ML20207G065
| ML20207G065 | |
| Person / Time | |
|---|---|
| Site: | Millstone |
| Issue date: | 09/30/1986 |
| From: | Elms A, Romberg W NORTHEAST NUCLEAR ENERGY CO., NORTHEAST UTILITIES |
| To: | NRC OFFICE OF RESOURCE MANAGEMENT (ORM) |
| References | |
| MP-9585, NUDOCS 8701060310 | |
| Download: ML20207G065 (4) | |
Text
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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-423 UNIT Millstone Unit No. 3 DATE October 3, 1986 COMPLETED'BY A. Elms TELEPHONE (203) 444-5388 MONTH September iDAY
' AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL
-(MWe-Net)
(MWe-Net) 1 1127 17 1094 i
2 1142 18 1146 3
1142 19 1107 4
1150' 30 1132 5
471 21 1131 6
235 22 1086 7
-58 23 1131 8
855 24 1118 9
1097 25 1141 10 1124 26 1105 11 1122
'27 1124 12 1120 28 1118 13 1118 29 1116 l
14 1125 30 1122 15 605 31 16 521 8701060310 860930 PDR ADOCK 05000423 R
PDR 34 f
.I,
E UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-423 e
UNIT Millstone Unit No. 3 DATE October 3, 1986 COMPLETED BY A. Elms TELEPHONE (203) 444-5388 -
REPORT MONTH SEPTEMBER 1986 Method of Licensee Cause & Corrective-Duration Shutting Event System-Component Action to No.
Date Type (1)
(Hours)
Reason (2)
Down Reactor (3)
Report #
Code Code Prevent Recurrence 86-08 9-5-8E F
N/A A
N/A N/A AB ISV Downpower due to excessive RCS identified leakage.
Leakage repaired.
Immediate notification sent to NRC.
86-09 9-6-86 F
25 G
3 86-051-00 JB N/A Low Steam Generator Water Level.
86-10 9-7-86 F
4.6 A
N/A N/A TG SCV Turbine Trip due to EHC lube oil leak on #2 Turbine Control Valve.
86-11 9-15-86 F
N/A A
N/A N/A SJ FCV Downpower due to
- 3 Feed Control Valve Malfunction.
1 2
3 4
-F:
Forced
-Reason:
-Method:
-Exhibit G - Instructions S:
Scheduled A - Equipment Failure (Explain) 1 - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram Entry Sheets for C - Refueling 3 - Automatic Scram Licensed Event Report D - Regulatory Restriction 4 - Continued from
'LER) File (NUREG-0161)
E - Operator Training & License previous month Examination 5 - Power Reduction 5 F - Administrative (Duration = 0)
Exhibit 1 - Same Source G - Operational Error (Explain) 9 - Other (Explain)
H - Other (Explain)
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HARTFORD. CONNECTICUT 06141-0270 k
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(203) 665-5000 October 7, 1986 MP-9585 Director, Office of Resource Management U. S. Nuclear Regulatory Commission Washington, D. C. 20555
Reference:
Facility Operating License No. NPF-49 Docket No. 50-423
Dear Sir:
In accordance with reporting requirements of Technical Specifications Section 6.9.1.5, the Millstone Nuclear Power Station - Unit 3 Monthly Operating Report 86-10 covering operations for the month of September is hereby forwarded.
Yours truly, NORTHEAST NUCLEAR ENERGY COMPANY h8*
Wayne D. Ro g
Station Superintendent Millstone Nuclear Power Station WDR/ ALE:sb Attachment cc:
Regional Administrator, Office (,f inspection and Enforcement, Region I Director, Office of Inspection and Enforcement, Washington, D.C. (10)
U. S. Nuclear Regulatory Commission, c/o Document Management Branch, Washington, D. C. 20555 h
4 Y
- C'.C OPERATING STATUS REPORT COMPLETED BY REACTOR ENGINEERIN3 He****
- l. 00CiET....50-423 OPERATING CTATUS 720
- 2. REPORilN6 PERIOD... SEPTEMBER 1986 0UTAGE + DNLINE HOURS.. 29.6 + 690.4 3
- 3. UilLITY CONTACT.................A. L. ELMS 203-444-5368
- He****
- 4. LICENSED THERMAL P0mER.........................................
3411
- MILLSichE *
- 5. NAMEPLATE RATING (6ROSS M E)...................................
1,253 M
- UNIT 3
- 6. DES 16N ELECTRICAL RATIN6 (NET ME).............................. !!53.61
- He*H HeH
- 7. MA!! MUM DEPENDABLE CAPACITY (6RDSS ME)........................
1197
- 9. MAIIMUM DEPENDABLE CAFAClif (NET ME)........................... 1149.35 9.
IF CHANSES DCCUR ABOVE SINCE LAST REPORT, REASONS ARE...........
N/A
- 10. POWER LEVEL TO NHlCH RESTRICTED, IF ANY (NET M E)...............N/A
!!. REASON FOR RESTR!CTION, IF ANY....N/A MONTH YEAR TO DATE CUMULATIVE TO DATE E3333 53E322333333 332223SEEEEEEEEEEE
- 12. HOURS IN REPORTING PERIOD 720.0 3863.0 3863.0
- 13. NUMBER OF HOURS THE REACTOR NAS CRITICAL 701.0 3203.8 3203.6
- 14. REACTOR RESERVE SHUTDOWN HOURS 0.0 83.2 63.2
- 15. HOURS GENERATOR ONLINE 690.4 3146.9 3146.9
- 16. UNIT RESERVE SHUTDDWN HOURS 0.0 0.0 0.0
- 17. GROSS THERMAL ENERGY SENERATED (M H) 2191008.5 10220375.2 10220375.2
- 18. 6ROSS ELECTRICAL ENER6Y SENERATED (M H) 746571.0 3523224.0 3523264.0
- 19. NET ELECTRICAL ENER6Y GENERATED th H) 712378.1 3357579.0 3357579.0
- 20. UNIT SERVICE FACTOR 95.9 B1.5 81.5
- 21. UN!i AVAILABILITY FACTOR 95.9 81.5 01.5
- 22. UNIT CAPACITY FACTOR (USING MDC NET) 86.1 75.6 75.6
- 23. UNif CAPACITY FACTOR (USING DER NET) 85.8 75.3 75.3
- 24. UNIT FORCED OUTAGE RATE 4.1 18.5 18.5
- 25. UNIT FORCED OUTA6E HOURS 29.6 716.1 716.1 SHUTDOWNS SCHEDULED DVER NEli SIX MONTHS (TYPE, CATE, AND DURATION OF EACH)..............
N/A IF CURRENTLY SHUIDOWN, EST! MATED STARTUP DATE......N/A
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