ML20199H442
| ML20199H442 | |
| Person / Time | |
|---|---|
| Site: | San Onofre |
| Issue date: | 01/15/1999 |
| From: | Brockman K NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | Ray H SOUTHERN CALIFORNIA EDISON CO. |
| Shared Package | |
| ML20199H447 | List: |
| References | |
| 50-361-98-18, 50-362-98-18, EA-98-563, NUDOCS 9901250207 | |
| Download: ML20199H442 (6) | |
See also: IR 05000361/1998018
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UNITED STATES
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NUCLEAR REGULATORY COMMISSION
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REGION IV
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611 RYAN PLAZA DRIVE SUITE 400
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ARLINGTON, TEX AS 76011 8064
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JAN I 51999
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EA 98-563
Haiold B. Ray, Executive Vice President
Southern California Edison Co.
San Onofre Nuclear Generating Station
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P.O. Box 128
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San Clemente, Califomia 92674-0128
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SUBJECT: NRC INSPECTION REPORT 50-361/98-18; 50-362/98-18 AND NOTICE OF
VIOLATION
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Dear Mr. Ray:
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From November 9 through December 18,1998, a special inspection of the circumstances
surrounding the inadvertent inoperability of the Units 2 and 3 Train B emergency chilled water
system during August and September 1998 was conducted at your San Onofre Nuclear
' Generating Station, Units 2 and 3, reactor facility. The enclosed report presents the scope and
results of that inspection.
Based on the results of this inspection, the NRC has determined that a violation of NRC
requirements occurred. The violation is cited in the enclosed Notice of Violation (Notice) and
the circumstances surrounding it are described in detail in the enclosed inspection report. This
violation was of concem because operators ran the chiller lube oil pump with the compressor in
standby for a period longer than recommended, which resulted in a degraded chiller.
The NRC has concluded that information regarding the reason for the violation and the
corrective actions taken and planned to correct the violation and prevent recurrence is already
adequately addressed on the docket in the enclosed inspection report. Therefore, you are not
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required to respond to this letter unless the description therein does not accurately reflect your
corrective actions or your position. In that case, or if you choose to provide additional
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information, you should follow the instructions specified in the enclosed Notice.
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In addition, one apparent violation (EA 98-563) was identified and is being considered for
escalated enforcement action in accordance with the " General Statement of Policy and
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Procedure for NRC Enforcement Actions" (Enforcement Policy), NUREG-1600, Revision 1.
The apparent violation involved the inoperability of the Train B emergency chilled water system
in excess of the action times required by Technical Specification Limiting Condition for
Operation 3.7.10. The NRC reviewed your risk determination and recognized that it was
comprehensive, which war., a strength. However, the NRC interpreted the results of the risk
analysis differently and determined that the apparent violation was potentially risk significant.
The circumstances surrounding this apparent violation, the significance of the issue, and the
9901250207 990115
ADOCK 05000361
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Southern California Edison Co.
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need for lasting and effective corrective action were discussed with members of your staff at the
inspection exit meeting on December 18,1998. Because the criteria for granting identification
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and corrective action credit were met, the NRC determined that it may not be necessary to
conduct a predecisional enforcement conference to enable the NRC to make an enforcement
decision.
Before the NRC makes its enforcement decision, we are providing you an opportunity to either
(1) respond to the apparent violation addressed in this inspection report within 30 days of the
date of this letter or (2) request a predecisional enforcement conference. if a conference is
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held, it will be open for public observation. The NRC will also issue a press release to
announce the conference. Please contact Linda Smith at (817) 860-8137 within 7 days of the
date of this letter to notify the NRC of your intended response.
If you elect to respond to the apparent violation, your response should be clearly marked as a
Response to An Apparent Violation in Inspection Report No. 50-361; 362/98-18 and should
include: (1) the reason for the apparent violation or, if contested, the basis for disputing the
apparent violation, (2) the corrective steps that have been taken and the results achieved,
(3) the corrective steps that will be taken to avoid further violations, and (4) the date when full
compliance will be achieved. Your response should be submitted under oath or affirmation and
may reference or include previous docketed correspondence, if the correspondence adequately
addresses the required response. If an adequate response is not received within the time
specified or an extension of time has not been granted by the NRC, the NRC will proceed with
its enforcement decision or schedule a predecisional enforcement conference.
In addition, please be advised that the number and characterization of the apparent violation
described in the enclosed inspection report may change as a result of further NRC review. You
will be advised by separate correspondence of the results of our deliberations on this matter.
In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter, its
enclosures, and your response (if you choose to provide one) will be placed in the NRC Public
Document Room (PDR). To the extent possible, your response should not include any personal
privacy, proprietary, or safeguards information so that it can be placed in the PDR without
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redaction.
Should you have any questions concerning this inspection, we will be pleased to discuss them
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with you.
Sincerely,
Ken . Brockman, Director
Division of Reactor Projects
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Southern Califomia Edison Co.
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Docket Nos.: 50-361.
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50-362
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License Nos.: NPF-10 -
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NPF-15 -
Enclosures:
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2. NRC Inspection Report
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50-361/98-18;50-362/98-18
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ec w/ enclosures:
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Chairman, Board of Supervisors
County of San Diego
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1600 Pacific Highway, Room 335
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San Diego, Califomia 92101
Alan R. Watts, Esq.
Woodruff, Spradlin & Smart
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701 S. Parker St. Suite 7000
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Orange, California 92868-4720 ,
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Sherwin Harris, Resource Project Manager
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Public Utilities Department
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City of Riverside
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3900 Main Street
Riverside, California 92522
R. W. Krieger, Vice President
Southem Califomia Edison Company
San Onofre Nuclear Generating Station
. P.O. Box 128
' San Clemente, California 92674-0128
Stephen A. Woods, Senior Health Physicist
. Division of Drinking Water and
Environmental Management
Nuclear Emergency Response Program
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California Department of Health Services
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P.O. Box 942732, M/S 396
. Sacramento, California 94334-7320
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Mr. Michael R. Olson
Sr. Energy Administrator
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San Diego Gas & Electric Company
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P. O. Box 1831
San Diego, California 92112-4150
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Southern California Edison Co.
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Mr. Steve Hsu
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Radiological Health Branch
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State Department of Health Services
P.O. Box 942732
Sacramento, California 94234
Mayor
City of San Clemente
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100 Avenida Presidio
San Clemente, California 92672
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Mr. Truman Burns \\Mr. Robert Kinosian
California Public Utilities Commission
505 Van Ness, Rm. 4102
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San Francisco, California 94102
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