Letter Sequence Approval |
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MONTHYEARML20151A3321988-03-30030 March 1988 Proposed Tech Specs Revising Tech Spec 3/4.4.2,Figures 3.4-2a & 2b,Tech Spec 3/4.4.9.1,Figures 3.4-2,3.4-4,3.4-4, Table 4.4-5 & Tech Spec Bases Section 3/4.4.9,Bases Table 4-1 & Bases 4-1 & 4-2 Project stage: Other ML20151A3121988-03-30030 March 1988 Application for Amend to License NPF-3,revising License Condition 2.C.(3)(d),including Tech Spec 3/4.4.2,Figures 3.4-2a & 2b,Tech Spec 3/4.4.9.1,Figures 3.4-2,3.4-3 & 3.4-4 & Table 4.4-5 & Tech Spec Bases Section 3/4.4.9 Project stage: Request ML20151A2981988-03-30030 March 1988 Forwards Application to Amend License NPF-3,revising License Condition 2.C.(3)(d),including Tech Spec 3/4.4.2, Figures 3.4-2a-2b,Tech Spec 3/4.4.9.1,Figures 3.4-2,3.4-3 & 3.4-4,Table 4.4-5 & Tech Spec Bases Section 3/4.4.9 Project stage: Request ML20154P3381988-05-25025 May 1988 Responds to Generic Ltr 88-03 Re Resolution of Safety Issue 93, Steam Binding of Auxiliary Feedwater Pumps Project stage: Other ML20207H3811988-08-19019 August 1988 Amend 116 to License NPF-3,revising & Deleting Listed Tech Spec Sections,License Conditions,Figures & Table Project stage: Other ML20207H3941988-08-19019 August 1988 Notice of Issuance of Amend 116 to License NPF-3 Project stage: Approval ML20207H3891988-08-19019 August 1988 Safety Evaluation Supporting Amend 116 to License NPF-3 Project stage: Approval 1988-05-25
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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 ML20249A7661998-06-11011 June 1998 Safety Evaluation Supporting Amend 222 to License NPF-3 ML20249A7551998-06-11011 June 1998 Safety Evaluation Supporting Amend 223 to License NPF-3 ML20216B9401998-04-15015 April 1998 Safety Evaluation Supporting Amend 221 to License NPF-3 ML20216B8381998-04-14014 April 1998 Safety Evaluation Supporting Amend 220 to License NPF-3 ML20202C6131998-02-0303 February 1998 Safety Evaluation Supporting Amend 219 to License NPF-3 ML20199J9511998-01-30030 January 1998 SER Related to Exemption from Section Iii.O of App R,To 10CFR50,for Davis-Besse Nuclear Power Station,Unit 1 ML20198R4771998-01-13013 January 1998 SER Approving Second 10-year Interval Inservice Inspection Program Plan Requests for Relief for Davis-Besse Nuclear Power Station,Unit 1 ML20203C1401997-12-0202 December 1997 Safety Evaluation Supporting Amend 217 to License NPF-3 ML20203B2141997-12-0202 December 1997 Safety Evaluation Supporting Amend 218 to License NPF-3 ML20203C2701997-12-0202 December 1997 Safety Evaluation Supporting Amend 216 to License NPF-3 ML20138L0491997-02-11011 February 1997 Safety Evaluation Supporting Amend 214 to License NPF-3 ML20128L3001996-10-0202 October 1996 SER Supporting Dbnp IPE Process of Identifying Most Likely Severe Accidents & Severe Accident Vulnerabilities ML20058M9591993-09-28028 September 1993 SE Accepting Licensee Response to GL 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants.' ML20057A3791993-08-20020 August 1993 SE Concluding That Second 10-yr Interval Inservice Insp Program Plan for Plant Has Unacceptable Exam Sample as Discussed in Encl Inel TER ML20056G4301993-08-18018 August 1993 Safety Evaluation Re Inservice Testing Program Requests for Relief.Licensee Made Changes to Subj Program to Include Exercising & fail-safe Testing of Auxiliary Feedwater Valves AF-6451 & AF-6452,in Response to TER Anomaly 8 ML20126A3051992-12-0808 December 1992 Safety Evaluation Supporting Amend 176 to License NPF-3 ML20056B2721990-08-20020 August 1990 Safety Evaluation Granting Relief from ASME Code Repair Requirements for ASME Code 3 Piping ML20248H6371989-10-0303 October 1989 Safety Evaluation Supporting Amend 139 to License NPF-3 ML20248D8271989-09-29029 September 1989 Safety Evaluation Accepting Util 890228 & 0630 Submittals Presenting Proposed Designs to Comply w/10CFR50.62 ATWS Rule Requirements ML20248E2771989-09-20020 September 1989 Safety Evaluation Supporting Amend 138 to License NPF-3 ML20248B3801989-09-20020 September 1989 Safety Evaluation Supporting Amend 137 to License NPF-3 ML20247E6901989-09-0505 September 1989 Safety Evaluation of Audit of Facility Design for Resolution of IE Bulletin 79-27 Re Loss of non-Class IE Instrumentation & Control Power Sys Bus During Operation.Preventive Maint & Testing Program Should Be Developed for Bus Power Sources ML20245K1871989-08-15015 August 1989 Safety Evaluation Supporting Amend 136 to License NPF-3 ML20245F5791989-08-0404 August 1989 Safety Evaluation Supporting Amend 134 to License NPF-3 ML20245H9531989-08-0404 August 1989 Safety Evaluation Supporting Amend 135 to License NPF-3 ML20247J8731989-05-18018 May 1989 Safety Evaluation Supporting Amend 133 to License NPF-3 ML20245G0371989-04-25025 April 1989 Safety Evaluation Supporting Amend 131 to License NPF-3 ML20245F0631989-04-25025 April 1989 Safety Evaluation Supporting Amend 132 to License NPF-3 ML20244D4031989-04-13013 April 1989 Safety Evaluation Supporting Amend 130 to License NPF-3 ML20196D9601988-12-0808 December 1988 Safety Evaluation Re Util Response Concerning Auxiliary Feedwater Sys Reliability Study.Util Should Ensure That Sys Mods Do Not Result in Net Reduction in Sys Reliability ML20207K7911988-10-0404 October 1988 Safety Evaluation Supporting Operation in Cycle 6 W/O Removing Flaws in Cracked HPI Nozzle ML20207K1071988-09-19019 September 1988 Safety Evaluation Supporting Amend 120 to License NPF-3 ML20207H9271988-08-24024 August 1988 Safety Evaluation Supporting Amend 117 to License NPF-3 ML20207H3891988-08-19019 August 1988 Safety Evaluation Supporting Amend 116 to License NPF-3 ML20207E3931988-08-0202 August 1988 Safety Evaluation Supporting Amend 114 to License NPF-3 ML20207D5171988-08-0202 August 1988 Safety Evaluation Supporting Amend 115 to License NPF-3 ML20150C4621988-03-0909 March 1988 Safety Evaluation Supporting Amend 109 to License NPF-3 1999-08-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
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o UNITED STATES g
NUCLEAR REGULATORY COMMISSION n
g 5
WASHING TON, D, C. 20555 g.....)
S SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO.
116 TO FACILITY OPERAT!NG LICENSE NO. NPF-3 TOLEDO EDISON COMPANY, AND THE CLEVELAND ELECTRIC ILLUMINATING COMPANY DAVIS-BESSE NUCLEAR POWER STATION, UNIT NO. 1 DOCKET NO. 50-346
1.0 INTRODUCTION
By letter dated March 30, 1988 Toledo Edison Company requested approval to revise section 3/4.4.9 and bases section 3/4.4.9 of the Davis-Besse Technical Specifications; both relate to the pressure-temperature limits of the Reactor Coolant System and surveillance capsule withdrawal schedule.
The primary purpose of this request is to revise the existing pressure temperature limits and extend the operation period of the limits up to 10 effective full power years (EFPY). The revised pressure-temperature limits are based on the Babcock and Wilcox analyses (BAW-1882 and BAW-2011) of irradiation data taken from removed surveillance capsule TEl-A. The limits provide pennissible pressure and temperature for three operating conditions -
heatup and core criticality (Fig m 3.4-2), cooldown (Figure 3.4-3), and inservice leak and hydrostatic tests (Figure 3.4-4).
The licensee also requested approval to revise the existing surveillance capsule withdrawal schedule.
2.0 DISCUSSION Part of the NRC's effort to ensure integrity of the reactor vessel is to periodically evaluate the reduction in fracture toughness of the vessel material caused by neutron irradiation embrittlement. The effort consists of three steps.
First, the licensee is required to establish a survei' lance program in accord-ance with Appendix H of 10 CFR Part 50, which requiras periodic withdrawal of surveillance capsules from the reactor vessel. The capsules are instelled in the vessel prior to startup and they should contain test specimens that l
were made from the plate, weld, and heat-affected-zone materials of the reactor oeltline.
8808260362 880819 PDR ADOCK 05000346 P
pon
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. Secondly, the licensee is required to perform Charpy impact tests, tensile tests, and neutron fluence measurements on the specimens. These tests define the condition of vessel embrittlement at the time of capsule withdrawal in terms of the increase of the reference temperature, RT and upper shelf energy. ThelicenseemustalsopredictthefuturevesNI,embrittlementby calculating the adjusted RT and upper shelf energy at a specific EFPY. The licensee may use either RevNIon 1 or draft Revision 2 of Regulatory Guide 1.99 to calculate the adjusted RT The upper shelf energy is the average energy value for all specimens whosUDIe.st temperature is above the upper end of the transition temperature region. The licensee is required by 10 CFR Part 50 Appendix G, to provide assurance that the adjusted RT will not exceed 200'F and that the upper shelf energy will not be below 50 bib at the end of plant life.
Thirdly, the licensee is required to develop a set of pressure-temper.ture curves based on the adjusted RT of the limiting vessel materials. The curvesmustsatisfytherecommebdmethodsandrequirementsdescribedin 10 CFR Part 50, Appendix G, and Standard Review Plan 5.3.2.
3.0 EVALUATION Surveillance Program The surveillance program in Davis-Besse Unit 1 is part of the Integrated Reactor Vessel Material Surveillance Program sponsored by Bab Jck and Wilcox (Report No.
BAW-1543A), which the staff approved in 1985.
B&W 1ritiated the Integrated Pro-gram as a result of flow-induced vibration that cause cracking of surveillance capsule holder tubes in some B&W reactor vessels.
T! t capsules were ramoved from these nuclear plants, redesigned, and installed in other B&W reactors.
Davis-Besse, Unit I was selected as a host reictor.
The surveillance program in Davis-Besse consists of six surveillance capsules.
Capseles TEl-F, and TEl-B, and TEl-A have been removed at the end of fuel cycles 1, 3, and 4, respectively.
The proposed pressure-temperature limits were determined based on the data taken from Capsule TEl-A, which was positioned inside the reactor vessel between the thermal shield and the vessel wall.
This capsule contained Charpy V-notch test specimens fabricated from two base metals, a weld metal, two heat-affected-zone metals, and a correlation metal.
All test specimens were machined from the 1/4-thickness of the forging material and can be traced to the vessel material.
The licensee proposed to delete the existing capsule withdrawal schedule in section 3/4.4.9 of the Technical Specifications and replace it with the withdrawal schedule recomended for Davis-Besse in the Integrated Program in Bases section 3/4.4.9. The remaining three capsules in Davis-Besse will be removed at the end of the sixth, eighth and eleventh fuel cycles. The staff concludes that this withdrawal schedule for the remaining capsules satisfies the requirements of Appendix H to 10 CFR Part 50 and ASTM E 185-82.
T
. UPPER SHELF ENERGY The licensee used methods in Regulatory Guide 1.99, Revision 2, and BAW-1803 (a B&W Owner Group method) to evaluate the reactor vessel end-of-life upper shelf energy (USE). The weld material in the Davis-Besse reactor used a submerged arc weld process with Linde 80 flux. This weld material has high copper content and low unirradiated Charpy USE; therefore, it is susceptible to neutron irradiation damage. The method given in Regulatory Guide 1.99, Rev. 2 estimated a USE of 47 ft-lbs whereas the BAW-1803 method estimated a 67 ft-lbs USE at end-of-life for weld WF-182-1. The BAW-1803 method uses a statistical analysis of all the existing surveillance Linde 80 weld metal; therefore, it estimates a higher USE than Reg. Guide 1.99.
The staff considers that the statistical analysis in BAW-1803 is an acceptable alternative to the R.G. 1.99 Rev. 2 method and that 67 ft-lbs is acceptabN. The licensee showed that none of the vessel raterial will have a USE below 50 ft-lbs at end-of-life at the T/4 wall location. The staff concludes that the USE's of Davis nesse reactor materials satisfy Appendix G of 10 CFR Part 50.
REFERENCE TEMPERATURE The observed herease in reference temperature (RTspecimens was detemined based o in the surveillance at the time of withdrawal and the initial RT The RT isthetesttemhSfaturethat correspondstothe30ft-lbimpaggT.absorptioMnergyintheCharpyv-notch impact tests.
From the Charpy test, the licensee determined that the maximum observed increase in the RT was 175'F and occurred in the middle circumference seamweld,WF-182-1.BasedBRTthe maximum RT shift, this weld metal is selected to be ghe limiting material.
CapsugTTEl-A received a neutron fluence of 1.29E19 n/gem and the inner wall fluance at 10 EFPY was calculated to be 5.63E18 n/cm. The ratio of the neutro i flux density at the capsule location to the maximum calculated neutron flux censity at the inside surface of the vessel wall (lead factor) was about 2.0, Since the pressure-temperature limits are usually needed for the future EFPY's, the licensee needs to predict the adjusted RT dt a could be used in detemining the hNssure future EFPY so that a valid RT temperature limits. The staff ush0Tthe Revision 2 method to evaluate the licensee's predictions of the adjusted RT The predicted RT depends on the neutron fluence at the specific vein 1 wall location, sp$SIfic EFPY, and copper content and nickel content of the vessel mater!al. The neutron fluence at T/4 vessel wall location (T=vesselthickness)and106FPYwasextrapolatedfromtheogservedneutron fluence of capsule TEl-A and was calculated to be 3.46E18 n/cm. The maximum 1
predicted adjusted RT was determined to be 146*F for the limiting weld NDT material,
i
, The observed and predicted RT for base metal and heat-aifected-zone metal TheNedictedRT for the base metal exceeds the N
- are compared in Table 1.
observed RT while the predicted RT f5ETthe weld metal is less than the NDT observed RT Thelicenseeusedth5%redictedRT of 147'F to determine the pressurN[e.mperature limits instead of the obseNd value of 175'F. The requirements in subsection 2.1 of Rep. Guide 1.99, Rev. 2 allow the use of the lower of the two RT when the licensee uses previous knowr, surveillance data in the prediction. Nkbe staff finds that the use of 147'F for the RT in the proposed pressure-temperature limits is more reasonable than 175'F bEluse the RT of 175'F corresponds to a neutron fluence at 22 EFPY.
NDT The RT at end-of-life and T/4 location was calculated to be 222'F. Davis-Besse NI a part of the pressurized thermal shock study that has an allowable RT of 300'F, as aescribed in section 50.61 of 10 CFR Part 50. The staff, thE[ fore, finds the end-of-life RT acceptable.
NDT PRESSURE-TEMPERATURE LIMITS The staff used the methods described in Standard Review Plan 5.3.2 to evaluate three proposed pressure-temperature limits for heatup and core criticality, cooldown, and hydrostatic leak test. The SRP 5.3.2 method uses the principle of linear elastic fracture mechanics to calculate the pressure-temperature limits. The basic parameter is the stress intensity factor, which is a function of pressure and thermal stresses and flaws in the vessel material. The stress intensity factor is related to the reactor coolant system temperature and prNIure,the vessel material by an exponential curve. For a given operating RT of a reference stress intensity factor is calculated and via the exponential curve, the system operating temperature could be detennined. Aside from the pressure and thennal stresses, the pressure-temperature limits should also consider the bolt preload stress at reactor closure flange regions as described in Appendix G to 10 CFR Part 50. The staff finds that the proposed pressure-temperature limits in Figures 3.4-2, -3, and -4 are in accord with SRP 5.3.2 and meet the requirements of Appendix G to 10 CFR Part 50, 4.0 FINDINGS l
The staf' finds that the proposed surveillance capsule withdrawal schedule is acceptab'.e based on the requirements of Appendix il to 10 CFR Part 50 and ASTM l
E 185-82.
The staff has concluded that the proposed pressure-temperature limits on the reactor coolant system for heatup, core criticality, cooldown, and hydrostatic test operating conditions are in conformance with requirements of Appendix G to 10 CFR Part 50. The proposed limits are acceptable up to 10 effective full power years.
The staff agrees that the proposed surveillance withdrawal schedule and pressure-temperature limits may be incorporated into the Davis-Besse Technical Specifications, i
i 1
.Y
i
5.0 ENVIRONMENTAL CONSIDERATION
Pursuant to 10 CFR 51.21, 51.32, and 51.35, an environwntal assessment and finding of no significant impact have been prepared and published in the Federal Register (July 18,1988,53FR27095). Accordingly, based upon the environmental assessment, the Comission has determined that the issuance of this amendment will not have a significant effect on the quality of the human environment.
6.0 CONCLUSION
The staff has concluded, based on the considerations discussed above, that:
(1) there is reasonable assurance,that the health and safety of the public will not be endangered by operation in the )roposed manner, and (2) such activities will be conducted in compliance with tle Commission's regulations, and the issuance of this amendment will not be inimical to the comon defense and security or to the health and safety of the public.
Principal Contributor:
J. Tsao Dated: August 19, 1988 i
1 I
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I J
l TABLE 1 i
Adjusted RTun, 9 10 EFPY and T/4 watt' location Neutron Copper Nickel Fluence 9 Observed Staff Pre-Licensee Specimen (1)
Content Content InnerSur{ ace RT diction Prediction n/cm WET
'F
'F Base Metal BCC-241 0.02 0.81 5.63E18 28 78 78 Base Metal AKJ-233 0.04 0.77 5.63E18 2
56 56 Heat Affected 0.02 0.81 5.63E18 34 78 Not Zone BCC-241 Available Weld Metal WF-182-1 0.24 0.63 5.63E18 175 146(2) 147(2) i Notes (1) All surveillance specimens can be traced to the vessel material.
(2) Use capsule fluences and observed RT shifts from capsules TEl-A, 1
TEl-B and TEl-F to calculate the chhIstry factor per subsectioli 2.1 of Reg. Guide 1.99 Rev. 2.
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