ML20206L793

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Insp Rept 50-298/88-31 on 881001-31.Violations Noted.Major Areas Inspected:Followup of Plant Events,Operational Safety Verification,Access Control,Monthly Surveillance & Maint Observations & Emergency Excercise
ML20206L793
Person / Time
Site: Cooper 
Issue date: 11/15/1988
From: Bennett W, Constable G, Greg Pick
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20206L780 List:
References
50-298-88-31, NUDOCS 8811300248
Download: ML20206L793 (7)


See also: IR 05000298/1988031

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APPENDIX B

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION IV

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NRC Inspection Report:

50-298/88-31

Operating License: OPR-46

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Docket:

50-298

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Licensee:

Nebraska Public Power District (NPPD)

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P.O. Box 499

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Columbus, NE

68602-0499

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Facility Name:

Cooper Nuclear Station (CNS)

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Inspection At:

CNS, Nemaha County, Nebraska

Inspection Conducted: October 1-31, 1988

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Inspectors:

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G.A. Pick,(VDv

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nt Inspector, Project

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W. R. Bennett, Senior Resident Inspector,

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Project Section C, Division of Reactor Projects

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Approved:

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'G.7. Constable, Chief, Project Section C,

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Div ion of Reactor Projects

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Inspection Summary

Inspection conducted October 1-31, 1988 (Report 50-298/88-31)

Areas Inspected:

Routine, unannounced inspection of followup of plant events,

operational safety verification, access control, monthly surveillance and

maintenance observations, and emergency excercise.

Results: The licensee continued to operate the plant in a safe, controlled

manner.

Surveillance and maintenance activities were performed in accordance

with prescribed programs.

One violation was identified in this report.

It involved allowing an

individual unescorted site access after his required training had expired.

The root cause appears to be a problem with training records which is similar

to the root cause of a previous violation.

This may indicate a problem with

the licensee's corrective action program. Another example of this potential

problem is the connonications deficiency in the practice energencies exercise

which had been previously identified in the 1987 annual emergency exercise.

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DETAILS

1.

Persons Contacted

Principal Licensee Employees

  • G. R. Horn, Division Manager, Nuclear Operations
  • G. A. Trevces, Division Manager, Nu: lear Support
  • J. W. Dutton, Nuclear Training Manager
  • G. E. Smith, Quality Assurance Manager
  • E. M. Mace, Senior Manager, Technical Support
  • J. V. Sayer, Radiological Manager
  • L. E. Bray, Regulatory Compliance Specialist
  • G. R. Suith, Licensing Supervisor

R. Windham, Technical Training Supervisor

In addition to the Senior Resident Inspector and the Resident Inspector,

NRC was represented by:

  • P. W. O'Connor, Senior Project Manager
  • Denotes those present during the exit interview conducted on

November 2,1988.

The NRC in..'-:ctors also interviewed other licensee employees during the

inspection period.

2.

Plant Status

The plant operated at essentially full power throughout the inspection

period.

3.

followuptoPlantEvents

(93702)

On October 21, 1988, the licensee performed Surveillance

Procediare 6.3.12.1, "Diesel Generator Operability Test," Revision 25, on

the Nt.mber 2 emergency diesel generator (EDG). Approximately 2 1/2 hours

into the test, a loss of control air pressure occurred and the "Turbo

Bearing Wear" annunciator alarmed. Consequently, the No. 2 EDG was

declared inoperable at 11:23 a.m. due to the unscheduled shutdown. A

maintenance work request (MWR) was issued to investigate and repair, or

replace, the relay and valve associated with maintaining a constant

control air pressure for the various EDG protective trips. After

replacement of the relay and rebuilding of the valve, control air pressure

still could not be maintained.

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Subsequently, the licensee performed o walkdown of the control air

instrument lines and identified a circumferential crack in a 1/4-inch

stainless steel instrument line.

The cracked line allowed 30 psi control

air to bleed off reducing pressure on the safety trip valve solenoid and

securing the EDG. Approximately 1 inch of the line was removed and

replaced with a compression fitting. The diesel generator was restarted

and, after completing a 4-hour run per SP 6.3.12.1, was declared operable

at 10:45 p.m.

Engineering sent the failed stainless steel instrument

tubing section to an offsite laboratory on November 3,1988, for analysis

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to determine the probable cause of the failure.

The control air system is a subsystem of the starting air system. The

starting air goes through two pressure reducing valves, 80 psi and 30 psi,

respectively, before it becoces control air. The control air subsystem is

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used to maintain the engine at a set speed regardless of engine load and

prctects the engine from abnormal conditions through protective trip

functions. The control air is used during engine operation, to hold the

valve open to the allow 80 psi air to hold the fuel racks in position.

If

control air or any of the diesel generator trips occur, 80 psi air flow to

the fuel shutoff cylinder is stopped which dumps the fuel racks and trips

the EDG.

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During followup of this event, the licensee identified to the NRC

inspectors that a design change relating to the EDGs is scheduled to be

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implemented on both EDGs during the next refueling outage.

The design

changes (DC 86-024 for EDG No. 2 and DC 87-061 for EDG No.1) will involve

replacing all copper instrunent tubing with stainless steel tubing and

moving all instruments subject to high vibration off the engine and onto

instrument racks.

The licensee demonstrated prompt, conservative action in responding to

this event.

No violations or deviations were identified in this area.

4.

Operational Safety Verification (71707)

The NRC inspectors ubserved operational activities throughout the

inspection period.

Proper control room staffing was observed to be

maintained, and control room activities and conduct were observed to be

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well controlled and professional.

The SRI observed selected shif t

turnover meetings and verified that infomation concerning plant status

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was properly communicated to the oncoming operators.

Control board

walkdowns and tours of accessible areas at thc facility were conducted to

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verify operability of plant equipment. Overall plant cleanliness was

observed to be very good throughout the inspection period.

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The NRC inspectors verified that selected activities of the licensee's

radiological protection program were implemanted in conformance with

facility policies and procedures and regulatory requirements.

Radiation

and/or contaminated areas were properly posted and controlled. Radiation

work permits contained appropriate information to ensure that work could

be performed in a safe and controlled manner.

Workers in radiation and/or

contaminated areas were observed to be wearing required protective

clothing and utilizing good radiological practices.

Radiation monitors

were properly utilized to check for contamination.

The NRC inspectors observed security personnel perform their duties of

vehicle, personnel, and package search.

Vehicles were properly authorized

and controlled or escorted in the protected area (PA). The NRC inspectors

conducted site tours to ensure that compensatory measures were properly

implemented as required because of equipment failure or equipment

deenergization due to the security upgrade in progress.

Personnel access

is documented in paragraph 5 of this report.

The PA barrier had adequate

illumination and the isolation zones were free of transient material.

The licensee continued to operate the plant in a safe, controlled manner.

Licensee personnel are aware of health physics requirements and perform

their duties utilizing good radiological control practices.

No violations

or deviations were identified in this area.

5.

Access Control - Personnel

(81070)

The NRC irspectors observed security personnel monitor personnel access to

the site.

On October 23, 1988, and October 24, 1988, an individual was

allowed unescorted access to the site after his security training had

expired. This is an apparent violation (298/8831-01), of Plant Services

Procedure 1.1, "Station Security," Revision 9, dated October 3,1988.

The NRC inspectors determined that the recurity department had not

received notice from the training department that the individual's

training had expired, as required by procedure. The training department

had not issued the required notice due to a computer problem.

Previous

records have been documented in NRC Inspection

problems with training (Violation 298/8802-02) and 50-298/88-09.The

Reports 50-298/88-02,

licensee was in the process of attempting to manually identify persons

whose site access training had expired, when the apparent violation was

identified by the NRC inspector.

The individual's training had been

expired for approximately 6 weeks.

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The root cause of the apparent violation is similar to a previous

violation and may indicate lack of timely corrective action.

No other

violations or deviations were identified in this area,

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6.

Monthly Surveillance Observations (61726)

The SRI observed the performance of portions of Surveillance

Procedure (SP) 6.2.1.4.3, "PCIS Main Steam Line Low Pressure Calibration

and Functional / Functional Test," Revision 19, dated April 14, 1988.

This

toverify(protective

surveillance was performed on October 26, 1988,

TS). The test

instrumentation operability per Technical Specifications

was performed by qualified technicians in accordance with the procedure.

All precautions and prerequisites were met and all reviews of the

completed procedure were properly performed. Test results were within TS

and procedure limits.

The SRI reviewed SP 6.3.12.1, "Diesel Generator Operability Test,'

Revision 25, dated October 6,1988. On October 21, 1988, this

surveillance was performed twice on diesel generator (DG) No. 2.

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first performance was conducted to meet TS requirements demonstrating

monthly operability of DGs. The second performance was to demonstrate

monthly operability as well as operability after repair.

The procedure,

in each instance, was properly reviewed by all required personnel.

The

first procedure adequately described the reason for termination and

failure of the test.

The liMnsee perfonced surveillances in accordance with applicable

procedures.

Corrective action is orompt and conservative when problems

are observed.

No violations or deviations were identified in this area.

7.

Monthly Maintenance Observation (62703)

On October 23, 1988, reactor recirculation Pump A twice increased speed

for no apparent reason, and with no operator action to cause the speed

increase.

The first time the speed increase was observed, the

recirculation pump returned to normal speed within a short period of time

with no operator action. When the speed increased the second time, the

reactor operators reduced speed manually to a level below the initial

speed setpoint and continued to monitor the pump.

On October 24, 1988, Work Item 88-4435 was issued to troubleshoot and

repair the problem.

It was determined that the speed increase was caused

by a dirty potentiometer which has since been replaced.

The NRC

inspectors monitored the troubleshooting and repair, and verified that no

limits had been exceeded during the pump speed increase.

The licensee's response to the plant problem was prompt and

conservative. No violations or deviatiens were identified in this area.

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8.

Emergency Excercise (82301)

The NRC inspectors observed a practice emergency exercise on October 4,

1988, and attended the NPPD critique and NRC exit concerning the annual

emergency exercise conducted on October 18, 1988.

Results of the annual

emergency exercise are documented in NRC Inspection Report 50-298/88-29.

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During the practice exercise the RI observed the licensee's response to a

personnel injury.

Inadequate medical team response had previously been

identified as a deficiency (298/8725-06).

During this portion of the

exercise, the RI noted that the injured man was moved approximately

50 feet to an area with a lower radiation dose rate with no apparent

consideration as to whether the radiation levels indicated an innediate

need to move the individual or whether further injury could be caused by

the move.

In addition, it was noted that there was little action taken by

personnel to prevent any potential spread of contamination although

sufficient time and resources were available.

Deficiency 298/8725-06 is

still open.

The NRC inspectors noted problems with communication and the exercise

scenario during the practice exercise and connunicated these observations

to licensee management.

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The SRI considered the practice exercise satisfactory; however, some

problems were observed.

The comnunications problem was identified during

the 1987 annual emergency exercise. No violations or deviations were

identified.

9.

Exit Interview (30703)

An exit interview was conducted on November 2,1988, with licensee

representatises (identified in paragraph 1).

During this interview, the

SRI reviewed the scope and findings of the inspection. Other meetings

between the NRC inspectors and licensee management were held periodically

during the inspection period to discuss identified concerns.

The licensee

did not identify as proprietary any information provided to, or reviewed

by, the inspectors.

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