ML20207T482

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Insp Repts 50-338/87-01 & 50-339/87-01 on 870112-0220. Violation Noted:Failure to Provide Maint Procedure & Perform post-maint Testing on Control Room Emergency Ventilation Sys.Violation Will Not Be Cited,Per 10CFR2,App C
ML20207T482
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 03/10/1987
From: Caldwell J, Cantrell F, King L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20207T474 List:
References
TASK-2.K.3.31, TASK-TM 50-338-87-01, 50-338-87-1, 50-339-87-01, 50-339-87-1, IEIN-85-017, IEIN-85-17, IEIN-86-053, IEIN-86-057, IEIN-86-53, IEIN-86-57, NUDOCS 8703240061
Download: ML20207T482 (15)


See also: IR 05000338/1987001

Text

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION il

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101 MARIETTA STREET.N.W.

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ATLANTA. GEORGI A 30323

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Repert Nos.: ~50-338/87-01 and 50-339/87-01

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Licensee: Virginia Electric & Power Company

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Richmond, VA 23261

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Docket'Nos.: 50-338 and 50-339

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Facility Name: North Anna l'and 2

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Inspection Conduc d

nua y 12 - February 20,s1987

Inspectors:

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w 11, SRI

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L. P. King, RI

Date Signed

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Approved by:

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F. Cantrell, Sectian',C

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Datd Signed

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Division of Reactor Pr ects

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SUMMARY

Scope:

This routine inspection by the resident inspectors involved the

following areas: plant status, unresolved items, licensee action on previous

enforcement matters, review of inspector followup items, monthly maintenance

. observation, monthly surveillance observation, ESF walkdown, operational safety

verification, maintenance program implementation, temporary instruction 2515/80

" Data Collection for the Performance Indicator Trial Program", TMI Item

II.K.3.31, IEIN 86-53, and region based inspector review of the Semi-Annual

Effluent Report for January - June, 1986.

Results: One violation was identified - failure to provide a maintenance

procedure and perform post maintenance testing on the control room emergency

ventilation system - see paragraph 6.

This violation was determined to meet the

criteria of 10 CFR 2 Appendix C for a licensee identified violation and will not

be cited.

8703240061 870312

PDR

ADOCK 05000338

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PDR

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REPORT DETAILS

1.

Licensee Employees Contacted

  • E. W. Harrell, Station Manager
  • R. C.'Driscoll,-Quality Control (QC) Manager

G. E. Kane, Assistant Station Manager

  • E. R. Smith, Assistant Station Manager
  • R. 0. Enfinger, Superintendent, Operations

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  • M. R. Kansler, Superintendent, Maintenance

A. H. Stafford, Superintendent, Health Physics

  • J. A. Stall, Superintendent, Technical Services

J. L. Downs, Superintendent, Administrative Services

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J. R. Hayes, Operations Coordinator

D._A. Heacock, Engineering Supervisor

D. E. Thomas, Mechanical Maintenance Supervisor

G. D. Gordon, Electrical Supervisor

R. A. Bergquist, Instrument Supervisor

F. T. Termine11a, QA Supervisor

  • J. P. Smith, Superintendent, Engineering

D. B. Roth, Nuclear Specialist

J. H. Leberstein, Engineer

  • G. G. Harkness, Licensing Coordinator

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Other licensee employees contacted include technicians, operators,

mechanics, security force members, and office personnel.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized on February 17, 1987,

with those persons indicated in paragraph 1 above. The licensee

acknowledged the inspectors findings. The licensee did not identify as

proprietary any of the material'provided to or reviewed by the inspectors

during this inspection.

(0 pen) Violation 338,339/87-01-01 - Failure to provide a maintenance

procedure' and perform post maintenance testing on the control room

emergency ventilation system (paragraph 6)

(0 pen)

Unresolved

Item 338,339/87-01-02

Reverification of the

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acceptability of the recirculation spray heat exchanger (paragraph 11)

(0 pen) Inspector Followup Item 338,339/87-01-03 - Potential ASCO solenoid

valve problem (paragraph 11)

(0 pen) Unresolved Item 339/87-01-04 - possible inoperability of the 2H and

2J EDGs (paragraph 11)

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(0 pen) Unresolved Item 338,339/87-01-05

Raychem splice problem

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(paragraph 15)

3.

Plant Status

Unit 1

Unit 1 began the inspection period operating at approximately 100% power

and maintained that power level through to the end of the inspection

period. Unit I has been operating on line without interruption for 111

days.

Unit 2

Unit 2 began the inspection period operating at approximately 100% power

and maintained that power level through to the end of the inspection

period. Unit 2 has been operating on line without interruption for 124

days.

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4.

Unresolved Items

An Unresolved Item is a matter about which more information is required to

determine whether it is acceptable or may involve a violation or

deviation.

Three unresolved items were identified during this inspection and are

discussed in paragraphs 11 and 15.

5.

Licensee Action on Previous Enforcement Matters (92702)

(Closed) Violation 338,339/86-25-01:

Failure of Licensee to Incorporate

Technical Specification Amendments Properly: The inspectors reviewed the

licensee's corrective actions and determined them to be acceptable.

(Closed)

Violation 338/86-17-03:

Failure to Perform a Written Safety

Evaluation. This violation was originally closed in inspection report

338,339/86-24.

However, the licensee changed their response in a letter

dated November 25, 1986.

This new response changes their commitment to

perform a 10 CFR 50.59 safety evaluation on all temporary modifications.

In the new response the licensee committed to perform technical

evaluations on all temporary modifications, but will only follow the rules

of 10 CFR 50.59 for the temporary modifications which fall under the rule.

The inspectors concur with the change to the original response and all the

requirements of 10 CFR 50.59 must continue to be met by the licensee.

6.

License Event Report (LER) Follow-up (90712 & 92700)

The following LERs were reviewed and closed. The inspector verified that

reporting requirements had been met, that causes had been identified, that

corrective actions appeared appropriate, that generic applicability had

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been considered, and that the LER forms were complete. Additionally,.the

inspectors confirmed that-no unreviewed safety questions were involved and

. that violations of regulations or Technical Specification (TS) ' conditions

had been identified.

. (Closed) LER 338/86-06: : Reactor Trip. The cause of the "B" sain steam

' line isolation valve inadvertently closing was investigated.

Shaft

movement was measured against the "A" and "C" valves. The-testing did not

disclose any problems.

The best' estimate of cause is prior damage-

sustained to at least one of the rupture diaphragms.

(Closed) LER 339/86-06 (Rev 0 and 1):

Forced Unit Shutdown, Station

Batteries Inoperable. The Administrative Procedure 3.1 has been revised

to ensure that TS . surveillance requirements are satisfied during the

design change process.

(Closed) LER 338, 339/85-31: Control Room Bottled Air System Inoperable.

Action has been taken in licensed operator retraining. to discuss the

event. Guidelines have been issued by the operations manager as to when

to enter an action statement.

(Closed) LER 338/85-20 (Rev 0 and 1): Steam Generators Tube Defects. The

licensee submitted Steam Generator Tube Integrity Reports prepared by

Westinghouse. These reports were submitted November 25, 1986.

(0 pen) LER 338, 339/86-19:

Control Room Emergency Ventilation System

High Flow Rates Due to Inadequate Post Maintenance Testing. During the

week of December 1-5, 1986, a team of NRC inspectors working with licensee

personnel identified to the licensee that the control room' emergency

ventilation system flow rates were outside TS requirements (see inspection

raport 338,339/86-28). The licensee verified this finding and took the

necessary corrective actions to bring the flow rates back into compliance

with TS.'LER 338, 339/86-19 was issued by the licensee to document this

problem and describes the cause for the emergency ventilation system flow

rates to be outside of TS criteria.

The LER states that maintenance,

consisting of cleaning the inlet filters, was performed on the control

room emergency ventilation systems in June of 1986. This maintenance was

performed under a work request but without a maintenance procedure or the

performance of a post maintenance test. The licensee contends that the

cleaning of the inlet filters, which was performed for the first time,

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caused the emergency ventilation system flow rates to increase above the

TS limits. The LER also states: "Since a maintenance procedure did not

exist, post maintenance testing requirements were not identified." This

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implies that a review for post maintenance testing requirements is only

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accomplished when a maintenance procedure is issued.

The inspector

determined that this assumption is incorrect. A review of Administrative

Procedures (ADM) 16.5, Work Request (WR) and 16.7, Corrective Work Orders,

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revealed numerous requirements for both the shop foreman and shift

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supervisor to review:

the work request; the work order prior to work

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starting; and finally the work order after the work is complete, to

determine if adequate post maintenance is performed. These reviews for

post maintenance testing are required to be performed regardless of

whether a maintenance procedure is issued or not.

Technical Specification (TS) 3.7.7.1.a requires the control room emergency

ventilation system to be operable. TS action statement 3.7.7.1.a states

in part, with the emergency ventilation system inoperable, restore the

inoperable system to operable status within 7 days or be in at least hot

standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in at least cold shutdown within the

following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

The failure of the licensee to perform a post

maintenance test following maintenance in June 1986 resulted in the

emergency ventilation system being inoperable from June 1986 until

December 1986 when discovered by the NRC. This failure to comply with TS 3.7.7.1.a will be identified as a violation.

The inspector questioned the licensee on the safety significance of the

control emergency ventilation system flow rates being in excess of the TS

limits. The licensee discussed the situation with the vendor using the

maximum flow rates discovered. Based on the normal filter efficiency, the

vendor supplied information and the licensee's engineering evaluation, the

emergency ventilation system effectiveness at the higher flow rates was

determined to still be better than assumed in the FSAR.

After an evaluation in conjunction with Region II personnel and

considering that the abnormal flow was identified in a joint effort by the

NRC and the Licensee, corrective action was instituted promptly to correct

the abnormal flow, action was initiated to prevent recurrence and the

discrepancy was reported as required, this event meets the requirements of

10 CFR 2, Appendix C as a Licensee identified violation (LIV). The LER

and a LIV will remain open to track completion of all the proposed

corrective action.

7.

Review of Inspector Follow-up Items (92701)

(0 pen) Unresclved Item 338,339/86-28-02: This unresolved item identified

two potentially inadequate surveillance procedures. The licensee has been

able to show that the surveillance procedures verifying control room

emergency ventilation system flow rates were adequate to ensure compliance

with Technical Specification (TS).

This item will remain unresolved

pending the determination of adequacy of the surveillance procedure for

verifying control room bottled air system compliance with TS.

8.

Monthly Maintenance (62703)

Station maintenance activities affecting safety related systems and

components were observed / reviewed, to ascertain that the activities were

conducted in accordance with approved procedures, regulatory guides and

industry codes or standards, and in conformance with Technical Specifi-

cations.

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Early in February 1987 a refurbished charging pump motor was installed on

Unit I charging pump 1-CH-P-1. This charging pump has been inoperable for

the past several months. PT 14.3 was performed satisfactorily to determine

operability of the charging pump. The only problem associated with the

maintenance was a small leak on the outboard pump bearing which was

repaired.

The inspector observed maintenance on Unit 1 "B" main feedwater regulating

valve.

The Baily feedwater positioner feedback cam and roller were

replaced.

This prevents hunting of the valve caused by excessive wear.

The procedure (IMP-C-MISC-05) for troubleshooting, repair and replacement

of non-safety related equipment was used. The parts were replaced without

any problems.

On February 12, 1986, the inspector reviewed EWR 87-123 " Instructions for

MOV Modification and Switch Valve Settings for Compliance with IE Bulletin 85-03 Valve Program." This, together with EMp-P-MOV-3 Predicative Analysis

of Motor Operated Valves, was being used to adjust the torque switch

setting on 2-CH-MOV-2286C.

The result of the test required readjustment

of the torque setting upward.

The inspector reviewed work taking place on the "A" gas stripper. Welding

repairs were being made to various reach rods. The welding permit was

also reviewed.

The inspector observed the welding on the cooling water line to the lube

oil cooler on the turbine driven feedpump on Unit 1.

The procedure used

was MMP-C-W-1 " Mechanical Welding Procedure for Preparation of Welding on

Safety Related Equipment".

No violations or deviations were identified.

9.

Monthly Surveillance (61726)

The inspectors observed / reviewed Technical Specification required testing

and verified that testing was performed in accordance with adequate

procedures, that test instrumentation was calibrated, that limiting

conditions for operation (LCO) were met and that any deficiencies

identified were properly reviewed and resolved.

On February 4,1987, the inspector observed the performance of 1-PT-77.1A

" Safeguards Area Ventilation System Flow Test Train A Filter".

No

problems were identified.

On February 12, 1987, the inspector reviewed 1-PT-15.1 " Boric Acid

Transfer Pump Test".

No problems were identified.

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On January 29,

1987, the inspector observed the performance of

surveillance' test 1-PT-57.2 " Valve Inservice Test (SI)".

This test

performs the stroke time testing of MOV-1860B and MOV-1863A, the Low Head

Safety Injection (LHSI) pump 18 Suction Valve and 2A Discharge Valve

respectively.

Following the test performance, the inspector discussed

with the licensee the need to evaluate the operability of TS equipment on

which surveillance tests are being performed. If the surveillance test or

any other operation places the TS equipment in a condition which will

prevent it from performing its safety function upon receiving an automatic trip signal, then the equipment is considered inoperable. An example of

this is illustrated by 1-PT-57.2 where the suction valve to.the LHSI pump

from the RWST was shut to allow the cycling of MOV-18608. During this

operation, the LHSI pump is technically inoperable, and the TS action

statement must be entered. The licensee acknowledged this requirement.

The inspector will continue to monitor surveillance tests and other

operations to determine if the licensee's evaluation for equipment

operability is being properly implemented.

On February

8,

1987, the inspector observed the performance of

surveillance test 1-PT-31.7.2 " Pressurizer Level Channel II (L-460)

Functional Test" and 1-PT-32.1.4 " Steam Generator IA' Narrow Range Level

Protection Channel II (L-475) Functional Test".

On February 11, 1987, the inspector observed portions of 2-PT-21.1

" Reactor Core Flux Mapping".

No violations or deviations were identified.

10.

ESFSystemWalkdown(71710)

The following selected ESF systems were verified operable by performing a

walkdown of the accessible and essential portions of the systems on

February 13, 1987.

A walkdown was performed on the auxiliary feedwater system for Unit I

using 1-0P-31.2A,

No discrepancies were noted.

All the valves were

labeled properly with the valve number and functional description.

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No violations or deviations were identified,

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11. Operational Safety Verification (71707)

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By observations during the inspection period, the inspectors verified that

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the ' control room manning requirements were being met. In addition, the

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inspectors observed shift turnover to verify that continuity of system

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status was maintained. The inspectors periodically questioned shift

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personnel relative to their awareness of plant conditions.

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Through log review and plant tours, the inspectors verified compliance

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with selected Technical Specification and Limiting Conditions for

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Operations.

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In the course of the monthly activities, the resident inspectors included

a review of the licensee's physical security program. The performance of

various shifts of the security force was observed in the conduct of daily

activities to include: protected and vital areas access controls,

searching of personnel, packages and vehicles, badge issuance and

retrieval, escorting of visitors, patrols and compensatory posts.

In

addition, the resident inspectors observed protected area lighting,

protected and vital areas barrier integrity and verified an interface

between the security organization and operations or maintenance.

On a regular basis, radiation work permits (RWP) were reviewed and the

specific work activity was monitored to assure the activities were being

conducted per the RWPs. Selected radiation protection instruments were

periodically checked and equipment operability and calibration frequency

was verified.

The inspectors kept informed, on a daily basis, of overall status of both

units and of any significant safety matter related to plant operations.

Discussions were held with plant management and various members of the

operations staff on a regular basis. Selected portions of operating logs

and data sheets were reviewed daily.

The inspectors conducted various plant tours and made frequent visits to

the Control Room. Observations included: witnessing work activities in

progress; verifying the status of operating and standby safety systems and

equipment; confirming valve positions, instrument and recorder readings,

annuciator alarms, and housekeeping.

The following comments were noted:

The Senior Resident Inspector at the Surry Power Station (SPS) informed

the residents of a potential problem with the Recirculation Spray Heat

Exchanger (RSHX) diaphragm seals. The SPS has replaced their one quarter

inch thick diaphragms with approximately one inch thick diaphragms to

correct the problem of weld cracks and flexing of the diaphragms during

the type A pressure tests. Since the North Anna Power Station (NAPS) has

similar designed RSHXs and the diaphragm seals are only one eighth inch

thick, the inspector questioned the operability of the RSHXs at NAPS. The

NAPS engineering staff informed the inspectors that the question of the

diaphragm withstanding Design Base Accident (DBA) pressure was addressed

1984. The NAPS staff was informed by Stone and Webster (S&W) in a letter

dated September 7,1984, that "The resulting stresses and strains in the

diaphragms for a DBA pressure loading will be well below ultimate.

Since

the diaphragm plate and its weld to the flange will have strains well

below ultimate, neither will fail during the DBA." This letter, however,

went on to say that the diaphragms would have stresses above their yield

values causing the diaphragm to flex during the type A pressure test with

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no service water flow on the other side of the diaghragm. Therefore, the

licensee installed Dow Corning 3145 RTV adhesive sealant between the outer

edge of the diaphragm and the strong back isolating the diaphragm but not

the weld from the type A pressure test. This would minimize the flexing

of the diaphragm during type A testing.

The inspectors reviewed the licensee's justification for the use of RTV

sealant and the S&W 1etter verifying that the one eighth inch thick

diaphrages were acceptable. However, the inspectors were still concerned

with the fact that SPS replaced their one quarter inch thick diaphragms

with much thicker diaphragms and were issuing a 10 CFR Part 21 report even

though they were aware of the S&W evaluation. The licensee was requested

to determine if there existed any difference in the SPS evaluation and the

NAPS evaluation of the problem. On February 6, 1987, the corporate office

issued a potential Part 21 report recommending a thorough technical review

be performed of both stations' evaluations of the diaphragm seal problem

and to perfonn a reverification of the S&W calculation prior to the

determination of Part 21 reportability. On February 13, another report

was issued from the corporate engineering staff addressing their review of

RSHX designs at SPS and NAPS to evaluate the potential for failures during

the DBA condition that could result in a significant safety hazard. This

report concluded that the designs at both plants were deficient in that

external pressure loading was not considered in the original equipment

design. However, the report went on to say that failures of the diaphragm

or its weld would not occur as a result of the DBA and the design

currently installed at NAPS did not pose a safety hazard for near term

operation. The engineering staff recognized that the effectiveness of the

RTV seal installed at NAPS was not verifiable and therefore not suitable

for long term operation. Consequently, the engineering staff recommended

that a permanent modification be installed at NAPS during the 1987

refueling outage.

In the body of the report issued February 13, 1987, the reverification of

the 1984 calculations performed by S&W for NAPS revealed a new

requirement.

S&W, in a letter dated February 12, 1987, informed the

licensee that their previous evaluation was acceptable with an additional

caveat that the fatigue life of the diaphragm consisted of only five

cycles. On February 16, 1987, the NAPS staff determined that Unit I upper

RSHX diaphragms had undergone six pressurization events (cycles). During

one of the cycles, service water was flowing through the RSHXs preventing

the differential pressure across the diaphragm from flexing the diaphragm.

This reduced the number of cycles to five.

Since the S&W evaluation

indicated a limit of five cycles and a DBA would place the Unit 1 RSHX

upper diaphragm seals in a six cycle condition, the licensee prepared a

Justification for Continued Operation (JCO). This JC0 takes credit for

the RTV installed on the diaghragm to prevent the diaphragm from seeing

the DBA pressure, even though the effectiveness of the RTV is not

verifiable, along with assurance from S&W via a telephone conversation

that new calculations will confirm the acceptability of the current number

of pressurization events (cycles).

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On February 18, 1987, a discussion of the RSHX situation and the

associated JC0 at NAPS was conducted between the resident inspector and

Regional and NRR staffs. Both the Region and NRR concluded that the JC0

was acceptable for short term continued operation, but the licensee must

expedite the results from S&W showing that they can exceed five cycles on

the Unit 2 RSHX diaphragm without a failure. On February 20, 1987 NAPS

stated in a conversation with the NRC that preliminary, unchecked S&W

elastic / plastic finite element analysis indicates that ten cycles are

acceptable. NAPS stated that the supporting data calculations should be

available on March 3, 1987.

Problems with the acceptability' of the RSHX diaphragm seals were first

identified by SPS in 1980, and the question war raised again at NAPS in

1984. The most recent question on the Part 21 reportability was raised by

SPS late in 1986 and now in February 1987, VEPC0 has determined that the

design deficiencies with the RSHX diaphragm are indeed reportable. During

the recent evaluation, both the SPS units were in cold shutdown and

therefore the diaphragms could be replaced with thicker ones. However,

both the NAPS units were operating at 100% power.

The inspector is

concerned that once the question of a design deficiency sufficient enough

to cause the replacement of the diaphragms at SPS and the consideration of

Part 21

reportability was identified, the reverification of the

acceptability of the NAPS RSHX diaphragm was not pursued in an expeditious

manner.

This

item will

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identified as

an Unresolved Item

(338,339/87-01-02) pending the results of the S&W calculations and further

review by the inspectors.

During a review of the Reactor Operators (RO) log on February 2,1987, the

inspectors discovered that 2-TV-BD-200F, "C" Steam Generator (SG) inboard

isolation valve, failed to shut after the solenoid valve had been

de-energized. This valve was being cycled per 2-PT-213.1 Valve Inservice

Inspection (Blowdown System) on January 31, 1987. The R0 log stated that

after mechanical agitation of its solenoid valve, 2-TV-BD-200F closed.

Since this valve is normally open during operation and is required to shut

for containment isolation on either a loss of power or a trip signal to

the solenoid valve the inspector questioned the operability of the trip

valve and its solenoid. The inspector was informed that the solenoid

which failed to operate until mechanically agitated, was manufactured by

Automatic Switch Company (ASCO).

The inspector, aware that other

facilities had identified problems with possible sticking of ASCO solenoid

valves as documented in IE Information Notices (IEIN) 85-17 and 86-57,

again questioned the operability of 2-TV-BD-200F since the licensee

had not determined the root cause of the valve's failure to close. The

inspector also reviewed the licensee's evaluation of IEIN 85-17 and 86-57

and determined the response basically concluded that NAPS did not use the

same model of ASCO solenoid listed in the IEINs. Based on the inspector's

questions, the licensee has committed to cycling 2-TV-BD-200F weekly for a

period of time to ensure that the solenoid valve is operating properly, to

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re-evaluate IEIN 85-17 and 86-57 for generic applicability and to review

the maintenance history to determine if this problem has occurred before.

The licensee has conducted two weekly performances of 2-PT-213.1 with

satisfactory results. The inspector witnessed the first weekly cycling of

2-TV-BD-200F conducted on February 5,1987.

The licensee's commitments

relating to the potential ASCO solenoid valve problem will be identified

as an Inspector Follow-up Item, 338,339/87-01-03.

Along with the follow-up of the 2-TV-BD-200F failure to close, the

inspector reviewed a Deviation Report (DR)87-105 dated February 4, 1987.

This DR identified that the corporate engineering staff became aware late

in 1986 of a potential deficiency in the Environmental Qualification (EQ)

documentation of ASCO solenoid valves.

The DR states that the EQ

evaluation did not take into account the internal heating effects (self

heating) of continuously energized solenoid valves as it pertains to

thermal aging and subsequent qualified life calculations. On December 12,

1986, the licensee requested information on the internal heating effects

from ASCO and received this information on January 9,

1987.

This

information indicated that a significant increase in temperature could be

expected in various portions of the solenoid valve if left continually

energized.

This increased temperature could result in significant

reduction in the qualified life of the ASCO solenoid valves. The DR which

was issued to the plant on February 4,1987, stated that a preliminary

evaluation performed by the corporate engineering staff determined that

maintenance would not be required until sometime in 1988. Therefore, they

concluded that safety system operability was not currently affected. The

planned corrective actions are to identify all solenoid valves which are

continuously energized, identify the critical elastomer for the safety

function and recalculate the qualified life.

On February 9,1987, the licensee reported to the NRC that the potential

existed for both the Emergency Diesel Generators (EDGs) for Unit 2 to have

been inoperable at the same time during the month of January 1987. This

identification resulted from a review of a plant Deviation Report (DR)87-102 issued on February 3,1987, for the 2H EDG and another DR 87-113

issued on February 6, 1987, for the 2J EDG, The review of DR 87-102 which

identified that the 2H diesel governor load limit was set at the 3000KW

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setpoint instead of the maximum setpoint, was determined to be

non reportable because the 2J diesel generator was considered operable.

However, following a review on February 9, 1987, of DR 87-113 which stated

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the same problem existed with the 2J EDG governor load limit, the licensee

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had to conclude that both EDGs could have been inoperable at the same

time. At the time of the discovery of the first event on February 3,

1987, it was reported that the other three EDGs 1H, IJ and 2J had been

checked and the governor load limits were set at maximum. However, after

the discovery of the 2J EDG governor load limit setting of 3000KW on

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February 6,1987, the operators could not remember whether or not 2J.

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which is the EDG located in the last room at the end of the hall, had been

checked on February 3, 1987. TS 3/4 8.1.1.e. requires, with both diesel

generators inoperable, that two offsite A.C. circuits be demonstrated

operable within one hour, and one diesel generator be restored to

operability within two hours or be in at least hot standby within the next

six hours.

The licensee determined the last time the governor was adjusted to the

3000KW setpoint was in the December 1986 to January 1987 time frame during

the performance of a special test, ST ST-69 " Determination of EDG Load

Limiter 3000KW Setpoint", on all four EDGs. The special test was being

conducted in parallel with the normal monthly EDG surveillance test for

the purpose of permanently marking on the EDG load limiter the 3000KW

setpoint. This 3000KW determination was being made for future reference

in case the engineering evaluation could justify leaving the governor load

limiter at the 3000KW setpoint instead of maximum.

This engineering

evaluation is being performed in an attempt to minimize the overloading of

the EDG during operation. The overloading of the EDG has been identified

as one of the causes of previous diesel generator failures. A review of

the completed surveillance procedures revealed that single verification of

the governor load limiter being returned to maximum had been performed on

both the 2H and 2J EDG during the completion of the monthly surveillance

tests in January 1987. This verification was not made by the individual

who signed the procedure but was made based on a report from personnel in

the EDG room performing the surveillance.

The returning of the load

limiter to the maximum setpoint should have been double verified because

of its safety significance. The licensee returned the governor settings to

maximum immediately following their discovery.

The operators performing

the rounds of the EDG compartments are now required to record the position

of the governor setting each shif t.

The licensee is also performing a

human factors investigation in an attempt to determine the cause of the

event.

This item will be identified as an Unresolved Item 339/87-01-04

pending the determination of the diesels operability and the cause of the

event.

12. Maintenance Program Implementation (Units 1 and 2) (62700)

The inspector reviewed the implementation of the maintenance program to

determine if it is meeting regulatory requirements, to determine the

effectiveness of the program on important plant equipment, and review the

maintenance staff's activities in this area. This review consisted, in

part, of a review of equipment operating history for specific component

failures leading to plant shutdowns and recurring safety related equipment

failure. This review included a review to assure that procedures were

followed during the maintenance process.

In addition, various records

associated with the maintenance activities performed were reviewed to

assure approved procedures were used when required, limiting conditions

for operations were met while the work was being performed, procedures

were adequate for the work being performed, functional testing was

performed as required, measuring and test equipment used was calibrated

and controlled, personnel were trained to perform the maintenance as

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necessary, and miscellaneous other required controls were met.

The

following documents were reviewed as part of this process:

Emergency Work Orders

5901017038

5901018019

5901016005

5902016543

5900038774

5900038733

Station Procedures

ADM 16.4 - Maintenance Program dated 8/28/86

ADM 16.5 - Work Request (WR) dated 9/19/86

ADM 16.7 - Corrective Work Orders dated 9/11/86

ADM 16.16 - Safety Related Equipment Failure Analysis Program dated

10/31/85 and draft dated 12/86

MD ADM 8.2 - Maintenance Department Administrative Procedure Equipment

History dated 12/10/85

ICP-NI-2-N31 - Source Range N31 dated 5/17/84

ICP-NI-2-N32 - Source Range N32 dated 5/17/84

IMP-C-SSPS-04 - Troubleshooting and Repair of Solid State Protection

System

IMP-C-MISC-05 - Troubleshooting, Repair and Replacement of Non-Safety

Related Equipment dated 4/5/84

IMP-C-NI-04 - Source Range Detector Replacement dated 3/6/81

2-PT-36.7.2 - Reactor Trip From Turbine Trip Response Time Test dated

11/1/84

EMP-C-EP-1 - Troubleshooting and Repair of Single Phase Static Inverters

dated 4/12/84

The inspector verified calibration equipment used during portions of work

requests listed above. This equipment is as follows:

Digital Voltmeter - NQC item 087

Multifunction Meter - NQC item 092

Counter - NQC item 169

Digital Voltmeter - NQC item 519

No violations or deviations were identified.

13. Temporary Instruction 2515/80, Data Collection for the Performance

Indicator Trial Program

During the month of July 1986, the inspectors collected the data requested

in TI 2525/80 and submitted it to the Region for processing.

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14. THI Item II.K.3.31 (71707)

Per letter dated November 21, 1986, from Leon B. Engle, Project Manager,

NRC, to W. L. Stewart, Vice President, VEPCO, the NRC has reviewed and

accepted the licensee's response to TMI item II.K.3.31.

Therefore, based

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on the safety evaluation attached to the letter, TMI item II.K.3.31 for

Unit 1 and Unit 2 is closed.

15.

IE Information Notice 86-53(92701)

The licensee issued an Engineering Work Request (EWR)87-073 dated

January 15, 1987, in response to IE Information Notice (IEIN) 86-53,

Improper Installation of Heat Shrinkable Tubing, dated June 26, 1986, and

the problems with Raychem splices discovered at the Surry Stattoo. This

EWR established the criteria and list of Raychem splices which wauld be

inspected at North Anna Unit 1. .This inspection commenced on February 2,

1987, and by February 15,1987, only 11 items containing Raychem splices

had been inspected.

Each of these items may have several splices

associated with it.

Of the 11 items inspected, all of the splices were

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determined to be faulty by Raychem criteria.

However, the equipment

associated with the splices inspected had very little, if any, safety

significance and therefore did not cause any operational issues. Based on

the type of equipment being inspected, the speed at which the inspection

was being conducted and the failure rate (100%), the inspector voiced a

concern to licensee management that the inspection program was not

receiving the attention that it should.

Licensee management agreed and

decided to change the scope of the inspection to include items of nore

safety significance and to increase the number of inspection teams from

one to three to expedite the inspection process. The original scope. was

defined based on ease of access and radiological concerns.

This revised inspection program did not recommence until February 17,

1987, at which time four more items were inspected and found to be

defective by Raychem criteria. On February 18, 1987, a conference call

between the licensee and the region was conducted to allow an exchange of

information on the Raychem issue.

The regional staff voiced a concern

that the licensee needed to look at some items of more safety signifcance

and to look at Unit 2 items as well.

The licensee committed to calling

the Region back on February 20, 1987, with an update on the inspection

process results of the Unit 1 and Unit 2 items inspected. Also, during

the call on February 18, 1987, the licensee informed the NRC that they had

just inspected four additional items which proved to be acceptable.

A review of the licensee's Deviation Reports (DRs) and their response to

IEIN 86-53 revealed that the licensee had identified problems with the

Raychem splices as early as December 1985. DR 85-1698 dated December 12,

1985, stated that of the 26 Raychem splices inspected inside Unit I

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containment all 26 were found deficient by Raychem criteria. IEIN 86-53

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was issued _in June of 1986 providing the licensee with additional

inforeation 'of industry problems with Raychem splices.

Finally, in

December of 1986 DR 86-1504 for Unit 1 and DR 86-1505 for Unit 2 were

issued documenting Raychem splice problem on all the narrow range delta

T/1ME protection / control temperature element electrical connections.

Since these splices were deficient, the licensee had to issue a

justification for. continued operation to allow the units to continue to

operate.

On February 20, 1987, a conference call between the licensee and the

region was conducted to provide an update on the inspection progress. The

licensee had examined 93 Raychem splices of which 5 did not meet the most

current acceptance criteria available.

It should be noted that this

acceptance criteria is less stringent than the Raychem criteria referenced

earlier. The licensee has inspection teams working outside containment on

both units ten hours a day, five days per week and estimates completion of

all items outsido containment in late March, 1987.

Items inside

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containment will be inspected during the scheduled refueling outages.

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In light of the above information, the inspector is concerned that the

' licensee had very good indications that a Raychem problem existed at North

Anna in l'!86 but waited until February 1987 to establish and perform a

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complete w pection program.

Pending the results of the present

inspection program, this will be identified as an Unresolved Item

338,339/87-01-05.

16.

Review of Periodic and Special Reports (90713)

Region based inspectors reviewed the Semi-Annual Effluent Report for

January - June 1986,,against the criteria given in Regulatory Guide 1.21,

Measuring, Evaluating, and Reporting Radioactivity in Solid Wastes and

Releases of Radioactive Materials in Liquid and Gaseous Effluents from

Light-Water-Cooled Nuclear Power Plants, and applicable regulatory

requirements.

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No violations or deviations were identified.

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