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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20249A4121998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7501998-04-30030 April 1998 Rev 2 to Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit ML20247F6721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Davis-Bess Nuclear Power Station,Unit 1 ML20249A4141998-04-30030 April 1998 Revised Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216B4041998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216C5131998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20202D3721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20198K7931997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20203A3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Davis-Besse Nuclear Power Plant,Unit 1 ML20198S5371997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Davis-Besse Nuclear Power Station ML20217H7701997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20216H3261997-08-31031 August 1997 Monthly Operating Rept for August 1997 for DBNPS ML20217K0241997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Davis Besse Nuclear Power Station,Unit 1 ML20140H0441997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Davis-Besse Nuclear Power Station Unit 1 ML20141B9521997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Davis-Beese Nuclear Power Station Unit 1 ML20137T5271997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20136G7221997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Davis-Besse Nuclear Station Unit 1 ML20134L9831997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Dbnps,Unit 1. W/Undated Ltr ML20133G0161996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20149M4071996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Davis-Besse Nuclear Power Station Unit 1 ML20134P9821996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20128Q0611996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Davis-Besse NPP, Unit 1 ML20117D5341996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20117D5411996-06-30030 June 1996 Revised MOR for June 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20116E0161996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Davis-Besse Nuclear Station Unit 1 ML20113B9111996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Davis-Beese Nuclear Power Station Unit 1 ML20117H7231996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Davis-Besse Unit 1 ML20112E6061996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for David-Besse Nuclear Power Station,Unit 1 ML20101G5251996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for DBNPS Unit 1 ML20149K7711996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Davis-Besse Nuclear Power Station.W/Undated Ltr ML20096C7971995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20095H3761995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20094L1041995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20093J2341995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Davis-Besse Nuclear Power Station ML20098A2651995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Davis-Besse Nuclear Power Station,Unit 1 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
[Table view] |
Text
-
s.
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-346 g7c4;7 Davis-Besse Unit 1 February 10. 1986 DATE COMPLETED BY Morteza Khazrai TELEPHONE (419) 249-5000 Ext.
MONTH
' January, 1986 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net!
1 0
17 0
2 n
Ig 0
3 0
39 0
4 0
20 0
5 0
21 0
0 6
22 0
7 0
D 0
8 0
0 24 9
0 25 0
10 0
26 0
11 0
27 0
12 0
0 28 13 0
29 0
14 0
30 0
15 0
33 0
16 0
INS'IRtJCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
(W77 i R
II
OPERATING DATA REPORT DOCKET NO.
50-346 DATE hhrmary 10, 1986 COMPLETED BY.Mo.r.t;;;uLl(hazrai TELEPHONE (419) 249-5000, Ext.
7290 OPERATING STATUS
- 1. Unit Name:
Davis-Besse Unit 1 Notes
. 2. % Paiod January 1986
- 3. Licensed Thermal Power (MWr):
2772
- 4. Nameplate Rating (Gross MWe):
QM
- 5. Design Electrical Rating (Net MWe):
onA
- 6. Maximum Dependable Capacity (Gross MWe):
904
~1. !4axnnum Dependable Capacity (Net MWe):
860
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since !.ast Report. Give Reasons:
- 9. Power Level To Which Restricted. If Any (Net MWe):
_10. Reasons For Restrictions,if Any:
This Month YrAo-Date Cumalative
(
- 11. Hours in Repon.g Period 744 744 65.809 l
!2. Number Of Hours Reactor Was Critical 0.0 0.0 35.877.I
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 4.058.8 i
- 14. Hours Generator On-Line 0.0 0.0 34.371.8 l
- 15. Unit Reserve Shutdown Hours 0.0 0.0
- 1. 732. 5
- 16. Gmss Thermal Energy Generated (MWH) 0.0 0.0 81.297.600
- 17. Gross Electrical Energy Generated (MWH) 0.0 0.0 25.233.I77 0.,0,
0.0 26,933,622
- 18. Net Electrical Energy Generated (MWH)
' 19. Unit Service Factor 0.0 0.0 52.2
- 20. Unit Availability Factor 0.0 0.0 54.9
- 21. Unit Capacity Factor iUsing MDC Net) 0.0 0.0 44.6
- 22. Unit Capacity Factor (Us;ng DER Net) 0.0 0.0 42.3 I
- 23. Unit Forced Outage Rate 100.0 100.0 26.:
AL Eb W!=us Scheduled Over Next 6 Months (Type. Date.and Duration of Each1:
L.
l
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units In Test Status (Prior o Commercial Operation):
Forecast Achiesed INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIA L OPERATION (9/77 )
1
_g 4
7,.
DOCKET Nob
~ 50-346' UNIT SMrfDOWNS AND POVER REDUCTIONS UNIT MAME.
D:vix-Berse Unit
.=%
DATE February 10, 1985 COMPLETED BY-Morteza Khazrai
. REPORT MONTH January, ~ 1986 TELEPHONE.
.(419) 249-5000 Ext. 7290;
- t "u
8,,,
"a I
Licensee a,e n
Cause & Corrective 1'
1 UE i UE Event 3I gj e
Action to.
I
.No.
Date N
Oo I
d.$ "
Roport #
EO 5o l'revent Recurrence 85 fi[
a 7
85 06 09 F
744 A
4 LER 85-013 JK SC The unit remained shutdown follow-
- on't ing the reactor trip on June 9, 4
1985 j
See Operational Summary for further l
details.
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I I
j F: Forced
. Reason:
Method:
Exhibit G - Instructions 4
i S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee 3
C-Refueling 3-Automatic Scram Event Report (LER) File j
D-Regulatory Restriction 4-Continuation from (NUREG-0161)
E-Operator Training & License Examination Previous Month F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-Other (Explain)
Exhibit I - Same Source (9/77)
H-Other (Explain)
4 OPERATIONAL
SUMMARY
JANUARY 1986 The unit-remained shutdown the entire month of December following the reactor trip on June 9, 1985.
Investigation of the causes of the event and corrective actions' continue. See NUREG 1154 for further details.
Below are some of the major activities performed during this month:
- 1) Completed reinstallation of Power Operated Relief Valve (PORV)
- 2) Completed condenser hydro leak test
- 3) Repair and replacement of all the hydro motor actuators
- 4) Completed work on Decay Heat Loop #2
- 5) Repair condenser internal damage (heater shroud metal)
- 6) Replacing gasket and studs on steam generator primary side manway
.r E
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R UELING INFORMATION
-DATE: J nuary, 1986 gn 1.
Name of facility: Davis-Besse Unit 1
~
Scheduled date for next refueling shutdown: March 1, l'987
- 2..
3.
Scheduled date for restart following refueling: May 10, 1987
-4..
.Will refueling or resumption of operation thereafter require a technical specification change or other license amendment? If answer is yes, what in general will these be? If answer is no, has the reload fuel design and core configuration been reviewed by your Plant Safety Review Committee to determine whether any unreviewed safety questions are associated with the core reload (Ref. 10 CFR Section-50.59)?
Ans: Expect the Reload Report to require standard reload fuel design Technical Specification changes (3/4.1 Reactivity Control Systems and 3/4.2 Power Distribution Limits).
5.
. Scheduled date(s) for submitting proposed licensing action and supporting information: Winter, 1986 6.
Important licensing considerations associated with refueling, e.g.,
new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
Ans: None identified to date.
7.
The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool.
(a) 177 (b) 204 - Spent Fuel Assemblies 8.
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.
Present: 735 Increase size by: 0 (zero) 9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity.
Date:
1992 -- assuming ability to unload the entire core into the spent fuel pool is maintained.
BMS/005
c-COMPLETED FACILITY CHANGE REOUEST FCR NO: 77-221 SYSTEM: ' Auxiliary Feedwater
~
COMPONENT: Auxiliary Feed Pump Turbine (AFPT) Speed Controller CHANGE, TEST OR EXPERIMENT: This FCR replaced the CW/ AUX and CCW/ AUX telays with relays and contacts that have adequate current ratings.
This FCR also replaced the dynamic braking resistor with a resistor with
. adequate wattage and voltage-rating.
This FCR and work was completed June 1, 1979.
REASON FOR CHANGE: The change was instituted due to the failures of the Couch /Deutsch relays used in the CW/ AUX and CCW/ AUX application.
Supplement 3 to FCR 77-221 involved the addition of a 50 ohm, 90 watt resistor in the AFPT control circuit. This resistor had been previously removed by the EIT for adverse environment.
SAFETY EVALUATION
SUMMARY
- The safety evaluation of the Couch relays for CW/ AUX and CCW/ AUX in disconnect switch cabinets CDE 12A-1 and CDF 12A-1 did not work satisfactorily for the following reasons:
- 1. DC interrupting rating of contacts were not capable to break the
_Bodine motor locked rotor current.
Contacts arced on opening, causing excessive wear.
- 2. The.Agastat relay is a more robust relay with larger contacts and much better DC interrupting rating.
- 3. The addition of a 50 ohm, 90 watt resistor in the AFPT control circuit. This additional resistor in JT2703 and JT2704 has been previously reviewed by the EIT for adverse environment.
These changes do not change the function of the AFPT speed control circuit.
Reliability of the circuit and speed control will be enhanced by this modification. This modification will not adversely affect the safety function of the Auxiliary Feedwater System.
~.
~
COMPLETED FACILITY CHANGE REQUEST FCR NO:
78-297 SYSTEM:. Reactor Coolant System COMPONENT: RCP Neutron Power Interlock CHANGE, TEST OR EXPERIMENT: This FCR is requesting approval of testing to obtain operational data on the restarting of the fourth Reactor Coolant Pump (RCP) above 22% power. This will confirm,the simulator results
' obtained by B&W. The basic test would be to establish reactor power at 50%
2% with three RCPs running and then start the fourth RCP.
This FCR requested relief from Section 15.2.6.1 of the FSAR (Page 15-47) which describes the 22% interlock.
This FCR test and request were completed February 28, 1979.
- REASON FOR CHANGE:
By' resetting the setpoint of RCP interlock to a higher setpoint, the fourth RCP could be started at a higher power level then the present power level.. B&W recommends this test be performed in SOM #378 dated June 7, 1978.
SAFETY EVALUATION SQKHARY: An analyst: of the data provided by the B&W simulator at 50% full power reveals that the highest and lowest pressure after the starting of the fourth RCP are 2192 psig and 2090 psig, respectively, which are well within the pressure trip setpoints.
If the trip setpoints are reached, the reactor will trip and any limits of the accident analysis in Chapter 15 of the FSAR will not be exceeded.
The 22% interlock is a non-nuclear safety related interlock and was introduced in the original Integrated Control System (ICS) to avoid the possibility of-frequent ' reactor coolant pressure trips.
Based on the analysis of the data, it is informed that starting a fourth RCP at 50% full power will not compromise nuclear safety and.does not involve an unreviewed safety question.
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m
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COMPLETED FACILITY CHANGE REQUEST
' FCR'NO: 80-278 SYSTEM: Safety Features Actuation System (SFAS)
COMPONENT: 'N/A CHANGE, TEST OR EXPERIMENT: This FCR changed the automatic transfer of the suctions of the decay heat and containment spray pumps from the BWST
' to the containment emergency sump to a manual transfer. Work was completed March 18, 1982.
REASON FOR CHANGE: This modification protects the decay heat and containment spray pumps from the possibility of damage due to an inadvertent transfer of pump suction to the dry containment emergency sump.
SAFETY EVALUATION
SUMMARY
- The safety function'of this transfer is to assure proper net positive suction to the decay heat and containment spray pumps during recirculation mode of operation.
Manual transfer from the Control Room will be performed when BWST level indication is between 49.5 inches and 96 inches.
Minimum level requirements for the BWST are met when transfer from BWST is performed within four minutes after BWST level has reached 96 inches.
This manual transfer provides the same safety function as the previous automatic transfer; hence, this does not involve an unreviewed safety question.
m
7=
- r
- COMPLETED FACILITY CHANGE REQUEST FCR NO:'83-046 SYSTEM: 'N/A COMPONENT: Borated Water Storage Tank (BWST)
- CHANGE, TEST OR EXPERIMENT: FCR 83-046 provided the addition of spray on foam insulation-to the exterior sides of the Borated Water Storage Tank (BWST).
To. protect the BWST from any direct contact with the foam insulation
- material, the tank had a protective base coating applied to its surface.
The BWST was also sealed and top coated. Work was completed October 5 1985.
REASON FOR CHANGE: This change is necessary due co stratification of temperature levels caused by tank heat losses, the uneven mixing'of water, and suspected icing on the inside of the BWST walls. Because of this, inaccurate temperature readings were received during cold weather.
Insulation added to the tank's external walls limits the tank heat losses such that the stratification of temperature levels are minimized and icing conditions are eliminated.
SAFETY EVALUATION
SUMMARY
- The safety function of the BWST is to provide a water source for the Emergency Core Cooling System and the Containment Spray System. The BWST temperature should be maintained between 50*F and 90*F.
The low temperature level listed in the Technical Specifications is-35'F.
However, a minimum of 50*F should be maintained based on a containment spray' initiation. Because this modification will not adversely affect'the integrity of the BWST or the operation of the.BWST from performing its design function, an unreviewed safety question does not exist.
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TOLEDO
%s EDISON February 10, 1986 Log No. KB86-0177 File: RR 2 (P-6-86-01)
Docket No. 50-346 License No. NPF-3 Mr. Norman Haller, Director Office of Management and Program Analysis U. S. Nuclear Regulatory Commission Washington, D.C.
20555
Dear Mr. Haller:
Monthly Operating Report, January 1986 Davis-Besse Nuclear Power Station Unit 1 Enclosed are ten copies of the Monthly Operating Report for Davis-Besse Nuclear Power Station Unit 1 for the month of January 1986.
If you have any questions, please feel free to contact Morteza Khazrai at (419) 249-5000, Extension 7290.
Yours truly, M'N Louis F. Storz Plant Manager Davis-Besse Nuclear Power Station LFS/MK/lj k Enclosures cc:
Mr. James G. Keppler, w/1 Regional Administrator, Region III Mr. James M. Taylor, Director, w/2 Office of Inspection and Enforcement Mr. Walt Rogers, w/1 g
NRC Resident Inspector IJK/002 y
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THE TOLEDO EDISON COMPANY EDISON PLAZA 300 MADISON AVENUE TOLEDO, OHIO 43652
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