ML20199C568

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Submits Response to Comments Re NRC SALP Repts 50-361/97-99 & 50-362/97-99,dtd 970729.SALP Board Concluded That No Change to Maint Category Rating or Engineering Category Rating Was Appropriate
ML20199C568
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 01/26/1998
From: Merschoff E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Ray H
SOUTHERN CALIFORNIA EDISON CO.
References
50-361-97-99, 50-362-97-99, NUDOCS 9801300040
Download: ML20199C568 (9)


See also: IR 05000361/1997099

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AR LINGT ON. T E X AS 760118064

January 26,1998

Harold B. Ray, Executive Vice President

Southem California Edison Co.

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, Califomia 92674-0128

SUBJECT: RESPONSE TO COMMENTS RELATED TO NRC'S SYSTEMATIC

ASSESSMENT OF LICENSEE PERFORMANCE (SALP) REPORT 50-361/97

99;50 362/97 99

Dear Mr. Ray:

On August 26,1997, the Southern California Edison Company (SCE) provided docketed

comments in response to SALP Report 50 361/97-99; 50-362/97 99, dated July 29,1997, for the

San Onofre Nuclear Generating Station (SONGS), and requested that NRC reconsider the

Category 2 rating assigned to the engineering functional area. In the enclosure to this letter,

SCE indicated that performance in the engineering area during the past SALP period was

consistently and properly focused on safety and compliance to NRC regulations, and has

resulted in a superior level of performance. This conclusion was made on the basis of: 1) the

SALP process definition of Category 1; 2) the engineering strengths noted in the SALP report; 3)

an analysis of three performance issues noted in the engineering functional area discussion of

the SALP report; 4) engineering strengths noted in the NRC inspection reports that were issued

during the SALP period; and 5) other major engineering accomplishments.

The SALP Doard reconvened to consider the information provided in this letter, the Information

provided at the August 27,1997, SALP public meeting, the information provided relative to the

September 30,1997, predecisional enforcement conference involving inconel 600 nozzle

failures, and other relevant assessment data, in itu deliberations, the SALP Board also

considered whether the information provided by SCE affected its assessment of the

maintenance functional area because of the overlap of programs, processes, and activities

between the maintenance and engineering functional areas. .

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In the August 26,1997, letter, SCE provided its perspective on three performance issues

discussed in the engineering functional area of the SALP report. The three issues were the /

implementation of the Maintenance Rule, the implementation of the Improved Technical

Specification Program (ITS), and inconel 600 instrument nozzle failures.

With respect to the SALP report discussion of engineering support to maintenance (relative to

the Maintenance Rule), SCE indicated that: 1) there are two important elements for successful

implementation of the Maintenance Rule, which are an aggressive corrective action system and

consideration of risk insights; and 2) the SALP ,eport noted that SCE has an excellent corrective

actio program, and strong programs for utilizing probabilistic risk assessment and the Safety

Monitor. While these are two important elements, they are not the only critical attributes of

ensuring an acceptable Maintenance Rule program. As you know, the Maintenance Rule

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became effective during the SALP period in July 1996. Accordingly, processes and procedures

were developed in order to implement the rule. In the SALP Board's view, establishment of

effective performance monitoring criteria as part of the process is also an essential element of a

satisfactory program. The problems ioentified by the NRC during the SALP period involved the

inadequate establishment of performance monitoring criteria.

Southern California Edison Co. stated that the observations in the SALP report stemmed from

an assessment of the Maintenance Rule program performed by the SONGS Nuclear Oversight

organization, which may have been taken out of context. The SALP Board was aware of the

information in SCE's self assessment, which identified strengths and improvement areas.

However, the SALP Board assessed the information developed during an NRC indepenaent

inspection of various aspects of your Maintenance Rule pre jram. Two violations were issued as

a result of this inspection. While the NRC concluded that the violations were not indicative of a

programmatic breakdown, they were indicative of problems with the establishment of effective

monitoring enteria. A third apparent violation involving the failure to have goals and monitoring

requirements established for 13 SSCs was not cited because: 1) the undocumented goals for

these SSCs were to reattain their performance criteria; and 2) the existing corrective action

program was adequate to identify and correct the causes of failure. While no citation was

issued, the letter that transmitted the enforcement action noted that the reattainment of

performance criteria is not always appropriate, and specific goals for monitoring the

effectiveness of corrective actions were not established for the 13 affected SSCs. In response

to these violations, SCE indicated that a Maintenance Rule implementation Team, consisting of

inter-divisional middle managers, was formed to address project management concerns

associated with the SONGS Maintenance Rule Program.

We acknowledge that the SALP Board's primary concern related to prob' ems involving

acceptable performance monitoring criteria, rather than the failure to set goals and monitoring

requirements as noted in the SALP report. Accordingly, the SALP report has been revised to

better reflect this assessment. However, since SCE did not provide any information that was not

already assessed by the SALP Board, the SALP Board's original assessment in this area of

engineering performance remains unchanged.

With respect to the SALP report discussion involving project management of the ITS conversion

process, SCE indicated that: 1) SCE has been actively involved in ITS for 10 years; 2) site

management decided to limit engineering's involvement during the preparation and

implementation of the ITS on the basis of SCE's understanding of what the ITS was intended to

accomplish; 3) after engineering independently identified discrepancies, engineering led a

comprehnsive review of all Suweillance Pequirements, which the NRC noted to be superior;

4) corrective actions were comprehensive and thorough; 5) the review found several subtle and

longstanding deficiencies in surveillances; 6) nine of the 14 examples identified in Licensee

Event Report (LER) 2 97-001, Revision 3 were due to implementation errors unrelated to the

ITS; 7) there was no instance in which safety related equipment was not properly maintained or

was not capable of performing its intended safety function; and 8) this effort did not identify any

safety significant condition, and NRC Inspection Report 50 361/97-11; 50-362/9711 noted that

the examples identified by SCE had limited actual safety significance.

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The information summarized above is generally consistent with the SALP Board's assossment;

however, SONGS Engineering Assessment (SEA) Report 97-001, "Self Assessment

implementation of SONGS 2/3 Technical Specification Surveillance Requirements," documented

over 300 discrepancies between Technical Specification Surveillance Requirements and their

implementing procedures, rather than the several noted in the preceding discussion. Although,

NRC Inspection Report 50-361/9711; 50-362/9711 acknowledged the limited actual

significance of the individual examples, this conclusion was made on the basis of only a sample

of the more than 300 deficiencies, rather than a comprehensive review of all of the problems that

were documented in SEA 97-001 Further review of SEA 97-001 revealed a number of

potentially significant issues, which were not necessarily reportable to the NRC, and, therefore

not documented in LER 2 97-001. Also, SCE subsequently identified additional surveillance

implementation problems, which were not reported in GR 2 97-001 or not documented in SEA

97 001, such as the issue discussed in LER 2 97-016.

With respect to SALP report comment regarding SCE management missing an opportunity to

replace inconel 600 instrument nozzles, SCE indicated that the inspect and repair program for

reactor coolant system nozzle primary water stress corrosion cracking is consistent with industry

prctice, and SCE's Inconel 600 nozzle self assessment is an example of a self-critical approach

to providing the most comprehensive analysis possible to improve perfnrmance. Southern

California Edison Co. stated that NRC may have relied on this self assessment as confirmation

of its conclusions, and that SONGS Nuclear Oversight reports are self-critical and the context of

individual statements must be considered.

The SALP Board assesst.J the information that was developed as a result of NRC's

independent inspection of this matter, rather than the SCE's self-assesment report. However,

the SALP Board's assessment is fully consistent with SEA 97-002," Assessment of the

Inconel-600 Nozzle inspection & Replacement Program a. d Decision Process Leading to the

March 1997 Nozzle Failure in Unit 2," dated April 9,1997. This report concluded, in part, that

missed opportunities occurred,". . when a technical recommendation was changed from a

proactive nozzle replacement program to an inspect and-replace ap necessary strategy The

seconr1 missed opportunity occurred when a decision was made to continue with the inspect-

and replace as necessary strategy in lieu of a plan to perform anticipated repairs as well as

proactively replace some of the nozzles during the Cycle 9 refueling outage " While SCE

provided information regarding the bases for the decisions that were made, the SALP Board

concluded that no information was provided that would invalidate the SEA 97-002 conclusion

noted above. Accordingly, the SALP Board concluded that no change to this part of the

assessment was appropriate.

The enclosure of SCE's letter of August 26,1997, summarized a number of positive comments,

which were documented in NRC inspection reports that were issued during the SALP period. As

discussed in the Handbook to NRC Management Directive 8.6," Systematic Assessment of

Licensee Performance (SALP)," the SALP report is intended to document the Board's

assessment of the functional area in one or two pages, including a characterization of overall

safety performance for that functional area, it is not intended to detail all the inspection findings

that were documented in individualinspection reports during the SALP period. Rather the SALP

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Southem California Euson Co. 4-

report functional area discussions provide an overall assessment of performance in each of the

four functional areas, with examples discussed as appropriate. Inspection report findings

constitute a significant portion of the assessment data provided to the Board members in

preparation for the SALP Board meeting. Cc .antly, the SALP Board members had

available to them all the information docur,'er .n inspection reports, which included the

information summarized in the enclosure t SL.'s letter in balance with other information

j regarding performance of engineering activities at SONGS. Since this information was

assessed as part of the SALP process, the SALP Board concluded that SCE did not provide anv

new information in this renard.

With respect to other major engineering accomplishments that were summarized in the

August 26,1997, letter, several of these accomplishments were specifically noted as examples

of good performance in the SALP report in the appropriate functional area discussion. Many of

these accomplishments pertained to the resolution of hardware and other material condition

problems, which signific antly contributed to the Category 1 rating in the Maintenance functional

area.

On the basis of the preceding discussion, the SALP Board concluded that no change to

either the maintenance category rating or the engineering category rating was appropriate.

Specifically, overall safety performance was again assessed as superior in the maintenanca

functional area (Category 1) and Good in the engineering functional area (Category 2) ' i

reviewed this recommendation of the SALP Board and concur. Accordingly, the categ

ratings for the maintenance and engineering functional areas will remain as stated in SALP

Report 50 361/97 99; 50-362/97 99, dated July 29,1997,

in accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter and its

enclosure will be placed in the NRC Public Document Room.

Should you have any qu?stions or comments, I would be pleased to discuss them with you.

Sincerely,

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Ellis W. Mersghpff

Regional Adn9histrator

Docket Nos.: 50-361;50-362

License Nos.: NPF 10; NPF-15

Enclosure: Revised NRC SALP Report

50 361/97-99;50 362/97-99

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cc w/ enclosure:

. Chairman, Board of Supervisors

4 County of San Diego

1600 Pacific Highway, Room 335

San Diego, California 92101

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i Alan R. Watts, Esq.

Woodruff, Spredlin & Smart

701 S. Parker St. Suite 7000

Orange, California 92868-4720 ,

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Sherwin Harris, Resource Project Manager

Public Utilities Department

City of Riverside

3900 Main Street

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Riverside, California 92522

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R. W. Krieger, Vice President

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, Califomia 92674-0128

Stephen A. Woods, Senior Health Physicist

Division of Drinking Water and

Environmental Management-

Nuclear Emergency Response Program

California Department of Health Services

P.O. Box 942732, M/S 996

Sacramento, California 94334 7320

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Mr. Gary D. Cotton, Sr. Vice President

Energy Supply

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San Diego Gas & Electric Company ,

P,0. Box 1831

San Diego, California 92112-4150

'- Mr. Steve Hsu

-

Radiological Health Branch

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State Department of Health Services

P.0, Box 942732

Sacramento, California 94234

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Mr. Truman BumsWr, Robert Kinosian

Califomia Public Utilities Commission

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DOCUMENT NAME: G:HOWELL/SONGSSAL. REB *Previously concurred

To receive copy of document, indicate in box:"C" = Copy without enclosures *E" = Copy with enclosures "N" = No copy

D:DRS E NRR E WCFO E RA E

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1/23/98 1/21/98 1/20/98 1/25/98

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[ AR LINoToN, T E X AS 760118064

July 29,1997

Harold B. Ray, Executive Vice President -

Snuthern California Edison Co.

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, California 92674-0128-

SUBJECT: SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP)

REPORT 50-361/97 99;50-362/97 99

Dear Mr. Ray:

Enclosed for your review is the SALP report for the San Onofre Nuclear Ganerating Station,

Units 2 and 3 for the period of December 31,1995, through July 5,1997. A public ,

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' meeting to discuss this report with you and your staff has been scheduled for "

10 a.m. (PDT) on August 27,1997, at the Training and Education Center at the San

Onofre facility. During this meeting you are encouraged and expected to candidly

comment on our report. Although this meeting is a forum between Southern California

Edison and the NRC,it will be open to observation by members of the public and other

interested parties.

In accordance with NRC policy, I have reviewed the recommendations of the SALP Bocrd -

and concur with the ratings and views. The Maintenance and Plant Support functional

areas were assigned Category 1 ratings, reflecting superior safety performance, and the

Plant Operations and Engineering areas were assigned Category 2 ratings, reflecting overall

good safety performance.

Overall performance in ihe area of Plant Operations was good, with strong performance

noted during plant evolutions and improved performance noted during outages. Instances

of inconsistent performance related to operator attentiveness, procedure implementation,

communications, and control of field activities were noted.

In the Maintenance area, safety performan::e improved to a superior level due to

improvement in the overall material condition of the station, reduction in the problem

identification threshold, and the conduct of maintenance activities in the field. We

encourage your continued efforts to improve the plant material condition and to improve

performance in the areas of surveillance testing and welding.

Performance in the area of Engineering was good. Strong performance was noted in the

areas of corrective actions, self-assessments, and outage support, although inconsistencies

were noted with management oversight and quality of engineering support to certain

activities. Particularly strong performance was noted in the resolution of the degraced

steam generator tube supports (i.e., eggcrates) in Unit 3.

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Overall performance in the Plant Support area remained superior. Radiological protection ,

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. during.the steam generator chemical cleanirig activities was strong.

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Safety assessment and quality verification activities continue to be a strength at San

Onofre. You have demonstrated strong self assessment performance by your line

organizations and the Nuclear Oversight organization,

in accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this let+er-

and its enclosures will be placed in the NRC Public Document Room.

Should you have any questions or comments, I would be pleased to discuss them with

you. While no written response is required, you may provide written comments within

30 days of the public SALP meeting.

Sincerely, l

Original signed by

//s// i

Ellis W. Merschoff

Regional Administrator

- Docket Nos.: 50-361

50 362

License Nos.: NPF-10 - '

NPF 15

Enclosure:

NRC SALP Report

50-361/97 99:50 362/97-99

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cc w/ enclosure:

Chairman, Board of Supervisors

County of San Diego

1600 Pacific Highway, Room 335

San Diego, California 92101

Alan R. Watts, Esq.

Woodruff, Spradlin & Smart

701 S. Parker St. Suite 7000

Orange, California 92868-4720

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Sherwin Harris, Resource Project Manager

Public Utilities Department

City of Riverside

3900 Main Street

Riverside, California 92522

R. W. Krieger, Vice President

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, California 92674-0128

Dr. Harvey Collins, Chief

Division of Drinking Water and

Environmental Management

California Department of Health Services

P.O. Box 942732

Sacramento, California 94234-7320

Terry Winter, Manager

Power Operations .

.

San Diego Gas & Electric Company

P.O. Box 1831

San Diego, California 92112

Mr. Steve Hsu

Radiological Health Branch

State Department of Health Services

'- P.O. Box 942732'

Sacramento, California 94234

'

Mayor

City of San Clemente

100 Avenida Presidio

San Clemente, California 92672

Mr. Truman Burns \Mr. Robert Kinosian

California Public Utilities Commission

505 Van Ness, Rm. 4102

San Francisco, California 94102

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SAN ONOFRE NUCLEAR GENERATING STATION

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

Report 50-361/97 99; 50-362/97 99

l. BACKGROUND

The SALP Board convened on July 9,1997, to assess the nuclear safety performance of

San Onofre Nuclear Generating Station for the period of December 31,1995, through

July 5,1997. The Board was conducted in accordance with Management Directive 8.6,

" Systematic Assessment of Licensee Performance." The Board members included:

K. E. Perkins (Board Chairperson), Director, Walnut Creek Field Office, Region IV:

A. T. Howell, Director, Division of Reactor Safety, Region IV; and J. W. Roe, Director,

Division of Reactor Projects ill/IV, Office of Nuclear Reactor Regulation. This assessment

was reviewed and approved by the Regional Administrator.

Functional Areas and Ratings:

Current Previous

Plant Operations 2 2

Maintenance 1 2

Engineering 2 1

Plant Support 1 1

II. PLANT OPERATIONS

Overall performance in the Plant Operations area during this assessment period was good.

Operations performance during outages improved during this assessment period; however,

performance throughout the period was inconsistent. Management involvement in control

room oversight and programs for operations were generally excellent. Operators generally

performed well during transient and routine operations; although, they occasionally

demonstrated weakness in attentiveness, procedure implementation, communications, and

control of evolutions involving important field activities.

Management involvement in control room oversight was generally excellent, including

effective oversight of important activities. The strong management coverage of control

room activities during the refueling outages and reduced reactor coolant level conditions

contributed significantly to improved performance during the outages. Although

management oversight of operations activities was improved, control room supervisory

oversight of plant activities and performance by control room operators did not always

meet management's written expectations for conduct of operations. The performance

problems included exceeding the pressurizer cooldown limit and the inadvertent transfer of

refueling storage tank water to the reactor coolant system in Unit 2. Management

consistently took effective corrective actions for identified problems.

Programs for operations were generally excellent, including the programs for conduct of

operations and minimizing operator work-arounds. However, procedure quality and usage

problems were observed. Some procedures were very complex, contained transition and

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component identification errors, or were inconsistent with other guidance. - Procedere

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changes continue to be numerousi_ indicating a need for improved procedures; although,

the backlog of changes was being effectively managed. Weaknesses in procedure detail

contributed to the failure to properly position a reactor vent valve. in addition, weaknesses

in operation's verification"and validation of the Improved Technical Specifications (TS)

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contributed to problems discussed in the Engineering functional area. The corrective

actions taken to resolve these deficiencies were thorough and effective.-

The conduct of operations was generally good. Planning and preparation for most

operational activities was good. Operators generally followed plant procedures during

normal operations; however, operators occasionally exhibited weakness in attention to

detail. Examples of this include setting the automatic boric acid fiow rate low, the  ;

mispositioning of several valves, and not verifying offsite power sources when an

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emergency diesel generator was inoperable. There were no reactor trips or other -

significant events and operators generally performed well during routine power operations.

Operation's performance of activities during outages was generally improved from the

previous period. Communications were generally good; although, they occasionally did not

conform to management expectations. Communications improved after management

attention to this area increased. Operations management consistently ensured that

appropriate corrective actions were taken in response to material deficiencies.and

procedural problems _ Plant and control board monitoring by operators was generally good;..

mithough, isolated lapses did occur.

- The operators performed'well during simulator training exercises. Some examples of weak

operator knowledge and skills were observed; including the failure to recognize a change in '  !

Unit 3 control element assembly position resulting in the upper electricallimit lights not lit

- and the failure to know the Unit 2 shutdown cooling flow limit applicable to the procedure

being execuud.-  !

Licensee selfassessments continued to be a program strength. The use of metrics to

critically self assess performance'and to provide feedback on the extent to which

management expectations were met was a strength'. The assessment of valve lineup

performance problems, performed by the Nuclear Oversight Division, was excellent.

The performance rating in the area of Plant' Operations is Category 2.

Ill. MAINTENANCE

Overall performance in the Maintenance area improved to a superior level. The quality of

existing programs was maintained at a high level. While maintenance procedures were of

very good quality, there were some surveillance problems that stemmed from procedural

weaknesses. The conduct of maintenance activities was excellent, while the conduct of

surveillance activities was good. The overall material condition of the plant improved

throughout the assessment period. Self-critical assessments and root cause evaluations

contributed to improvement in this area.

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The quality of existing programs was maintained at a high level. For example, the steam

generator inservice inspection program was a noteworthy strength. However, as

discussed in the Engineering functional area, weak engineering oversight and support

resulted in the development of inadequate Maintenance Rule performance criteria for

structures, systems, or components and in the improperly scoped review of the improved

TS surveillance requirements.

Maintenance procedures were very good overall and the licensee initiated a comprehensive

plan to further enhance them. However, there were a number of surveillance

implementation problems, stemming in part from procedural weaknesses. Some of these

problems were attributed to procedural validation and verification weaknesses associated

with the implementation of the improved TS Licensee actions to' correct these

deficiencies were comprehensive.

The overall conduct of maintenance was excellent. Maintenance activities were well

planned and conducted in accordance with procedures by knowledgeable personnel.

Supervisors were frequently observed in the field providing oversight and guidance at job

sites. The performance of welding activities improved; however, some implementation

problems continued to be identified.

Surveillance and testing performance was good. Although not individually significant,

there were a number of surveillance implementation problems that occurred throughout the

assessment period. As discussed in the Operations functional area, many of these

problems were attributed to control room operator inattention and operations surveillance

procedure weaknesses.

The licensee continued to demonstrate a conservative approach to outage planning and

management. The work scope of the two 1997 refueling outages was well defined, and

the outage schedules appropriately incorporated risk-informed considerations. However,

reactor coolant system instrument nozzle leaks and other emergent hardware problems

caused significant unplanned delays during both 1997 refueling outages.

The material condition of the plant was improved throughout the assessment period

because of plant preservation and maintenance backlog reduction activities. There were no

reactor trips that were caused by hardware problems.

Efforts to encourage problem identification resulted in a significant reduction in the problem

identification threshold. Comprehensive, performance-based assessments were conducted

throughout the assessment period. The quality of root cause analyses, a strength noted in

the previous SALP, was maintained at a high level.

The performance rating in the area of Maintenance is Category 1.

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IV. ENGINEERING

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Performance in the Engineering area was good during this assessment period. Strong i

performance was noted ira engineering support to outages, self assessments, and corrective

action development and implementation. Management did not always provide the

appropriate level of oversight for engineering activities. Weaknesses were noted in the

support to maintenance and in the translation of design basis requirements into appropriate

operational requirements and surveillances. Superior performance was noted in the

resolution of complex engineering issues and in self assessment and corrective action

efforts,

Support to Maintenance and Operations during outage activities was excellent overall, with

timely evaluation of emerging issues and good technical support for planned activities. The

use of the safety monitor to plan maintenance activities optimized plant safety, as did the

( detailed risk assessments performed for each refueling outage. However, Engineering

support to Maintenance lacked rigor and thoroughness for one significant program, which

resulted in a failure to develop adequate performance monitoring criteria in accordance with

the Maintenance Rule.

The capability of the engineering organization to conduct complex engineering activities

continued to be superior. The efforts to resolve the degraded steam generator tube

supports (i.e., eggerates) in the Unit 3 steam generators were excellent. A comprehensive

strategy was developed to identify and address all relevant issues, and extensive technical

support for meetings with the NRC provided timely and accurate responses to staff

questions. Also, Engineering took a leadership role in identifying and resolving the

problems associated with the coaxial cable for the containment high range radiation

monitors.

Management oversight of engineering activities was inconsistent. Oversight weaknesses

resulted in inadequate control of some projects. The project management of the improved

TS conversion process did not properly scope the effort and engineering support was not

sufficiently rigorous to ensure all surveillance requirements were properly verified by the

implementing surveillance procedures. This resulted in a number of design basis

requirements that were not translated into appropriate operational requirements and

surveillances and in missed opportunities to identify severallong-standing surveillance

procedure deficiencies. Also, management missed an opportunity to replace inconel 600

instrument nozzles with a history of susceptibility to primary water stress corrosion

cracking. Conservative decisions related to plant safety included a commitment to perform

midcycle inspections of the steam generators in both units and the decision to request staff

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approval to add an inter-unit 4.16 kV bus cross-tie.

Self-assessment and corrective action activities continued to be superior, After discovery

of errors in the implementing procedures for the improved TS, a thorough review of eveiy

surveillance requirement and associated implementing procedure was performed. Other

notable activities during this assessment period included a detailed review of the Updated

Final Safety Analysis Report and a number of comprehensive root cause assessments of

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equipment malfunctions. The Independent Safety Engineering Group performed excellent

root cause assessments of industry events.

The performance rating in the area of Engineering is Category 2.

V. PLANT SUPPORT

Performance in the Plant Support functional area was maintained at a superior level

Performance in radiological protection was strong. Emergency preparedness effectiveness

remained a noteworthy strength. In the security area, overall performance was very good

and was improving during the latter part of the assessment period. The fire protection

program was effectively maintained and implemented. Housekeeping improved throughout

the assessment period. Audits and self-assessments were self-critical and performance-

based, and corrective actions were thorough and timely.

Performance in the radiological protection area continued at a high level. A comprehensive

as-low as reasonably-achievable program was implemented and functioned effectively to

maintain radiation exposures at a low level. Shutdown chemistry controls contributed to

exposure reduction results. Collective radiation exposure was less than the national

average during the assessment period. Good training was provided in all radiological

control areas and technical staff qua'ifications were a strength. Consequently, technical

reviews and analysis of information were excellent. Performance by radiation protection

technicians was good; however, a few problems were noted in the implementation of some

program areas. Strong programs were maintained in the solid weste management,

transportation of radioactive materials, radiological environmental monitoring, and

meteorological monitoring areas.

Radiochemistry and secondary chemistry programs were also effectively implemented.

There as a marked improvement in the reduction of radioactivity released in gaseous

efflut..ts between 1994 and 1996. Chemical cleaning of the Units 2 and 3 steam

generators resulted in the removal of large quantities of sludge and tube deposits.

Performance in the emergency preparedness area continued to be a program strength.

Operating crews performed in an excellent manner during simulator walkthroughs.

Emergency classifications, offsite agency notifications, and protective action

recommendation formulation were correct and timely. Internal communications and

procedural usage were effective. Emergency response facilities and equipment were j

operationally maintained; however, the program for control of emergency lighting permitted

some safe shutdown emergency lighting to become ineffective.

Overall performance in the security area remained very good and improvements were noted

during the latter part of the assessment period. Program strengths included records and

reports, security plan changes, management support, security organization, training and

qualifications, and access authorization. Some isolated problems involving security

procedures, the land vehicle barrier system, lock and key control, and protected area

barriers were ioentified.

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The fire protection program continued to be effectively implemented. The dedicated,

on-site fire department provided a strong, well trained, and effective fire response

capability. Systems were appropriately tested and well maintained. A fire protection

innovation team maintenance program was initiated to reduce the fire protection

maintenance backlog.

Overall, plant housekeeping was welt maintained and continued to improve throughout the

assessment period. Radiological housekeeping was good, with some minor exceptions

noted.

Self assessment activities were effective at identifying problems, and corrective actions

were comprehensive and timely. In one instance, the quality assurance audit of the

security program was not of sufficient scope.

The performance rating in the area of Plant Support is Category 1.

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