ML20205C957

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Monthly Operating Rept for Jan 1987
ML20205C957
Person / Time
Site: Farley 
Issue date: 01/31/1987
From: Mcdonald R, Woodard J
ALABAMA POWER CO.
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
NUDOCS 8703300300
Download: ML20205C957 (7)


Text

'

f JOSEPH M. FARLEY NUCLEAR PLANT

-UNIT 1

NARRATIVE SIDetARY OF OPERATIONS January,' 1987 There were four unit shutdowns during the' month of January.. The first.

unit shutdown occurred on January 8 when a turbine trip was initiated manually due to~an air-leak on an air supply lline to a main steam isolation valve (MSIV)..The air line to the MSIV had moved into contact with a rigid.

tubing support due to thermal expansion. This caused the air supply line

-to crack and leak. The air line was replaced and the tubing support notched so that it would not be in contact with the air line.

The second unit shutdown occurred on January 9 when the unit was ramping up from the first shutdown of the month and the reactor tripped due to lo-lo steam generator level following.a manual tripping of the main turbine.

The turbine was tripped because both steam generator feed pumps (SGFPs) had tripped ~due to low suction pressure. This reactor trip was caused by personnel error in that the operators and shift supervisor failed to adequately'_ monitor the SGFP suction pressure and take appropriate action to prevent the'SGFP pressure from decreasing below the trip setpoint for SGFPs.

The appropriate procedures have been revised to remind operators to monitor SGFP pressure.

The third unit shutdown occurred on January 13 when-the unit was ramped down and the generator taken off-line to repair a leaking turbine interface valve.

The valve was replaced and the unit returned to power operation.

The fourth unit shutdown ~ occurred on January 22 when the reactor tripped.due to high flux rate as indicated by nuclear instrumentation channels N41 and N42. The lA inverter which supplies power-to N41 failed

-while N42 was in test. for surveillance. This resulted in the two-out-of-

~

four coincidence for a high flux rate reactor trip. The testing on N42 was completed and N42 was returned to service. The backup power supply for N41 was placed in service and the unit returned to power operation.

The following major safety-related maintenance was performed in the month of January:

1.-

An air leak was repaired on an MSIV-air supply line.

2.

The 1A inverter was tested and four blown fuses were replaced. No cause for the blown fuses could be found. The inverter was returned to service.

3.

Miscellaneous corrective and preventive maintenance was performed on diesel generators.

~

8703300300 870131 p

DR ADOCK 0500 8

DOCKET NO.

50-348 UNIT 1

DATE February 3, 1987 COMPLETED BY J. D. Woodard TELEPHONE (205)899-5156 M0tGH January DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (PWe-Net)

(PWe-Net) 1 833 17 831 2

835 18 825 3

835 19 810~

4 835 20 836 5

835 21 835 6

835 22 411 7

832 23 281 8

210 24 821 9

26 25 823 10 656 26 828 11 832 27 827 12 832 28 828 13 286 29 830 14 764 30 822 15 874 31 832 16 830 INSTRUCTIONS On this format, list the average daily unit power level in PWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.

Form 13/21

/

\\

OPERATING DA'm REPGtT DOCKET NO.

50-348 DATE 2/3/87 COMPLETED BY J. D. Woodard

'IELEPHONE (205)899-5156 OPERATING S'm'IUS Notes

1. Unit Name:

Joseph M. Farley - Unit 1

2. Reporting Period:

January, 1987

1) Cumulative data since
3. Licensed Thermal Power (Nt):

2,652 12-1-77, date of

4. Nameplate Rating (Gross Ne):

860 commercial operation

5. Design Electrical Rating (Net Ne): 829
6. Maximum Dependable Capacity (Gross Ne):

856.0

7. Maximum Dependable Capacity (Net MNe):

825.1

8. If Changes occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

Items #6 and #7 have been changed due to evaluation of operating experience.

9. Power Level To Which Restricted, If Any (Net Ne):

N/A

10. Reasons For Restrictions, If Any:

N/A

'Ihis Month Yr-to-Date Cumulative

11. Hours In Reporting Period 744 744 80,376
12. Number Of Hours Reactor Was Critical 719.5 719.5 57,629.0
13. Reactor Reserve Shutdown Hours 0.0 0.0 3,650.0
14. Hours Generator On-Line 685.5 685.5 56,307.9
15. Unit Reserve Shutdown Hours

.0.0 0.0 0.0

16. Gross Thermal Energy Ger.erated (MWH) 1,751,070 1,751,070 343,078,738
17. Gross Electrical Energy (MWH) 572,974 572,974 45,936,018
18. Net Electrical Energy Generated (MH) 541,584 541,584 43,265,918
19. Unit Service Factor 92.1 92.1 70.1
20. Unit Availability Factor 92.1 92.1 70.1
21. Unit Capacity Factor (Using MDC Net) 88.2 88.2 67.0
22. Unit Capacity Factor (Using DER Net) 87.8 87.8 64.9
23. Unit Forced Outage Rate 7.9 7.9 10.5
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

N/A

25. If Shut Down At End Of Report Period, Estimated Date of Startup:

N/A

26. Units In Test Status (Prior to Commercial Operation):

Forecast Achieved INITIAL CRITICALLY 08/06/77 08/09/77 INITIAL ELECTRICITY 08/20/77 08/18/77 COMERCIAL OPERATION 12/01/77 12/01/77 Form 2/34

~

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O UNITSiluTDOWNS AND POWER REI)UCTIONS X)OCKETNO. _50-348 UNITNAME J. M. Farl_ey-Unit 1' ilATE _ February 4, 1987 Page 1 of 3 REPORT MONTil January COMPLETER) uY J. D. Woodard TELEtllONE

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001 870108 F

25.2 A

2 87-002-00 SB TBG A turbine trip was initiated manually g

due to an air leak on an air supply line to a main steam isolation valve (MSIV) resulting in a reactor trip.

The air'line to the MSIV had mo'ved into contact with a rigid tubing support due to thermal expansion of th'e main steam line. This caused the air supply line to crack and leak. The air line was replaced and ~

the tubing support was notched so that it would not be in contact with the air line.

I 3

  • J 4

F: Fos ed Reason:

kleshod:

Exhibis G. Insisuctiims s

S: Selieduled A Eigul miens failure (Emplain) 14tanual fin Prepasasion of Data i

I 41ainicnance of Test 24fanual Scram.

Ensey Sliccis for 1.itensee C-RelucFmg 3 Ausoniatic Scrans.

Etens Repos:(i.ER) fileINUREG-13 Hegu14tosy Hesielcliam 4 Osliet (Emplain) 0161)

E Opesasus Training & license Enandnation F Adminisisasive 5

G Opceasismal Enot (limplain)

I'J/77) ll Oslics (Eaplain)

E.sinbis I. Same Simsce

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. O UNITSilUTDOWNS AND POWER REIMM'TIONS ETNO l

E Farlev-Unit 1 DATE Februarv 4.

1987

'Page 2 of 3' REPORT MONTil January COMPLETED BY T-n_ unnanrd El.EPilONE (205)899-5156

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g Ey Licensee

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Cause & Caureceive No-Daic

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Action to iN0 oIE r2 jis g Repmt a

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002 870109 F

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3 87-003-00

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The reactor tripped due to lo-lo steam generator level following the manual tripping of the main turbine. The turbine was trippe.d because both steam generator feed pumps (SGFPs) had tripped due to low suction pressure. The reactor trip was caused by personnel error in that the operators and shift supervisor failed to adequately.

i.

monitor the SGFP suction pressure and take appropriate action to prevent the SGFP suction pressure j

from decreasing below the SGFP~

trip setpoint. The appropriate procedures have been revised to remind operators'to monitor j

SGFP suction pressure.

I 1

2 3

4 I

F: Forced Reason:

Methoil:

Exhibit G. Instructions

i S: Soheduled A-Equipment Failure (Explain) 1 Manual for Pseparation of Data 1

B-Maintenance of Test 2-Manual Scram.

Ensey $heets for Iicensee C Refueling 3 Automatic Scram.

Event Report (1 ER) File (NUREG-D-Regulatosy Resiticsion 4 Osher (Explain) 0161)

E-Operator Training & license Examination F-Administrative 5

G-Operational Esaur (Explain)

Exhibit I-Same Source (9/77) 11 Othes (Explain)

)

q V

v UNITSilinDOWNS AND POWER REIMICIIONS

' DOCK!!T NO.

5'0-348 UNIT NAhlE J. M. Farlev-Unit l' DAIE _Fehrnarv 4.

1987 Page 3 of 3 gg,;OltT AIONiil January COMi*l.ElliD llY.

J. D. Woodard TEl.LPilONE (205)899-5156

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c ee Na ~

Date TS

'"S# A I"'C'8 IVC

.E g a:

Evens

r. ?
o. g acigon go So n

$b dj lteport #

N0 O

l**Cveni Hecursence 5

003 870113 F

7.5 B

1 N/A TG XCV The unit.was ramped down and the generator taken off line to repair a leaking turbine interface valve. The valve was replaced and the unit returned to power operation.

004 870122 F

19.2 A

3 87-004-00 EF INVT Reactor tripped due to high flux rate as indicated by nuclear instruments N41 and N42. The 1A inverter which supplies power to N41 failed while N42 was in test for surveillance. This resulted in the two out of four coincidence for.high flux rate trip.

The testing on N42 was completed and N42 was returned to service. The backup power supply for N41 was placed in service and the unit returned to power operation, i

2 3

4 F: For6cd Reason:

Method:

Exhibit G - Instiuctions S. S<lieduled A Eaguipinent Failure (Explain) 1 -Manual for Picparation of Data li-Maintenance of Test 2 Manual Scrain.

Ensiy Sliec s for iicensee C-l<cfueling 3 Autoenatic Scrain.

Event Repius (1.ER)lile INUMEG-D-Itegulatiny itesuiction 4 Othes (Explain) 0161) 1 Opesaior Tsaining1 Iicense Exainination F-Adsninists sive 5

G Opes.stional I. sos (lixplain) thhibil 1 Sanie Source 19//7)

It Olhes (Explain)

.* ~

Alabama Power Company 600 North 18th Street Post Office Box 2641 Birmingham, Alabama 35291-0400 Telephone 205 250-1835 AlabamaPower enio V ce r sident February 10, 1987 Docket No. 50-348 Director, Office of Resource Management U. S. Nuclear Regulatory Commission Washington, D.C.

20555

Dear Sir:

RE: Joseph M. Farley Nuclear Plant Unit 1 Monthly Operating Data Report Attached are two (2) copies of the January 1987 Monthly Operating Report for Joseph M. Farley Nuclear Plant Unit 1, required by Section 6.9.1.10 of the Technical Specifications.

If you have any questions, please advise.

Yours very ly,

- ut/

t R. P. Mcdonald RPM /BCE:mab/F-2 Enclosures xc: Director, IE (10 copies)

Director, RII (1 copy) t 1/t mv

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