piping systems examination results;

walkdown inspections of electrical installations to compare

installed components with "as-built" drawings; observation

of electrical and instrumentation cable installation and cable

termination activities; review of electrical installation

procedures and quality assurance records; observation of

'

!

electrical equipment storage and maintenance activities;

walkdown inspections of instrument and control systems; review

of instrument and control quality assurance records; licensee

action on IE Bulletins, previous inspection findings, and

10 CFR 50.55(e) reports; and allegations.

One Severity Level V violation was identified in the construction

area. The violation did not represent a recurrence from the

l

previous assessment period nor were there generic or programmatic

implications.

!

26

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- - - . . -

-.

- -

-

-

. -. -. - - .-- . -

- - -

-

'

-

.

b

The licensee's responsiveness to NRC concerns and resolution

of technical issues were found to be acceptable. Minor

deficiencies identified by the NRC inspectors were immediately

corrected and action ~s taken by the licensee to address open

or unresolved items were found to be acceptable.

Concerns expressed in 4 allegations were reviewed including:

discrepancies in as-built piping drawings, hiring of unqualified

inspectors, and the performance of deficient engineering

calculations.

Review of these concerns was completed. One

concern, dealing with the performance of deficient engineering

calculations was substantiated; however, it was found that

there was no technical basis that resulted in the identification

of a violation of NRC requirements. Another concern dealing

with the same topic was not substantiated; however, the

architect engineer committed to review calculations in addition

to those reviewed by the NRC inspectors. A concern involving

the hiring of unqualified inspectors was found to be

unsubstantiated and a concern dealing with discrepancies in

as-built piping drawings was substantiated; however, no

significant safety problems were identified.

Since construction was essentially completed, licensee

performance in construction areas was collectively evaluated.

The licensee's involvement and control systems were adequate

for dealing with the areas examined.

In general, discussions

with licensee and contractor personnel indicated that they were

knowledgeable of their job duties. Observations indicated that

personnel had an adequate understanding of work practices and

adhered to procedures.

In addition, records were available,

complete, and well maintained. The licensee's responsiveness to

IE Bulletins, Construction Deficiency Reports, and previous NRC

findings was found to be timely, thorough, and technically sound.

Licensee management was very responsive to concerns expressed by

the NRC. For example, as construction came to an end, licensee

management was responsive to reducing the number of open

construction and other items when the NRC identified the high

number as a concern.

2.

Conclusion

The licensee is rated Category 2 in this area. The licensee

was not rated in " Construction during the previous assessment

period, but rather in individual construction functional areas.

In these construction areas which were Containment and Other

Safety-Related Structures, Safety-Related Components, Piping

Systems and Supports, Instrumentation and Control Systems, and

Electrical Power Supply and Distribution, the licensee

received Category 2 ratings.

3.

Board Recommendation

None.

27

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.

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V.

SUPPORTING DATA ANL_ SUMMARIES

A.

Licensee Activ'. ties

1.

Unit 1

During this assessment period, Unit 1 engaged in routine

power operation for extended periods. However, Unit 1

began the assessment period while in an extended

environmental qualification maintenance outage that lasted

until December 17, 1985. Subsequent to the maintenance

outage, Unit 1 experienced two forced outages.

The

average plant availability during the assessment period

was approximately 71%.

The Unit experienced two forced

outages resulting in an average force outage rate of 9%.

Additional Unit 1 outages are summarized below:

Forced outage to repair

July 3 - July 24,1986

-

primary system leaks.

Forced outage to repair

February 17 - March 4,1986

-

damaged transformer. The

plant remained down to

perform scheduled

maintenance outage

activities.

Unit 1 experienced a total of 6 reactor trips during this

assessment period, with 5 occurring above 15% rated power;

and 1 between 0 and 15% power. Three of these trips were

due to procedural inadequacies or personnel errors, 2 were

due to mechanical / equipment problems, and I was related to

an external cause.

In addition to the reactor trips, Unit i

experienced 21 Engineering Safety Feature (ESF) actuations.

i

'

2.

Unit 2

During this assessment period, Unit 2 was considered

'

to be in the construction /preoperational testing phases.

l

Six days subsequent to the end of the assessment period

Unit 2 received its Low Power License limiting the

licensee to fuel loading and initial testing activities up

l

to 5% power. Major milestones accomplished during this

assessment period included: Completion of essentially

100% of construction activities; completion of nearly all

pre-operational testing; activation of the plant security

systems; and close out of nearly all NRC open items and

issues required prior to issuing the low power license.

,

B.

Inspection Activities

There were 67 inspections conducted during this assessment

period, November 1,1986 through October 31, 1986. Major or

'

28

-

---

-

_ __

__

_

.

..

- _ - _ .

--

_.

.

'

.

4

.

significant inspection activities are listed in paragraph 2 of

this section, Special Inspection Summary.

1.

Inspection Data

Facility Name: Byron

Unit: 1

Docket No.: 50-454

Inspection Reports Nos.: 85037, 85047, 85048 thru 85056,

86001 thru 86020, 86022, 86023, 86025, 86029, 86030,

86032, 86039, 86041, and 86044.

Unit: 2

Docket No.: 50-455

Inspection Reports Nos.: 85028, 85031, 85033 thru 85037,

85041, 85044 thru 85047, 86001 thru 86006, 86008 thru

86014, 86016, 86018 thru 86029, 86031 thru 86033, 86035,

86037, and 86039 thru 86041.

TABLE 1

Number of Violations in Each Severity Level

Common

Unit 1

Unit 2

Both Units

Functional Areas

I II III IV V

I II III IV V

I II III IV V

4 1

'-

- -

A.

Plant Operations

-

B.

Radiological Controls

-

- -

-

- -

C.

Maintenance

1

2 1

-

- -

5 2

D.

Surveillance

-

- -

-

1

E.

Fire Protection

-

-

- -

-

F.

Emergency Preparedness

-

- -

-

- -

G.

Security

1

1

-

-

- -

1

H.

Outages

-

-

- -

-

1

I.

Quality Programs and

-

- -

-

-

Administrative Controls

Affecting Quality

J.

Licensing Activities

-

- -

-

- -

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K.

Training & Qualification

-

- -

-

- -

1 6

l

L.

Preoperational Testing

-

- -

-

1

'

M.

Construction

-

- -

-

-

I II III IV V

I II III IV V

I II III IV V

TOTALS

0 0 2 13 5

0 0 0

2 7

0 0 0

0 0

2.

Special Inspection Summary

A Special NRC Independent Measurement

November 7, 1985

-

Inspection and NDE Examinations were conducted (Ref:

455/85031).

29

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- . _ - _ . _ _ - .

. _ - _ . _ . - _

- - - . .

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.

a

-

.

A Team Inspection was conducted to

November 22, 1985

-

ensure that applicable corrective act' ions from the Byron 1

Integrated Design Inspection (IDI) and the Independent

Design Reviews (IDRs) were being correctly implemented on

Unit 2 (455/85047).

C.

Investigations and Allegations Review

Allegation Review

Eleven allegations relating to Byron consisting of 103 concerns

were received in Region III during this assessment period.

Three of the 11 allegations remained open at the end of the

assessment period and will be reviewed by Region III in the

near future.

Significant allegation findings are discussed in

-

Section IV under the appropriate functional area.

D.

Escalated Enforcement Actions

1.

A $25,000 Civil Penalty was issued on June 25, 1986. This

action was based on a Severity Level III v.iolation of

10 CFR 50.70 in which a subcontractor of Commonwealth Edison

Company, discharged an employee for reporting to NRC,

,

inadequate inspection procedures and the insta11atio.n of

non-radiation proof seals at the Byron Nuclear Power station.

This case was being handled by the U.S. Department of Labor

(DOL). The licensee has requested that NRC mitigate this

Civil Penalty. NRC is reviewing the licensee's request.

2.

A 550,000 Civil Penalty was issued March 5, 1986, because of

inadequate vital barriers (454/85054). The licensee has paid

this Civil Penalty.

3.

Escalated enforcement actions were initiated on August 12,

1985, (during the previous assessment period) based on the

conduct of Technical Specification surveillances which rendered

both ECCS systems inoperable, while in MODE 1; and failure of

management and management systems to ensure the unit was

operated in accordance with T.S. requirements. These eyents

were evaluated as two Severity Level III Violations. TWo

$50,000 Civil Penalties were assessed. The first one was

mitigated to $25,000 based on the licensee's response.

4.

A 525,000 Civil Penalty was issued November 18, 1986

'

(subsequent to this assessment period) for a Severity Level

III violation which was the aggregate of three problem areas

(i.e., management oversight of implementation of the QA and

Maintenance programs; failure to control identified

nonconforming material to prevent its inadvertent use; and

the use of a defective component as a fission p"roduct barrier

for the reactor coolant system pressure boundary).

30

.

_ _ - - _. - _ _ -

_ _ _ . _ _ _

. - . _ - -

_.

.. - _ _ - _

O

.

  • -

e

E.

Licensee Conferences Held During Assessment Period

1.

November 20, 1985, January 16, Maren 25, April 22, and June 24,

1986, (Byron Site) - management meetings to discuss Unit 1

operational history and licensee managements efforts to improve

plant and staff performance.

2.

November 22 and 27, 1985, Enforcement Conferences to discuss

the inoperable condition of both RHR trains; operation of

Unit 1 at core thermal power levels in excess of that allowed

by the facility operating license; failure to follow Technical

Specifications (T.S.); and an apparent breakdown in management

controls manifested by T.S. violations.

3.

December 19, 1985, Enforcement Conference to discuss inadequate

plant security regarding removal of vital area barrier floor

plugs.

4.

December 23, 1985, (Regional Office) - a management

meeting was held with licensee representatives to discuss

it's response to the Notice of Violation regarding the

radiation protection inspection conducted May 6 - July 22,

1985.

5.

February 3, 1986, (Byron Site) - a management meeting with

licensee representatives to discuss the SAlp 5 results.

6.

April 21, 1986, Enforcement Conference to discuss a contractors

fiting of an employee performing protected activities.

7.

July 1,1986, (Byron Site) - e management meeting with

licensee representatives to discuss electrical issues at

the Byron station.

8.

August 25, 1986, Enforcement Conference to discuss the Licensee

performance regarding the installation and replacement of a

non-functional primary safety relief valve.

9.

September 11, 25, October 9, and 23, 1986, (Byron Site) -

management meetings to discuss Unit 2 readiness to receive a

low power license.

F.

Confirmatory Action Letters (CALs)

No Confirmatory Action Letters were issued during this assessment

period,

i

31

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o

G.

A Review of Licensee Event Reports, Construction Deficiency

Reports, and 10 CFR 21 Reports Submitted by the Licensee

1.

Licensee Event Reports (LERs)

Byron Unit 1

Docket No. 50-454

LER Nos. 85090, 85092 thru 85102 and 86001 thru 86028

Thirty-nine LERs were issued during this assessment period;

16 LERs were the result of personnel errors; 5 LERs were

the results of procedure inadequacies; 7 LERs were the

result of component / equipment failures; 2 LERs were

related to design problems; and 9 LERs fell into the

others category (i .e., electrical / noise spikes, lightning,

ice). The total number of LERs was markedly reduced from 135

in SAlp 5.

However, personnel errors continue to represent a

significant percentage of the total at 43.6 percent. With

regard to Immediate Notifications, 32 were telephoned to the

NRC within the time limits of 10 CFR 50.72 and 5 were not.

Of

the 5 notifications that were not timely, two were associated

with reactor trips and two were associated with the

inoperability of the process computer and subsequent loss of

emergency assessment.

2.

Analysis and Evaluation of Operational Data (AE00)

The results of the Office of Analysis and Evaluation of

Operational Data (AEOD) assessment of Byron Unit 1 LERs for

this assessment period indicated a major improvement in the

quality of the licensee's issued LERs. AEOD sssessed an

average score of 9.4 out of a possible 10 points, compared

to their previous overall average score of 7.5 and a current

industrial average score of 8.1.

The licensee's current

average score of 9.4 is the highest overal average of all

units / stations that have been evaluated to date. AEOD

considered Byron LERs a model for the industry. Strong points

identified during the AEOD review included the licensee's

discussions concerning personnel errors, and the failure mode,

mechanism, and effect of failed components. AEOD indicated

that improvements in the discussion of corrective actions

in the LER text could be made.

3.

Construction Deficiency Reports (CDR)s:

10 CFR 50.55(e)s

During this assessment period, five CDRs were submitted by

the licensee to Region III for Unit 2 under the requirements

of 10 CFR 50.55(e). One report was closed and one was

subsequently withdrawn. Three remained open at the end of

the assessment period.

32

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0

4.

10 CFR 21 Reports

No 10 CFR Part 21 Reports were submitted by the licensee

during this assessment period for Unit 1 or Unit 2.

H.

Licensing Activities

1.

NRR Site Visits / Meetings / Licensee Management Conferences

Management Readiness Visit for

October 9, 1986

-

Unit 2

Diesel Generator Testing

October 21, 1986

-

LC0 Relaxation Program

December 3, 1985

-

LC0 Relaxation Program

December 6, 1985

-

SALP 5 Presentation

February 3,1986

-

Inadequate Core Cooling Audit

March 25, 1986

-

ISI of Pumps and Valves

July 8, 1986

-

ISI of Pumps and Valves

July 9, 1986

-

Hot Leg Reduction Program

July 25, 1986

-

2.

Commission Meetings

None

3.

Schedule Extensions Granted

,

Construction Completion Date

April 24, 1986

-

Extension for Unit 2.

4.

Reliefs Granted

,

ASME Section XI Relief for

October 29, 1986

-

Unit 2.

5.

Exemptions Granted

None.

6.

Licensee Amendments Issued

Correct typographical and

(

February 13, 1986

-

-

grammatical errors. Amendment 2.

Acceptance criteria for RHR pump

June 6, 1986

-

Performance. Amendment 3.

Five changes (grid plan location,

October 29, 1986

-

weight of uranium, etc.).

Amendment 4.

7.

Other Activities

None.

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33

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_ -..

_

_ _ - _ - _ _ _ _ _ _ _ - . - _ _ _

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--_