ML20207J529

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Insp Rept 50-382/86-13 on 860601-30.Violations & Deviation Noted:Failure to Preplan & Perform Station Mods,Take Prompt Corrective Action & Implement Response to IE Bulletin 85-001
ML20207J529
Person / Time
Site: Waterford 
Issue date: 07/23/1986
From: Bundy H, Constable G, Luehman J, Staker T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20207J480 List:
References
50-382-86-13, IEB-85-001, IEB-85-1, NUDOCS 8607290154
Download: ML20207J529 (13)


See also: IR 05000382/1986013

Text

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APPENDIX C

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

NRC Inspection Report:

50-382/86-13

License:

NPF-38

Docket:

50-382

Licensee:

Louisiana Power & Light Company (LP&L)

317 Baronne Street

P. O. Box 60340

New Orleans, Louisiana 70160

Facility Name: Waterford Steam Electric Station, Unit 3 (W3 SES)

Inspection At:

Taft, Louisiana

Inspection Conducted: June 1-30, 1986

Inspectors:

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J. G. Luehman, Senior Resident Inspector

Date

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7/M/TC

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. R. Staker, Resi' dent Inspector

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H. F. Bundy, Projecf Inspector, Project

Date

Section C, Reactor Projects Branch

(Pa,ragraphs 5, 6, 7, 8, and 9)

Approved:

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$.L. Constable, Chief, Project Section C,

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\\Reacdor Projects Branch

Inspection Summary

Inspection Conducted June 1-30, 1986 (Report 50-332/86-13)

Areas Inspected:

Routine, unannounced inspection of:

(1) Plant Status,

(2) Licensee Event Report (LER) Followup, (3) Monthly Surveillance, (4) Routine

Inspection, (5) Licensee Followup on Previously Identified items, (6) Monthly

Maintenance, (7) Potential Generic Problems, (8) License Conditions, and (9) IE

Bulletins.

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Results: Withintheareasinspected,twoviolations(failuretopreplanand

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perform station modifications in accordance with written procedures,

paragraph 6, and failure to take prompt corrective action, paragraph 8) and one

deviation (failure to fully implement commitments made in response to IE

Bulletin 85-01, paragraph 11)'were identified.

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DETAILS

1.

Persons Contacted

Principal Licensee Employees

G. W. Muench, Director, Nuclear Operations

  • R. P. Barkhurst, Plant Manager, Nuclear

T. F. Gerrets, Corporate QA Manager

S. A. Alleman, Assistant Plant Manager, Plant Technical Services

  • N: S. Carns, Assistant Plant Manager, Nuclear, Operations and Maintenance

J. N. Woods, QC Manager

A. S. Lockhart, Site Quality Manager

R. F. Burski, Engineering and Nuclear Safety Manager

K. L. Brewster. Onsite Licensing Engineer

G. E. Wuller, Onsite Licensing Coordinator

T. H. Smith, Maintenance Superintendent, Nuclear

  • P. V. Prasankumar, Technical Support Superintendent
  • Present at exit interviews.

In addition to the above personnel, the NRC inspectors held discussions

with various operations, engineering, technical support, maintenance, and

administrative members of the licensee's staff.

2.

Unresolved /Open Items

An unresolved item is a matter about which more information is required to

determine whether it is acceptable or may involve a violation or deviation.

No new unresolved items were identified during this inspection but two

previous items are discussed in paragraph 7.

3.

Plant Status

The inspection period began with the plant at full power. At 6:29 p.m.

(CDT) on June 5, 1986, with the plant at 100% power, a loss of the turbine

closed cooling water (TCCW) system occurred.

Immediately upon losing the

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system, the reactor operator began a turbine load reduction while attempts

were made to restore level in the system and restart the TCCW pumps.

Subsequently, the 0 TCCW Heat Exchanger was taken out of service due to

suspected tube leakage and the TCCW system was restarted using only the A

TCCW Heat Exchanger. At 9:09 p.m. the plant was stabilized at 60% power.

The licensee plugged seven tubes in the B TCCW Heat Exchanger. After the

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B Heat Exchanger was returned to service, the A Heat Exchanger was opened

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and inspected. With both heat exchangers back in service the plant began

the return to full power on the afternoon of June 6,1986.

At 10:28 p.m. on June 27, 1986, a plant power reduction from 100% power

was commenced due to concerns with the trends of various parameters on

the reactor coolant pumps.

Power was stabilized at about 70% and, on the

morning of June 28, 1986, licensee management decided that a slow return

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to full power could be accommodated.

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At 11:41 a.m. (CDT) on June 30, 1986, with the plant again at 100% power,

a reactor trip occurred and the plant responded normally.

LO-DNBR reactor

trip signals were received on the Core Protection Calculator (CPC)

Channels. The cause of the signals was apparently faulty reed switch

position indication from Control Element Assembly (CEA) 35 on Control

Element Assembly Calculator (CEAC) 1.

No violations or deviations were identified.

4.

Licensee Event Report (LER) Followup

The following LERs were reviewed and closed.

The NRC inspectors verified

that reporting requirements had been met, that causes had been identified,

that corrective actions appeared appropriate, that generic applicability

had been considered, and that the LER forms were complete. Additionally,

the NRC inspectors confirmed that no unreviewed safety questions were

involved and that violations of regulations or Technical Specification (TS)

conditions had been identified.

(Closed) LER 50-382/85-10, Automatic Actuation of the Reactor Protection

System. The licensee has completed all corrective actions including

Station Modification 814, revision of OP-3-031 and upgrading of OP-10-001

and OP-100-010.

(Closed) LER 50-382/86-02, Reactor Trip Due to Dropped CEA Number 88 and

Failure of Blowdown Isolation Valves to Close. The licensee has hung a

chain and sign across the entrance to the control element drive mechanism

control system (CEDMCS) area in order to reduce the possibilities of

future inadvertent operation of switches on controls by restricting area

access.

As short term corrective action for the problem with the blowdown isolation

valves, the licensee issued an instruction to operations personnel about

the event. The NRC inspector verified the long term corrective action was

taken by verifying OP-3-010, " Steam Generator Blowdown" had been changed to

ensure that proper removal of the gags is accomplished.

This change was

made to Sections 6.3, " Routine Processing of Steam Generator Blowdown";

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6.16, " Operation of Blowdown System with Steam Generator Tube Leakage or

Tube Rupture"; and 6.7, " Operation of Blowdown System with Main Condenser

Unavailable" of OP-3-010. Additionally, caution labels have been placed on

the valves to alert the operator to the valve gagging device.

(Closed) LER 50-382/86-06, Insufficient Tracking of Surveillance Resulted

in Mode Change Without Performing Surveillance on the Boric Acid Makeup

Tank. The chemistry technician who attempted to perform the sample on

March 17, 1986, made an error when he placed the surveillance notice back

in the file so that it would be performed on the normally scheduled day of

the following week. This led the person reviewing surveillances for the

mode change to assume all requirements had been met.

In order to ensure

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that future incomplete surveillances are carried over on a day-to-day

basis the chemistry supervisor has issued instructions to that effect in a

memorandum dated April 29, 1986. Additionally, in order to minimize the

probability of missing one of the many conditional surveillance require-

ments prior to a future mode change, Chemistry Department Standing

Instruction 17. "Startup Mode Change Check Sheet," has been issued.

(Closed) LER 382/86-09, Reed Switch Failure Results in Reactor Trip on Low

Departure from Nucleate Boiling Ratio.

The NRC inspector reviewed this

report and found that it adequately covers the event time frame chosen by

the licensee.

However, the report omits any description of the sequence

of CPC pretrips, and subsequent operator actions to determine their cause,

that occurred in the 20 minutes prior to receiving the reactor trip signals

on two channels at 2028. Additionally, the report fails to accurately

describe the generation of the CPC penalty factors.

If, as the report implied, position deviation was the only input to the

penalty factor generation, then the plant should have tripped the first

time the faulty reed switch ' closed.

But, penalty factors generated for a

given CEA are actually dependent on which CEA is deviating, how large the

deviation is, and how long the deviation exists.

In this report, the CEA

in question was a part-length CEA with one faulty reed switch position

indicator.

Each time the reed switch spuriously closed, a penalty factor

was generated and the longer the switch closed the larger the penalty

factor became.

Reactor trip signals finally occurred when the faulty reed

switch remained closed long enough for the penalty factors to increase

encJgh to generate not only the pretrips seen earlier in the event, but

the reactor trip signals first seen at 2028.

The NRC inspector's

observations were discussed with licensee management.

No violations or deviations were identified.

5.

Monthly Surveillance

The NRC inspectors observed / reviewed TS required testing and verified

that testing was performed in accordance with adequate procedures, that

test instrumentation was calibrated, that limiting conditions for operation

(LCO) were met, and that any deficiencies identified were properly reviewed

and resolved.

On June 23, 1986, the NRC inspector witnessed the performance of portions

of Procedure NE-2-002, Revision 2, " Variable Tavg Test."

This test was

conducted to meet the requirements of TS Surveillance 4.1.1.3.2.c.

A note

at the beginning of the procedure actio., steps advised the test engineer

that the load rate-of-change should be 2J0 MW/ min. for best results

(consistent with saf2 operating practice). At the start of the test there

was some discussion between plant operations personnel and the test

engineer as to the rate that would be used.

The operations personnel

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informed the test engineer that load changes would be performed at rates

substantially lower than he requested.

(The NRC inspector noted rates-of-

change from 0.3-6.0 MW/ min. used during the test.)

Discussions between the NRC inspector and operations personnel, including

the operations superintendent, revealed that the licensee would rarely, if

ever, conduct this test at the high rate-of-change recommended. Based on

that information, the NRC inspector recommended that the procedure be

changed to include a lower target load rate-of-change if such a lower rate

would not significantly impact the test results.

Such a change would

probably reduce future discussion and delays.

Additionally, during this inspection period, the NRC inspectors observed

portions of:

OP-903-005, " Control Element Assembly Operability Check"

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OP-903-007, " Turbine Inlet Valve Cycling Test"

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Performar.ce of the CHANNEL FUNCTIONAL TEST for containment radiation

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monitor ARM-IR-5400 AS per TS 4.3.3.1.

Demonstration of OPERABLE condition of each fire pump diesel starting

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12-volt battery bank and charger per TS 4.7.10.1.3.1.

No violations or deviations were identified.

6.

Routine Inspection

The NRC inspectors verified by observation that the control room manning

requirements were being met.

In addition, the NRC inspectors observed

shift turnover to verify that continuity of system status was maintained.

The NRC inspectors periodically questioned shift personnel relative to

their awareness of the plant conditions.

Through log review and plant tours, the NRC inspectors verified compliance

with selected TS and limiting conditions for operations.

During the course of the inspection, observations relative to protected

and vital area security were made including access controls, boundary

integrity, search, escort, and badging.

On a regular basis, radiation work permits (RWPs) were reviewed and the

specific work activity was monitored to assure the activities were being

conducted per the RWPs. Selected radiation protection instruments were

periodically checked and equipment operability and calibration frequency

were verified.

The NRC inspectors kept informed on a daily basis of overall status of

plant and of any significant safety matter related to plant operations.

Discussions were held with plant management and various members of the

operations staff on a regular basis. Selected portions of operating logs

and data sheets were reviewed daily.

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The NRC inspectors conducted various plant tours and made frequent visits

te the control room. Observations included: witnessing work activities

in progress; verifying the status of operating and standby safety systems

and equipment; confirming valve positions, instrument and recorder

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readings, annunciator alarms; and housekeeping.

The licensee's Potential Reportable Event (PRE-86-037) documents the

identification of a number of cracks in the nuclear plant island structure

(NPIS) foundation basemat found during performance of Procedure PE-5-033

(18-month requirement). Though these cracks had not been previously

identified, it appeared, upon observation by the NRC inspectors, that these

cracks have existed for a considerable length of time. The cracks that

were identified are located in the Diesel Storage Tank B and sanitary

equipment rooms, as well as both the east and west vault areas.

The licensee staff explained to the NRC inspectors that there are a number

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of probable reasons why these cracks were not identified either when

setting up the basemat surveillance program or during the first 18-month

inspection.

The initial 18-month inspection was considered complete based on the

nondestructive testing done on the basemat by Muenow and Associates, Inc.

during the period June to September 1984. This testing was an evaluation

of selected existing cracks with emphasis on those that appeared to be

continuous cracks running under the reactor containment, fuel handling, and

reactor auxiliary buildings.

The monitoring program set up to meet the requirements of TS 6.8.4.e does

require the monitoring of all significant cracks in the basemat and

adjacent walls.

However, prior to plant licensing, technical evaluation

of the NPIS basemat cracks concentrated on those cracks that appeared to

be continuous cracks running through the basemat below the reactor contain-

ment structure and even those were found acceptable.

These newly identi-

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fied cracks do not appear to fall into that category as they are considered

of less significance and therefore also acceptable.

The licensee plans to submit a special report to the NRC as outlined in

Procedure PE-5-033.

During a review of Procedure OP-9-001, " Containment Spray," following the

maintenance on the B Containment Spray Pump discussed in paragraph 8 of

this report, the NRC inspector noted one minor but apparently chronic

problem.

In Section 7 of the procedure, the title of one of the annunci-

ator windows (7.1.6) was changed as part of the licensee's continuing

annunciator upgrade program but this change has not been reflected in the

procedure. The NRC inspector discussed with the licensee the need to make

comprehensive changes to plant equipment and procedures for future

annunciator changes.

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On June 26, 1986, during a control room tour the NRC inspector questioned

the shift technical advisor (STA) about certain aspects of the operation

of the component cooling water (CCW) system. At one point, the STA

consulted the control room drawings to explain the function of the check

valve in the CCW surge tank vent line.

The control room drawing did not

indicate such a valve; however, the STA informed the NRC inspector that

this valve had been put in under a station modification (SM). That valve

and a second check valve designated to operate as a vacuum breaker had been

put in under SM 896. The SM documentation in the control room contained a

work completion notice (WCN) dated February 26, 1986, indicating the

completion of the modification. PE-2-006, Revision 7, " Station Modifica-

tions," requires, in section 5.9.5, that the action engineer redline any

control room drawings affected by the modification.

This was not done in

the case of this SM; the drawing had only been annotated to indicate that

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SM 896 did affect that drawing.

Concerns in this area were first brought to the licensee's attention in

NRC Inspection Report 382/85-20 and were reemphasized in the Systematic

Assessment of Licensee Performance (SALP) Board Report 382/85-30.

Further, paragraph 7 of NRC Inspection Report 382/86-08 discusses a

similar failure to update drawings and procedures which led to a number of

inadvertent radiological releases. The NRC inspector stressed to licensee

management that problems with the station modification program still exist

and that more aggressive action needs to be taken to both prevent future

problems and correct any past errors.

The failure to properly implement PE-2-006, Revision 7, is an apparent

violation and is identified as 382/8613-01.

7.

Licensee Followup on Previously Identified Items

(0 pen) Unresolved Item 382/8602-01 - This item involved apparent failure

to adequately document the investigation performed subsequent to the

inadvertent dropping of a control element assembly while the reactor was

at approximately 40% power.

The NRC inspector reviewed a number of docu-

ments which appear to be responsive to the problem including the following:

a.

Memo W3A86-0017 from the plant manager to various members of plant

management on the subject of determining accountability when

. investigating and reporting events.

b.

Various event reports documented by memos to file including one for

the dropped rod incident discussed abnve.

The NRC inspector discussed this documentation with the assistant plant -

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manager, operations and maintenance (APM, O&M) and stated the following

continuing concerns:

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It appeared that an independent review of the report would be

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appropriate in some instances. The APM, 0&M indicated that he would

forward a recent report involving a dropped subgroup of rods to the

independent safety engineering group-(ISEG) for evaluation.

It is not clear what the threshold is for initiating an event report

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in all instances. Also, the method of documentation (e.g., potential

reportable event, condition identification work authorization, -

quality notice, memo to file, etc.) required is not always clear.

The APM, 0&ll stated he would further address the above concerns.

(Closed)UnresolvedItem 382/8611-01 - In NRC Inspection Report 382/86-11

the procedural requirement to have a 15 F temperature difference across

the heaters in the shield building ventilation trains and the inability of

the system to meet this requirement was identified as Unresolved Item

50-382/8611-01. While reviewing the data being taken for Surveillance

Procedure OP-903-51, Revision 4, (TS 4.7.6.b) " Control Room Emergency

Filtration Unit Operability Check," for Train A, the NRC inspector

identified the same problem in this procedure as discussed in the

unresolved item.

In this case, a temperature difference of only 6.6*F

was recorded. Further review identified that the same 15 F temperature

difference is also specified in OP-903-52, Revision 4, " Controlled

Ventilation Area Section System Operability Check" (TS 4.7.7.a), and

OP-903-076, Revision 2, " Fuel Handling Building Ventilation System

Operability Check" (TS 4.9.12.a).

The performance of OP-903-076 for

Train A yielded a temperature difference value of 13.4 F.

The licensee has evaluated the 15 F temperature difference requirement and

determined that it is unnecessary.

The ventilation fans in the systems

discussed have a low temperature difference cut off of 5 F.

This temper-

ature difference is adequate to ensure the system filters and adsorbers are

properly maintained by running the 10-hour surveillance. The licensee is

in the process of deleting the 15 F temperature difference from the various

ventilation system procedures and Unresolved Item 50-382/8611-01 is

considered closed.

No violations or deviations were identified.

8.

Monthly Maintenance

-Station activities affecting safety-related systems and components were

observed / reviewed to ascertain that the activities were conducted in

accordance with approved procedures, regulatory guides and industry codes

or standards, and in conformance with TS.

Activities observed during this inspection period included the

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troubleshooting and repair of the valve operator for MS-401A (main steam

to emergency feedwater pump A/B turbine). This work was performed under

Condition Identification Work Authorization (CIWA) 027312 using Procedure

ME-7-00.8, " Motor Operated Valves."

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On June 18, 1986, the NRC inspector was reviewing the approved work in

progress on safety-related equipment. Work was being done on the B Safety

Injection Header to inspect and rewire, if necessary, certain valves that

possibly did not meet the requirements of the licensee's equipment quali-

fication program which implements the requirements of 10 CFR Part 50.49.

The NRC inspector noted that the plant operators had properly logged entry

into the applicable TS action requirement while the work was in progress.

The NRC inspector questioned the shift supervisor to ascertain why there

was environmental qualification (EQ) work still needing to be completed.

The shift supervisor told the NRC inspector that he only knew that the

electrical maintenance group had requested to do the work and that he was

not sure as to how or when the possible problems had been discovered. The

NRC inspector reviewed the applicable documentation and found that the

identification of the possible problems with wiring of the valve operators

for SI-121B [ low head safety injection (LPSI) Pump B upstream recirculation

isolation valve] and SI-228A [high pressure safety injection (HPSI)

Header A to Loop 2B cold leg injection valve] were identified April 9, 1986,

on CIWA 026203.

Similar possible problems with SI-225B (HPSI Header B to

Loop 1A cold leg injection valve) and SI-227B (HPSI Header B to 2A cold leg

injection valve) were identified on CIWA 026204 issued on the same date.

The inspections of the four listed valves on June 18 and 19, 1986,

revealed that only SI-2258 and SI-227B needed to be rewired in order to

comply with EQ requirements. This work was done at the time of the

inspection. The NRC inspector questioned licensee management as to the

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reason prompt corrective action had not been taken on these potential

problems identified over 2 months earlier.

Licensee management explained

that even though compliance with 10 CFR 50.49 had been required by

November 30, 1985, industry experience since that date had shown problem

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areas that had not been anticipated.

So, even though the Waterford 3

equipment qualification program was in place on the date required, it was

not unlikely that some future problems would be identified in a program of

such a large scope. The NRC inspector agreed that emergent problems were

not unlikely; however, in this case the possible deficiencies had already

been identified and timely actions to resolve them were not taken. The

failure to take prompt corrective actions to bring Valves SI-225B and 2278

into compliance with the EQ requirements is an apparent violation and is

identified as 382/8613-02.

The NRC inspector observed portions of bearing replacement work and

subsequent retesting for the B Containment Spray Pump.

The work was

performed in accordance with CIWA 024732 which appeared generally adequate

for the work to be performed. However, there appeared to be deficiencies

in work planning and/or training.

The pump to motor coupling was installed

backwards on the first attempt.

It had to be reheated for removal and the

first attempt failed. After the second failure, the lead mechanical

maintenance technician discovered specific instructions for preheating the

coupling in the technical manual (TM).

It would have been advisable for

the CIWA to specifically refer to these instructions.

Prior to reinstal-

lation of the pump, the NRC inspector and a licensee quality control (QC)

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inspector observed that the pump was attached to a chain hoist which was

attached to a pipe snubber. No pump weight had been transferred to the

snubber. Also, a metal platform was positioned across two electrical

conduits under where the pump was to be placed. The QC inspector advised

the mechanical maintenance technicians that it was improper to rig from the

pipe snubber and that the platform should be removed from the conduits.

The pump was subsequently placed by utilizing a ceiling chain hoist after

the platform was removed.

The NRC inspector discussed the above occurrences with the APM-0M and the

plant maintenance superintendent (PMS).

The NRC inspector emphasized that

continual effort is needed to ensure CIWA work instructions are clear and

detailed. Also, the NRC inspector suggested an evaluation of the

effectiveness of training for rigging and equipment protection may be

appropriate.

Containment Spray Pump B was successfully tested utilizing plant Procedure

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OP-903-035, Revision B, " Containment Spray Pump Operability Check," which

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satisfies TS 4.6.2.1.c and TS 4.0.5.

However, on the first start it showed

evidence of being potentially air bound. Operations shut it down and then

bumped it twice more before a sustained test run after the fourth start.

The NRC inspector expressed concern to the operations superintendent (OS)

regarding what appeared to be an excessive number of motor (300 hp) starts

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in a short period of time.

The OS stated that he also had this concern

prior to the starts and had researched the TM, but could find no restric-

tions on motor starts. The OS agreed to consider establishing plant

generic motor starting guidelines for motors that are not presently

addressed procedurally. During further discussions of this event between

the APM-0M, the PMS and the NRC inspector, the APM-0M stated that they

would consult the motor manufacturer to determine if excessive motor

temperature could have been experienced in this instance.

During testing of the containment spray pump two significant leaks (steady

streams) were observed at fittings connecting component cooling water to

the bearing oil cooler. When the NRC inspector asked the STA about the

leaks the following afternoon the STA discovered the leaks continued to

exist.

CIWA 027405 was initiated to request repair of the leaks. Though

the leaks did not appear to affect operability, in order to repair them

now, the pump must be taken out of service a second time. The NRC

inspector informed plant management that such maintenance practices are

not compatible with maximizing the availability of safety-related

equipment or with goals for keeping radiation exposure as low as

reasonably achievable ( ALARA).

Prior to performing work observation activities, the NRC inspector

reviewed the following procedures:

UNT-5-002, Revision 5, Change 1, Condition Identification and Work

Authorization

UNT-5-004, Revision 3, Change 2, Temporary Alteration Control

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Other maintenance activities observed included routine preventive

maintenance for the diesel fire pump and auxiliary diesel starting

batteries.

9.

Potential Generic Problems

The NRC inspector provided the licensee with a copy of a report regarding

detection of "intergranular attack" corrosion in the St. Lucie 1 steam

generators in the egg-crate tube support region. The corrosion was

detected during inspection of three representative tubes which had been

removed from the steam generator. This corrosion had not been identified

during eddy current tests which had been done on two previous occasions.

The NRC inspector also followed up on possible seismic interactions

between the movable incore flux mapping system and the seal table which

was first identified as a concern at Westinghouse designed facilities. The

concern does not appear to be applicable to Waterford 3 as the incore

instrument penetrations are attached to the reactor vessel head and do not

rely on a seal table and bottom penetrating design.

The NRC inspector made the licensee aware of a deficiency discovered in

the high energy line break (HELB) analysis for the Monticello facility.

In performing the analysis based on the " worst case" approach, the

architect / engineer (AE) failed to consider the effects of a HELB in certain

areas of the plant.

Further analysis demonstrated that a masonry wall

failure could occur which, in turn, results in a harsh environment in an

area where one was not previously presumed to exist. The NRC Region III

office believes similar deficiencies could exist in other HELB analyses and

has recommended that all other licensees for power reactor facilities

review their analyses.

No violations or deviations were identified.

10.

License Conditions

(Closed) Condition 2.C.14, Verification of Boraflex in Spent Fuel Storage

Racks.

In a letter dated June 6,1986, the licensee informed the Office

of Nuclear Reactor Regulation (NRR) that the storage rack Boraflex

verification had been completed during the period March 11-17, 1985. The

NRC inspector has reviewed the report documenting the testing made to the

licensee by National Nuclear Corporation and had no questions.

NRR, iri a

letter dated June 23, 1986, informed the licensee that this license

condition is considered closed.

No violations or deviation were identified.

11.

IE Bulletins

(0 pen) IEB 85-01, Steam Binding of Auxiliary Feedwater Pumps.

This

bulletin required, in part, that procedures be developed "for recognizing

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steam binding and for restoring the AFW system to operable status, should

steam binding occur." In a letter dated February 26, 1986, the licensee

described the procedures they had implemented to meet the above require-

ments.

In summary, the licensee's response stated that procedures had been

changed to require monitoring of emergency feedwater (EFW) discharge piping

temperatures and that upon these temperatures reaching 120 F, closer

monitoring would be required and possible corrective actions considered.

The response went on to say that, tpon reaching 230 F, control room

supervisors had been instructed that corrective actions were required to

vent, drain, and fill the system as reguired to reduce tamperature.

The reactor auxiliary building (RAB) radiologically controlled area logs,

which are an attachment to 01-004-000, " Watch Station and Shift Logs,"

require that temperatures on the discharge of the EFW piping be monitored

and specify 120 F as the maximum acceptable temperature. Additionally,

OP-903-001, the control room " Technical Specification Logs" record the EFW

,

discharge piping temperatures. A note accompanying that procedure requires

increased monitoring of the temperatures and outlines possible corrective

actions.

The NRC inspector could find no procedural requirement that would

implement the 230 F limit for initiation of corrective actions described in

the licensee's response to the IE Bulletin.

Further, the NRC inspector

asked a number of senior reactor operators (SR0s) about the existence of a

temperature limit above the 120 F discussed in the two station logs.

Though the SR0s were aware that the probability of steam binding of the

pumps would increase as the discharge piping temperature increased, they

were not familiar with the 230 F limit specified in the licensee's

February 26, 1986, letter.

The failure to fully implement the actions

committed to in response to IE Bulletin 85-01 is an apparent deviation

from a commitment to the NRC and is identified as 382/8613-01.

12.

Exit Interview

The inspection scope and findings were summarized on July 1, 1986, with

those persons indicated in paragraph 1 above. The licensee acknowledged

the NRC inspectors findings. The licensee did not identify as proprietary

any of the material provided to or reviewed by the NRC inspectors during

this inspection.

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