ML20210Q500

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Monthly Operating Repts for Apr 1986
ML20210Q500
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 04/30/1986
From: Fay C, Krause C
WISCONSIN ELECTRIC POWER CO.
To:
NRC
References
CON-NRC-86-41 VPNPD-86-210, NUDOCS 8605140107
Download: ML20210Q500 (10)


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8605140107 860430 PDR ADOCK 05000266 R

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1 DOCKET NO.

50-266 UNIT NAME Point Beach, Unit 1 DATE May 5, 1986 COMPLETED BY C. W. Krause TELEPHONE 414/277-2001 l

AVERAGE DAILY UNIT POWER LEVEL MONTH APRIL 1986 AVERAGE AVERAGE AVERAGE DAILY DAILY DAILY POWER LEVEL POWER LEVEL POWER LEVEL DAY MWe NET DAY MWe NET DAY MWe NET l

1 497 11 454 21

-2 l

2 496 12

-5 22

-2 i

3 493 13

-9 23

-2 4

494 ~

14

-7 24

-2 5

495 15

-7 25

-2 6

495 16

-5 26

-2 l

l

- 7, 494 17

-2 27

-2 l

j 8

494 18

-2 28

-2~

9 493 19

-2 29

-2 10

'492 20

-2 30

-2 31 l

EQR-28a l

(04-86)-

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.

50-266 UNIT NAME Point Beach Unit 1 DATE May 5, 1986 REPORT MONTH APRIL 1986 COMPLETED BY C.

W.

Krause ho

+1 c^

N 4-4 Q M c

o un c

o 4

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tD o Ev cm No.

Date N$

E.3 o Licensee Event 8,$

Cause & Correctie Action h

y$

j Report No.

gj

@j To Prevent Recurrence a

e 0 0; un U

2:.c v1 2

860412 S

427.7 C

1 N/A ZZ ZZZZZZ Unit shutdown to commence thirteenth refueling and maintenance outage i

l

(

1 F:

Forced 2 Reason:

3 Method:

4 Exhibit G-Instructions S:

Scheduled A - Equipment Failure (explain) 1 - Manual for preparation of B - Maintenance or Test 2 - Manual Scram data entry sheets C

. Refuelirig 3 - Automatic Scram LER file (NUREG-0161)

D

. Regulatory Restriction 4 - Continuation of

.E - Operator Training &

Previous Shutdown l

Licensing Exain 5 - Reduced Load SExhibit I-Same Source i

F - Administrative 6 - Other (explain) l G - Operational' Error (explain)

H - Other (explain)

AD-28B l

(04-85) l

NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE Docket No.

50-266 Unit Name Point Beach Unit 1 Date May 5, 1986 Completed By C. W.

Krause Telephone 414/277-2001 Unit 1 operated at approximately 494 MWe net from the start of the period until April 12, 1986, when the unit was shut down to commence refueling and maintenance outage No. 13.

Significant maintenance items being completed during the outage include replacement of both trains of the Nos. 1, 2, 3, and 5 feedwater heaters, modifications to the moisture separator reheater internals, replacement of the Unit 1 plant process control computer (P-250), condenser tube replacement, the replacement of power range detectors NE-42 and NE-43 and the upgrade of the control circuits on 20 environmentally qualified valve motor operators.

Eddy current testing in the steam generators was completed and no pluggable indications were discovered.

Fuel motion has been completed.

Evidence of baffle jetting was discovered on one fuel

. assembly which was removed during the fuel shuffle.

The assembly

~had been in core location D12.

The fuel assembly which had been in that location the previous cycle also had failed fuel rods.

Hardware and wiring problems encountered during the startup of the new oxygen gas analyzer have been resolved and the system has been declared operational.

On April 17, 1986, during Operations refueling testing, component cooling water supply check valve 1-755A to the reactor coolant pump s'als was discovered with excessive back leakage.

Maintenance was e

completed and the valve retested satisfactorily. ' Licensee Event Report 86'-002'is being written to further document the event.

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e OPERATING DATA REPORI DOCKET NO. 50-301 F'IE May 5, 1986 COMPLETED BY C. W. KRAUSE TELEPHONE 414 277 2001 OPERATING STATUS

1. UNIT NAME: POINT BEACH NUCLEAR PLANI UNIT 2

. NOTES

2. REFORilNG FERIOD:

. APRIL 1986

3. LICENSED THERMAL POWER (MW1): 1518.
4. NAMEPLATE RATING (GROSS MWE):

523.8

5. DESIGN ELECTRICAL RATING (NET MWE): 497.
6. MAXIMun DEPENDABLE CAPACITY (GROSS MWE) 509.
7. MAXIMUM DEPENDABLE CAPACITY (NET MWE): 485.

S. IF CHANGES DCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:

NOT APPLICABLE

9. POWER LEVEL TO WHICH RESTRICIED, IF AN) (NET MWE): NOT APPLICABLE
10. REASONS FOR. RESTRICTIONS, (If ANY'): NOT APPLICABLE THIS MONTH YR 10 DATE CUhULATIVE 11.. HOURS IN REPORTING PERIOD-719 2,879 120,504
12. NunBER OF HOURS REACTOR WAS CRITICAL 715.2 2,875.2 106,423.8
13. REACIOR RESERVE SHUIDOWN HOURS 0.0 0.0 207.4
14. HOURS GENERATOR ON LINE 705.3 2,855.2 104,655.9
15. UNIT RESERVE SHUTDOWN HOURS 9.9 9.9 244.2
16. GROSS THERMAL ENERGY GENER~ATED (MWH) 1,037,164 4,255,986 147,135,856
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 353,990 1,447,740 4?,863,590
18. NET ELECTRICAL ENERGY GENERATED (MWH) 337,690 1,384,872 47,499,353 19.~ UNIT SERVICE FACTOR 98.1 99.2 86.8 l
20. UNIT AVAILABILITY FACTOR 99.5 99.5 87.1 l
21. UNIT. CAPACITY FACTOR (USING MDC NET) 96.8 99.2 80.3 l
22. UNIT CAPACITY FACTOR (USI.NG DER NET) 94.5 96.8 79.3 l

.23. O' NIT FORCED OUTAGE RAIS 1.9 0.8 1.3 l

24. SHUTD0WNS SCHEDULED OVER NEXT 6 MONTHS (TffE, DATE, AND DURATION OF EACH):

(

Refueling outage scheduled to commence September 26, 1986.

25. IF' SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: NOT SHUTDOWN DATA. REPORTED AND FACTORS CALCULATED AS REQUESTED IN NRC LETTER DATED SEPTEMBER 22, 1977 i

DOCKET NO.

50-301 l

UNIT NAME Point Beach, Unit 2 l

l DATE May 5, 1986 COMPLETED BY C. W. Krause TELEPHONE 414/277-2001 AVERAGE DAILY UNIT POWER LEVEL MONTH APRIL 1986 l

t AVERAGE AVERAGE AVERAGE DAILY DAILY DAILY POWER LEVEL POWER LEVEL POWER LEVEL DAY MWe NET DAY MWe NET DAY MWe NET 1

469 11 492 21 492 2

494 12 492 22 491 3

494 13 492 23 498 4

493 14 492 24 488 5

475 15 491 25 491 6

479 16

'492 26 493 7

494 17 492 27 492 l

8 493 18' 491 28 489 9

~493 19 492 29 159 10 492 20 470 30 206 31 EQR-28a

~

(04-86)

.- ~

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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.

50-301 UNIT NAME Point Beach Unit 2, DATE May 5,-1986 REPORT MONTH APRIL 1986 COMPLETED BY C. W. Krause ho a

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G No.

Date p,

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-Report No.

$8

@8 To Prevent Recurrence o

G c as u) o 2: a u) 2 860429

'F 13.7 G-2 86-001 ZZ ZZZZZZ Reactor trip due to technician error during reactor protection logic testing 2

8 Method:

4 Exhibit G-Instructions 1F:

Forced :

2 Reason:

S:

Scheduled

.A - Equipment Failure (explain) 1 - Manual for preparation of B - Maintenance or Test 2 - Manual Scram data entry sheets C - Refueling 3 - Automatic Scram LER file (NUREG-0161)

D - Regulatory Restriction 4 - Continuation of E - Operator Training &

Previous Shutdown Licensing Exam 5 - Reduced Load sExhibit I-Same Source F - Administrative 6 - Other (explain)

G - Operational Error (explain)

H - Other (explain) e AD-28B (04-85)

o.

.g o

NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE Docket No.

50-301 Unit Name Point Beach Unit 2 Date May 5, 1986 Completed By C. W. Krause 4

Telephone 414/277-2001 Unit 2 operated at approximately 493 MWe net from the start of the period until 0729 hours0.00844 days <br />0.203 hours <br />0.00121 weeks <br />2.773845e-4 months <br /> on April 29 when a reactor / turbine trip occurred.

The trip was the result of a technician error which occurred during reactor protection logic testing.

The reactor was taken critical at 1114 hours0.0129 days <br />0.309 hours <br />0.00184 weeks <br />4.23877e-4 months <br /> and the generator was placed on line at 2109 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.024745e-4 months <br /> the same day.

Currently, the unit is at full power.

Licensee Event Report 86-001 is being drafted to further document the event.

Safety related maintenance included the replacement of jumper wires in the control circuits in the environmentally qualified valve motor operators.

k 4

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SUPPLEMENT TO MONTHLY REPORT FOR Apr#1 1986 REFUELING INFORMATION REQUEST In accordance with our letter dated February 21, 1978, which provided certain refueling infonnation, we are providing the following update to that refueling information:

(NC = No Change) a) Next Scheduled Refueling Shutdown:

Unit 1:

April 11. 1936 Unit 2:

Sect. 26. 1986 b) Scheduled Date for Restart:

Unit 1:

May 26. 1986 Unit 2:

November 11. 1986 c) License Amendment Required / Staff 10 CFR 50.59 Review Completed:

Unit 1:

50.59 Review Complete Unit 2:

October 1986 d) Scheduled Date for Submitting Supporting Information:

Unit 1:

NA Unit 2:

NA e)

Important Licensing Considerations:

Unit 1:

2nd Reaion 0FA Fuel Unit 2:

3rd Reaion 0FA Fuel f) Number of Fuel Assemblies in Storage Pool:

788 g) Other:

Three fuel assemblies were shipped to Battelle in Fall 1985.

l

^

WlSCORSin Electnc ma coumr 231 W. MICHIGAN. P.O. BOX 2046. MitWAUMEE. WI 53201 VPNPD-86-210 NRC-86-41 May 9, 1986 Director of Nuclear Regulatory Operations U. S. NUCLEAR REGULATORY COMMISSION Washington, D. C.

20555 Gentlemen:

MONTHLY OPERATING REPORTS POINT BEACH NUCLEAR PLANT Att ached are monthly operating reports for Units l 'and 2, Point Beach Nuclear Plant, for the calendar month of April 1986.

Very truly yours, 6'

ffd-C. W. Fay Vice President Nuclear Power Attachments Copies to R. S. Cullen, PSCW J. G. Keppler, NRC Region III NRC Resident Inspector

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