ML20205C722
| ML20205C722 | |
| Person / Time | |
|---|---|
| Site: | Calvert Cliffs |
| Issue date: | 08/31/1985 |
| From: | Porter R, Russell L BALTIMORE GAS & ELECTRIC CO. |
| To: | NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| NUDOCS 8509230168 | |
| Download: ML20205C722 (11) | |
Text
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OPERA'11NG DATA REPORT Docket No. 50-317 Date: September 11,1985 Completed by R. Porter Telephone: (301) 260-4747 OPERA'11NG STATUS eeeeeeeeeeeeeeeeees 1.
Unit Name:
Calvert Cliffs No.1 2.
Reporting Period:
AUGUST 1985 3.
Licensed Thermal Power (MWT):
2,700 4.
Nameplate Rating (gross MWe):
918 5.
Design Electrical Rating (Net MWE):
845 6.
Maximum Dependable Capacity Gross MWe:
860 7.
Maximum Dependable Capacity (Net MWe):
825 8.
Change In Capacity Ratings:
None 9.
Power LevelTo Which Restricted (Net MW):
NA 10.
Reasons For Restrictions:
NA
'Ihis Month Yr-To-Date Cumulative 11.
liours in Reporting Period 744 5,831 90,444 12.
Number Of IIours Reactor Was Critical 313.0 2,595.6 70,093.5 13.
Reactor Reserve Shutdown IIours 300.0 1,034.3 3,019.4 14.
IIours Generator On-line 264.0 2,448.2 68,619.0 15.
Unit Reserve Shutdown liours 0.0 0.0 0.0 16.
Gross Thermal Energy Generated (MWil) 453,502 6,246,068 170,028,805 17.
Gross Electrical Energy Generated (MWil) 139,131 2,107,815 56,151,195 18.
Net Electrical Energy Generated (MWII) 128,417 2,011,289 53,567,855 19.
Unit Service Factor 35.5 42.0 75.9 20.
Unit Availability Factor 35.5 42.0 75.9 21.
Unit Capacity Factor (Using MDC Net) 20.9 41.8 72.4 22.
Unit Capacity Factor (Using DER Net) 20.4 40.8 70.1 20 Unit Forced Outage Rate 10.6 25.7 9.2 24.
Shutdowns Scheduled Over the Next Six Months (type, date, and duration): None 25.
If Shutdown At End Of Report Period, Estimated Date Of Startup: NA E509230168 850031 7
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UNIT SIRTITX)WNS AND l'UWFR REDtXTIONS IX)CKI'T NO.
50-317 UNIT NAME Calvert Cliffs I DNI1? September 11 1985 n
COMPI.ETI',D IlY R. J. Port,e,r_ _
REIN)RT M)N'11I August 17,I.EPIK)NE (301) 260-4747_-
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Cause & Correct ive No.
Dat e yg g
yg I' vent.
go
'g Action t o j,y RelMu'l #
U l'revent Recuri ence H
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ova 5 y
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.8 85-03 850801 S
124.1 C
4 NA RC FUELXX The 7th scheduled refueling o'it-age, which commenced on April 5, 1985, is continuing due to failed upper and lower shaft seals on 11B Reactor Coolant Pump.
85-04 850806 F
9.4 11 3
85-08
!!J IrfEXCil Moisture Separator liigh Level 85-05 850806 S
3.2 B
NA NA IIA MECFUN Main Turbine was removed from service for planned maintenance.
85-06 850806 F
8.0 11 3
85-09 CC lirEXCll Steam Generator Low Level 85-07 850807 F
13.8 11 3
85-10 llA MECFUN Main Turbine Thrust Bearing Trip 85-08 850814 S
321.5 B
1 NA IIA PIPEXX Blockage in Main Generator Stator Coolant piping.
I 3
4 F: Forcect Reason:
Met hext:
Exhibi t G-Inst ruct. ions S: Sche <lu t et!
A-Feriipment. Failure (Explain) l -Fhrnia l for Pr eparat. ion of Dat.a Il-Maint cnance or Test.
2-Ruinal Scram.
Ent ry Sheet s for I irense C-Refneling 3-Ant omat ic Scram.
Event Report. (I.ER) File-D-Regulat ory Rest rict ion 1-Ot her (Explain)
( NTRI G-0161 )
E-Operator Training & l.icense Examinat ion F-A<lmi n i st rat ive G-Ogw rational Error (Explain) 5 Exhibit. I - same S<=irce II-Ot her (Explain)
AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-317 Calvert Cliffs Unit No.1 Date: September 11,1985 Completed By R. Porter Telephone: (301)-260-4747 AUGUST 1985 Day Average Daily Power Level Day Average Daily Power Level (MWe-Net)
(MWe-Net) 1 0
17 0
2 0
18 0
3 0
19 0
4 0
20 0
5 0
21 0
6 0
22 0
7 87 23 0
8 162 24 0
9 362 25 0
10 371 26 0
11 588 27 0
12 402 28 309 13 376 29 767 14 267 30 829 15 0
31 830 16 0
INSTRUCTIONS:
On this forraat, list the avera e daily unit power level in MWe-Net for each l
day in the reporting month. gompure to the nearest whole megawatt.
i
OPERATING DATA REPORT Docket No. 50-318 Date: September 11,1985 Completed by R. Porter Telephone: (301) 260-4747 OPERATING STATUS seeeeeesseeeeeeeeee 1.
Unit Name:
Calvert Cliffs No. 2 2.
Report'.ng Period:
AUGUST 1985 3.
Licensed Thermal Power (MWT):
2,700 4.
Nameplate Rating (gross MWe):
911 5.
Design Electrical Rating (Net MWE):
845 6.
Maximum Dependable Capacity Gross MWe:
860 7.
Maximum Dependable Capacity (Net MWe):
825 8.
Change In Capacity Ratings:
None 9.
Power Level To Which Restricted (Net MW):
NA 10.
Reasons For Restrictions:
NA This Month Yr-To-Date Cumulative 11.
IIours In Reporting Period 744 5,831 73,799 12.
Number Of Ifours Reactor Was Critical 641.6 5,169.5 61,728.3 13.
Reactor Reserve Shutdown IIours 102.4 292.7 1,260.7 14.
Hours Generator On-line 637.9 5,149.8 60,769.1 15.
Unit Reserve Shutdown Ilours 0.0 0.0 0.0 16.
Gross Thermal Energy Generated (MWil) 1,628,734 13,597,564 152,318,501 17.
Gross Electrical Energy Generated (MWil) 521,673 4,489,353 50,147,556 18.
Net Electrical Energy Generated (MWII) 499,692 4,295,629 47,837,837 19.
Unit Service Factor 85.7 88.3 82.3 20.
Unit Availability Factor 85.7 88.3 82.3 21.
Unit Capacity Factor (Using MDC Net) 81.4 89.3 78.9 22.
Unit Capacity Factor (Using DER Net) 79.5 87.2 76.7 23.
Unit Forced Outage Rate 0.0 6.9 6.3 24, Shutdowns Scheduled Over the Next Six Months (type, date, and duration): Sixth Refueling Outage, October 19,1985 to December 22,1985 25.
If Shutdown At End Of Report Period, Estimated Date Of Startup: NA
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4 UNIT SillTI1X1WNS AND l'UWi-R RFJMICTIONS INXXET NO. 50-318 IINIT NAW Calvert Cliffs 2 DAE.S.eptember 11, 1935 CO WI.F/IV,D BY R. J. Porter REI'tRT PENffli August
'IT,f.EPIIONE (3011 260-4747 "c
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l.icensee g
Caisse & Correct ive h
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}gg No.
Dat.e Event.
g g
Act ion t o Regwirt #
gy H
- t. 3 y
y ]n 5 v
Prevent, Recurrence b
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8 w
85-07 850801 S
106.1 A
1 NA CC PIPEXX TheUnitwasshutdownon7/23/85 to repair cold reheat piping.
Startup is being delayed while repairs are made to 21 Main Steam Isolation Valve Ilydraulic System.
1 85-08 850813 S
0 B
4 NA IIF flTEXCil 85-09 850817 S
O B
4 NA IIF flTEXCil Reduced load to clean c ndenser water boxes I
85-10 850819 S
O B
4 NA I!F flTEXCII of crabs, fish, and 85-11 850820 S
0 B
4 NA IIF flTEXCll grass 85-12 850823 S
O B
4 NA IIF IITEXCil 85-13 850826 F
0 A
4 NA lill VALVEX 21 Ileater Drain Tank level control valve failed shut when the disc became separated from the valve stem.
I 4
F: Forced Reason:
M tluwt:
Exhibit G-Inst :1ct. ions
.S:
Schethaled A-E<piipment failure (Explain) 14tunna t for Prejnration of Dat.a B-Maintenance or Test.
24tinual Scram.
Ent ry Sheet s for 1,icense C-Refueling 3-Aut omat ic Scram.
Event, Report (LER) File D-Regulat ory Restrict. ion 4-Other (Explain)
E-Operator Training & License Examinat. ion F-Achninist.rative G-Operational Error (Explain) 5 Exhibit I - Sam S<xn ce II-other (Explain)
AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-318 Calvert Cliffs Unit No. 2 Date: September 11,1985 Completed By R. Porter Telephone: (301)-260-4747 AUGUST 1985 seeeeeeeeee.
Day Avwege Daily Power Level Day Average Daily Power Level (MWe-Net /
(MWe-Net) 1 0
17 651 2
0 18 597 3
0 19 665 4
0 20 756 5
235 21 770 6
824 22 816 7
829 23 820 8
832 24 748 9
833 25 835 10 831 26 827 11 831 27 755 12 827 28 828 13 815 29 817 1s 839 30 787 15 805 31 834 16 812 INSTRUCTIONS:
l On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
l
SUMMARY
OF UNIT 1 OPERATING EXPERIENCE AUGUST 1985
/
8/1 At the beginning of this reporting period, Unit I was shut down continuing its seventh scheduled refueling outage.
8/5 No.11D Reactor Coolant Pump shaft seal replacement was complete and the reactor was taken critical at 1406.
8/6 The Unit was paralleled at 0405. At 0426, the reactor tripped on loss of load when the main turbine tripped on high levelin 11 Moisture Separator Reheater. The Unit was brought critical at 0922 and paralleled at 1350.
The main turbine was removed from the grid at 1804 for planned maintenance and paralleled at 2120. At 2146, the reactor tripped on low steam generator level.
l 8/7 The reactor was brought critical at 0318 and paralleled at 0547. At 1950, i
the reactor tripped on loss of load when the thrust bearing wear sensor erroneously tripped the main turbine.
J 8/8 The reactor was brought critical at 0615 and paralleled at 0935.
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8/14 Commenced shutting down the Unit at 1700 to investigate high temperatures in the main generator stator. The Unit was removed from the grid at 2024 and the reactor shut down at 2030.
1 8/27 A stator coolant flow problem was corrected and the Unit was brought critical at 0830.
8/28 The Unit was paralleled at 0553.
8/29 The Unit was brought to 100% power (820 MWe) at 1045.
8/31 At the end of this reporting period, Unit 1 was operating at 830 MWe with i
the reactor at 100% power.
i
SUtdMARY OF UNIT 2 OPERA'I1NG EXPERIENCE AUGU8T 1985 8/1 At the beginning of this reporting period, Unit 2 was shut down continuing a planned outage while repairs were being made to 21 Main Steam Isolation Valve hydraulic system.
8/5 The reactor was brought critical at 0623 and paralleled at 1006.
8/6 The Unit was brought to fullload operation (825 MWe) at 0400.
8/13 Reduced load to 630 MWe at 2205 to clean main condenser waterboxes.
8/14 Resumed fullload operation (800 MWe) at 0910. Reduced load to 790 MWe at 1747 when two condenser air removal units tripped.
Resumed full load operation (800 MWe) at 1810.
8/17 Reduced load to 600 MWe at 0400 to clean main condenser waterboxes.
8/19 Load was increased to 700 MWe at 0700, but 100% power could not be reached due to high circulating water differential temperature. Reduced load to 570 MWe at 2225 to clean waterboxes.
8/20 Resumed full load operation (813 MWe) at 0745. Reduced load to 630 MWe at 2200 to clean main condenser waterboxes.
8/21 Resumed full load operation (815 MWe) at 0930.
8/23 Reduced load to 620 MWe at 2155 to clean main condenser waterboxes.
8/24 Resumed full load operation (840 MWe) at 1415.
8/26 Reduced load to 640 MWe at 2258 when 21 heater drain tank level control valve failed shut.
8/27 Resumed fullload operation (827 MWe) at 1010.
8/29 Reduced load to 680 MWe at 2150 to clean main condenser waterboxes.
8/30 Resumed full load operation (833 MWe) at 0930.
8/31 At the end of this reporting period, Unit 2 was operating at 833 MWe with the reactor at 100% power.
4
September 4,1985 REFUELING INFORMATION REQUEST 1.
Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No.1 2.
Scheduled date for next Refueling Shutdown: October 25,1986 3.
Scheduled date for restart following refueling: December 27,1986 4.
Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?
Resumption of operation after refueling will require changes to Technical 1
Specifications. The changes will be such as to allow operation of the plant with a fresh reload batch and reshuffled core.
5.
Scheduled date(s) for submitting proposed licensing action and supporting information.
September 23,1986 6.
Important licensing considerations associated with the refueling.
Reload fuel will be similar to that reload fuel inserted into the previous cycle.
7.
The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool.
(a) 217 (b) 940 Spent Fuel Pools are common to Units 1 and 2 8.
(a) The present licensed spent fuel pool storage capacity, and (b) the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.
(a) 1830 (b)0 9.
The prcjected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off load.
April,1991 s
_ ~...
September 4,1985 REFUELING INFORMATION REQUEST
- 1. Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No. 2.
- 2. Scheduled date for next refueling shutdown: October 19,1985.
- 3. Scheduled date for restart following refueling: December 4,1985.
- 4. Will refueling or resumption of operation thereafter require a technical specification change or other licensed amendment?
Resumption of operation after refueling will require changes to Technical Specifications. The changes will be such as to allow operation of the plant with a fresh reload batch and reshuffled core.
- 5. Scheduled date(s) for submitting proposed licensing action and supporting information.
September 2,1985
- 6. Important licensing considerations associated with refueling.
Reload fuel will be similar to that reload fuel inserted in the previous cycle.
- 7. The number of fuel assemblies (a) in the core and (b) in the Spent Fuel Storage Pool.
(a) 217 (b) 940 Spent Fuel Poolis common to Units 1 and 2.
- 8. (a) The present licensed spent fuel pool storage capacity, and (b) the size of any increase in lleensed storage capacity that has been required or is planned, in number of fuel assemblies.
(a) 1830 (b)0
- 9. The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed espacity and maintainir.g space for one full core off load.
April,1991
'e BALTIMORE G AS AND ELECTRIC COMPANY P.O. BO X 14 7 5 B ALTIMOR E. M A R YL AN D 21203 C LvER
- CL FFS NUCL A WER PLANT tussy. u=RvLAno ross7 September 11,1985 Director Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Washington, D.C. 20055 Attention:
Document Control Desk
Subject:
August Operating Data Reports for Calvert Cliffs Units 1 and 2 (Dockets 50-317 and 50-318)
Gentlemen:
The subject reports are being sent to you as required by Technical Spepcification 6.9.1.6.
If there are any questions, please contact Bob Porter (301)-260-4747.
Sincerely, L. B. Russell Plant Superintendent LBR/djw Attachment Copies:
R. F. Ash (BG&E)
P. A. Pieringer (BG&E)
M. Beebe (NRC)
D. Reilly (INPO)
E. K. Bewley (BG&E)
P. Ross (N RC)
T. Foley (NRC)
T. E. Ruszin, Jr. (BG&E)
K. Gibbard (DOE)
P. D. Sierer, Jr. (BG&E)
A. E. Lundvall, Jr.(BG&E)
J. A. Tiernan (BG&E)
T. Magette (DNR)
E. Wenzinger (NRC)
R. R. Mills (CE)
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,