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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20212J9251999-10-0101 October 1999 Safety Evaluation Accepting Licensee Relief Request IWE-3 for Second 10-year ISI for Plant ML20211N2611999-09-0808 September 1999 Safety Evaluation Concluding That Proposed Irradiation of Fuel Rods Beyond Current Lead Rod Burnup Limit & Clarification of Terminology with Respect to Reconstituted Fuel Assemblies Acceptable ML20211J2421999-08-31031 August 1999 Safety Evaluation Supporting Removal of Augmented Insp Program on RCS Bypass Lines from Licensing Basis of North Anna,Units 1 & 2 ML20211J2561999-08-31031 August 1999 Safety Evaluation Accepting Elimination of Augmented ISI Program for Pressurizer Spray Lines at North Anna Unit 2 ML20210T0791999-08-13013 August 1999 Safety Evaluation Concluding That Revised Withdrawal Schedules for North Anna Units 1 & 2 Satisfy Requirements of App H to 10CFR50 & Therefore Acceptable ML20206L4831999-05-10010 May 1999 SER Accepting Request to Delay Submitting Plant,Unit 1 Class 1 Piping ISI Program for Third Insp Interval Until 010430, to Permit Development of Risk Informed ISI Program for Class 1 Piping ML20205S0391999-04-21021 April 1999 SER Accepting Request for Relief IWE5,per 10CFR50.55a(a)(3) & Proposed Alternatives for IWE2,IWE4,IWE6 & IWL2 Authorized Per 10CFR50.55a(a)(3)(ii) ML20198H9541998-12-0303 December 1998 Safety Evaluation Authorizing Proposed Alternative for Remainder of Second 10-yr Insp Interval for Plant ML20196G1381998-11-0303 November 1998 Safety Evaluation Authorizing Rev to Relief Request NDE-32 for Remainder of Second 10-yr Insp Interval for Each Unit ML20236K5531998-07-0707 July 1998 SER Accepting Request for Change in ISI Commitment on Protection Against Pipe Breaks Outside Containment ML20248C8831998-05-29029 May 1998 SER Accepting Alternatives Proposed by Licensee for Use of Code Case N-535,pursuant to 10CFRa(a)(3)(i) in ASME Section XI Inservice Insp Program ML20217B5321998-04-20020 April 1998 Safety Evaluation Supporting Proposed Alternative to ASME Code for Surface Exam of Seal Welds on Threaded Caps for Plant Reactor Vessel Head Penetrations for part-length CRDMs ML20216E8801998-03-0606 March 1998 Safety Evaluation Authorizing Licensee Request for Relief from ASME Code Requirements,Paragraph IWA-2400(c) (Summer Edition W/Summer 1983 Addenda),For Upcoming Naps,Unit 1 Outage,Per 10CFR50.55a(a)(3)(ii) ML20199J6431998-02-0202 February 1998 Safety Evaluation Approving Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Code Class 3 SW Piping for North Anna,Unit 1,as Submitted in ISI Relief Request NDE-46 on 971218 ML20198S7571998-01-15015 January 1998 Safety Evaluation Accepting Licensee Request for Approval to Repair Flaws IAW GL-90-05 for ASME Code Class 3 Svc Water Piping ML20198H5541997-12-29029 December 1997 SER Accepting Request for Approval of ASME Case N-498,rev 1, as an Alternative to Required Hydrostatic Pressure Test for Plant,Unit 2 ML20197K1541997-12-18018 December 1997 SER Granting Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Code Class 3 Service Water Piping for North Anna Power Station,Per Util 970919 Submittal ML20199L0501997-11-24024 November 1997 SER Accepting Inservice Insp Program Relief Request NDE-32 ML20199E4971997-11-14014 November 1997 Safety Evaluation Authorizing Proposed Alternative of Licensee Relief Requests NDE-35 & NDE-37,for Plant,Units 1 & 2 During Second 10 Yr Interval ML20217E0701997-09-24024 September 1997 Safety Evaluation Granting Licensee ASME Section XI Relief Request NDE-33 at Plant,Unit 1 ML20217E2411997-09-24024 September 1997 SER Accepting Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Code Class 3 Service Water Piping,Virginia Electric & Power Co,North Anna Power Station,Unit 1 ML20217E1871997-09-24024 September 1997 SER Approving Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Code Class 3 Service Water Piping,Virginia Electric & Power Co,North Anna Power Station,Units 1 & 2 ML20149L2001997-07-29029 July 1997 SER Granting Requests for Relief NDE-33,34 & 35 Re ISI Program,Per 10CFR50.55a(g)(6)(i) ML20149F1321997-07-17017 July 1997 Safety Evaluation Supporting Amends 205 & 186 to Licenses NPF-4 & NPF-7,respectively ML20148H1971997-06-0404 June 1997 Safety Evaluation Granting Licensee Relief Request NDE-31 Related to Inservice Insp Program ML20140F4811997-04-30030 April 1997 Safety Evaluation Accepting Licensee 951207 Proposed Alternative in Request for Relief SPT-16 Re Second 10-yr Interval Inservice Insp Program for Unit 2 ML20133G1561997-01-10010 January 1997 Safety Evaluation Accepting Second 10-year Relief Requests for Relief Numbers NDE-27,NDE-28 & NDE-29 ML20133G1911997-01-10010 January 1997 Safety Evaluation Accepting Second 10-year Interval Inservice Insp Plan Relief Request NDE-30 ML20138G1931996-10-16016 October 1996 SER Accepting Second 10-year Interval Inservice Insp Plan Request for Relief SPT-14,rev 1 Virginia Electric & Power Co North Anna Power Station,Unit 2 ML20128P1701996-10-10010 October 1996 Safety Evaluation Supporting Second 10-year Interval Inservice Insp Program Plan Requests for Relief NDE-23 Through NDE-30 for Plant Unit 2 ML20128F5981996-10-0101 October 1996 Safety Evaluation Authorizing Licensee Proposed Alternative to Examine Terminal End Welds on Lower Regenerative Heat Exchanger sub-vessels,per 10CFR50.55a(a)(3)(ii) ML20059M1181993-11-15015 November 1993 SER Accepting Category 3 Qualification in Lieu of Category 2 for Pressure Monitoring Instrumentation ML20057C0401993-09-17017 September 1993 Safety Evaluation Re Inservice Testting Program Requests for Relief ML20126C1221992-12-0404 December 1992 Safety Evaluation Authorizing Util to Continue Current Test Method for Interim Period,Based on Util Plans to Develop & Implement Use of non-intrusive Testing Techniques for Check Valves Following 1993 Unit 2 Refueling Outage ML20125B7251992-12-0303 December 1992 Safety Evaluation Granting Temporary Exemptions from Requirements of GDC-2 & 10CFR50.49 for Phase 1,stage 1 of Svc Water Sys Restoration Project ML20062C4441990-10-18018 October 1990 SER Re Station Blackout.Plant Does Not Conform W/Station Blackout Rule ML20247C2091989-09-0707 September 1989 Safety Evaluation Accepting Util 890512 Response to IE Bulletin 80-11, Masonry Wall Design ML20245J8401989-06-28028 June 1989 Safety Evaluation Supporting Restart of Unit 1 & Util 890528 Response to NRC Bulletin 89-001, Failure of Westinghouse Mechanical Steam Generator Tube Plugs ML20195J0061988-11-29029 November 1988 Safety Evaluation Supporting Licensee Responses to NRC Bulletin 88-002, Rapidly Propagating Fatigue Cracks in Steam Generator Tubes, Subj to Util Adopting Addl Administrative Controls ML20207F1391988-08-12012 August 1988 Safety Evaluation Supporting Util Responses to IE Bulletin 80-11, Masonry Wall Design, W/Exception of One Open Item ML20196G9081988-03-0404 March 1988 SER Re Util 831104 & 850208 Responses to Generic Ltr 83-28, Item 2.2.1, Equipment Classification (Program for All Safety-Related Components. Responses Acceptable ML20149J9301988-02-18018 February 1988 Safety Evaluation Re Relief Request 6 of Inservice Testing Program for Pumps & Valves ML20154E8221987-12-11011 December 1987 Safety Evaluation Supporting Util Identification of Major Causal Factors Leading to 870715 Tube Rupture Event & Adequacy of Diagnostic & Corrective Measures Implemented in Order to Preclude Similar Events ML20237B5981987-12-11011 December 1987 Safety Evaluation Accepting Util 870915 & 0925 Responses to Steam Generator Tube Rupture on 870715.Util Has Adequately Demonstrated That Primary Failure Mechanism Leading to Event Caused by flow-induced Vibration ML20236F4971987-10-23023 October 1987 Safety Evaluation Re Util 870925 Request for Approval of Steam Generator Downcomer Flow Resistance Plate Mods & Increase in Calculated Offsite Dose Per 10CFR50.59.Mods Acceptable ML20235U8811987-07-13013 July 1987 Safety Evaluation Supporting Request for Relief from Certain Exam & Hydrostatic Test Requirements of ASME Code ML20213G8081987-05-11011 May 1987 SER Re Util 850208 Response to Generic Ltr 83-28,Item 2.1 (Part 2), Vendor Interface Programs (Reactor Trip Sys Components. Program Acceptable ML20212K5111987-02-27027 February 1987 SER Accepting Licensee 831104 Response to Generic Ltr 83-28, Item 4.5.2, Reactor Trip Sys Reliability,On-Line Testing ML20207Q0651987-01-0909 January 1987 Safety Evaluation Denying Util 850401 Request to Reduce Number of Thimbles Required for Monthly Surveillance Flux Mapping ML20215D0811986-09-30030 September 1986 Safety Evaluation Granting Util 860613 Request for Relief from Inservice Hydrostatic Test Requirements for Svc Water Spray Sys 1999-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N9281999-10-20020 October 1999 Special Rept:On 991003,PZR PORV Actuation Mitigated RCS low- Temp Overpressure Transient.Caused by a RCP Facilitating Sweeping of Entrained Air Out of RCS Loops.Operating Procedure 2-OP-5.1 Will Be Revised ML20217H3631999-10-14014 October 1999 Rev 0 to COLR for North Anna 2 Cycle 14 Pattern Su ML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML20212J9251999-10-0101 October 1999 Safety Evaluation Accepting Licensee Relief Request IWE-3 for Second 10-year ISI for Plant ML20217D6851999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for North Anna Power Station,Units 1 & 2.With ML20211N2611999-09-0808 September 1999 Safety Evaluation Concluding That Proposed Irradiation of Fuel Rods Beyond Current Lead Rod Burnup Limit & Clarification of Terminology with Respect to Reconstituted Fuel Assemblies Acceptable ML20211J2561999-08-31031 August 1999 Safety Evaluation Accepting Elimination of Augmented ISI Program for Pressurizer Spray Lines at North Anna Unit 2 ML20216E5011999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Naps,Units 1 & 2. with ML20211J2421999-08-31031 August 1999 Safety Evaluation Supporting Removal of Augmented Insp Program on RCS Bypass Lines from Licensing Basis of North Anna,Units 1 & 2 ML20210T0791999-08-13013 August 1999 Safety Evaluation Concluding That Revised Withdrawal Schedules for North Anna Units 1 & 2 Satisfy Requirements of App H to 10CFR50 & Therefore Acceptable ML20210S1411999-07-31031 July 1999 Monthly Operating Repts for July 1999 for North Anna Power Station.With ML20210Q9931999-07-31031 July 1999 Rev 1 to COLR for North Anna Power Station,Unit 2 Cycle 13 Pattern Ud ML20209E5641999-06-30030 June 1999 Monthly Operating Repts for June 1999 for North Anna Power Stations,Units 1 & 2.With ML20195G1901999-05-31031 May 1999 Monthly Operating Rept for May 1999 for NAPS Units 1 & 2. with ML20206L4831999-05-10010 May 1999 SER Accepting Request to Delay Submitting Plant,Unit 1 Class 1 Piping ISI Program for Third Insp Interval Until 010430, to Permit Development of Risk Informed ISI Program for Class 1 Piping ML20206Q6671999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for North Anna Power Station,Units 1 & 2.With ML20205S0391999-04-21021 April 1999 SER Accepting Request for Relief IWE5,per 10CFR50.55a(a)(3) & Proposed Alternatives for IWE2,IWE4,IWE6 & IWL2 Authorized Per 10CFR50.55a(a)(3)(ii) ML20205K3041999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for North Anna Power Station,Units 1 & 2.With ML20207K5921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for North Anna Power Station,Units 1 & 2.With ML20207E1731999-02-18018 February 1999 Informs Commission of Status of Preparations of IAEA Osart Mission to North Anna Nuclear Power Plant Early Next Year ML20205A0241998-12-31031 December 1998 Summary of Facility Changes,Tests & Experiments,Including Summary of SEs Implemented at Plant During 1998,per 10CFR50.59(b)(2).With ML20199C8781998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for North Anna Power Station,Units 1 & 2.With ML20198H9541998-12-0303 December 1998 Safety Evaluation Authorizing Proposed Alternative for Remainder of Second 10-yr Insp Interval for Plant ML20198J5561998-12-0303 December 1998 ISI Summary Rept for North Anna Power Station,Unit 1 1998 Refueling Outage Owner Rept for Inservice Insps ML20197G8551998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for North Anna Power Station,Units 1 & 2.With ML20196G1381998-11-0303 November 1998 Safety Evaluation Authorizing Rev to Relief Request NDE-32 for Remainder of Second 10-yr Insp Interval for Each Unit ML20195D0571998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for North Anna Power Station,Units 1 & 2.With ML20154L0691998-10-14014 October 1998 COLR for North Anna Power Station Unit 1 Cycle 14 Pattern Xy ML20155J6911998-10-0909 October 1998 Staff Response to Tasking Memorandum & Stakeholder Concerns ML20154H4001998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for North Anna Power Station,Units 1 & 2.With ML20151X8011998-09-10010 September 1998 Special Rept:On 980622,groundwater Level at Piezometer P-22 Was Again Noted to Be Above Max Water Level by 0.71 Feet. Increased Frequency of Piezometer Monitoring & Installed Addl Piezometers at Toe of Slope Along Southwest Section ML20151W4711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for North Anna Power Station Units 1 & 2.With ML20237A4341998-07-31031 July 1998 Monthly Operating Repts for July 1998 for North Anna Power Station,Units 1 & 2 ML20236V1251998-07-14014 July 1998 ISI Summary Rept for Naps,Unit 2,1998 Refueling Outage Owners Rept of Isis ML20236K5531998-07-0707 July 1998 SER Accepting Request for Change in ISI Commitment on Protection Against Pipe Breaks Outside Containment ML20236M3381998-06-30030 June 1998 Monthly Operating Repts for June 1998 for North Anna Power Station,Units 1 & 2 ML20248M1011998-05-31031 May 1998 Monthly Operating Repts for May 1998 for North Anna Power Station,Units 1 & 2 ML20248C8831998-05-29029 May 1998 SER Accepting Alternatives Proposed by Licensee for Use of Code Case N-535,pursuant to 10CFRa(a)(3)(i) in ASME Section XI Inservice Insp Program ML20247K9281998-05-15015 May 1998 Special Rept:On 980428,letdown PCV Exhibited Slow Response When C RCP Was Started.Cause to Be Determined.Review of Operating Procedure Will Be Performed to Determine If Enhancements Are Necessary ML20216A8971998-05-0606 May 1998 Rev 0 to Cycle 13 Pattern Ud COLR for North Anna Unit 2 ML20247F4441998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for North Anna Power Station,Units 1 & 2 ML20217B5321998-04-20020 April 1998 Safety Evaluation Supporting Proposed Alternative to ASME Code for Surface Exam of Seal Welds on Threaded Caps for Plant Reactor Vessel Head Penetrations for part-length CRDMs ML20217H9611998-04-0707 April 1998 Special Rept:On 980216,groundwater Level at Piezometer P-22, Again Noted to Be Above Max Water Level by 0.41 Feet.Design Package for Installation of Addl Standpipe Piezometers at Toe of Slope Southeast Section,Developed ML20216B1891998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for North Anna Power Station,Units 1 & 2 ML20216E8801998-03-0606 March 1998 Safety Evaluation Authorizing Licensee Request for Relief from ASME Code Requirements,Paragraph IWA-2400(c) (Summer Edition W/Summer 1983 Addenda),For Upcoming Naps,Unit 1 Outage,Per 10CFR50.55a(a)(3)(ii) ML20216E2561998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for North Anna Power Station,Units 1 & 2 ML20199J6431998-02-0202 February 1998 Safety Evaluation Approving Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Code Class 3 SW Piping for North Anna,Unit 1,as Submitted in ISI Relief Request NDE-46 on 971218 ML20202D5811998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for North Anna Power Station,Units 1 & 2 ML20198S7571998-01-15015 January 1998 Safety Evaluation Accepting Licensee Request for Approval to Repair Flaws IAW GL-90-05 for ASME Code Class 3 Svc Water Piping ML20198P1351997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for North Anna Power Station,Units 1 & 2 1999-09-08
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! o NUCLEAR REGULATORY COMMISSION D E WASH WGTON, D. C. 20666 ENCLOSURE SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION VIRGINIA ELECTRIC AND POWER COMPANY CLOSE0VT OF BULLETIN 88-02 ISSUES
- 1. INTRODUCTION By letter dated March 24, 1988 (Reference 1), Virginia Electric and Power Company (the licensee) submitted its response to NRC Bulletin 88-02, "Rapidly Propagating Fatigue Cracks in Steam Generator Tubes."Bulletin 88-02 requested that licensees for plants with Westinghouse steam generators employing carbon steel support plates take certain actions (specified in tha bulletin) to minimize the potential for a steam generator tube rupture (SGTR) event caused by a rapidly propagating fatigue crack which occurred at North Anna Unit 1 on July 15,1987.
- 2. NORTH ANNA UNIT 1 2.1 Discussion Actions taken by the licensee and their Westinghouse consultant to investigate and correct the conditions which led to the July 15, 1987 SGTR event were provided in (1) the licensee's report, "North Anna Unit 1 July 15,1987, Steam Generator Tube Rupture Report," September 15, 1987, Revision 1 (Reference 2),
and (2) Westinghouse reports WCAP-11601 (proprietary version) and WCAP-11602 (non-proprietary version) (Reference 3).
The failure mechanism was established by Westinghouse as fatigue due to excessive flow induced vibration associated with a fluid-elastic instability. To prevent future fatigue crack initiation, the licensee installed a downcomer flow resis-tance plate in each steam generator to reduce the steam generator crossflow velocities and, thus, the stability ratios for all tubes. In addition, extensive preventive plugging was performed on tubes with potentially high stability ratios which were unsupported by anti-vibratiun bars (AVBs). This preventive plugging program included all unsupported tubes beyond row 8 and unsupported row 8 tubes which apprared to be subject to lucalized flow peaking effects. These corrective actions were estimated by Westinghouse to reduce the maximum stability ratio for unsupported tubes remaining in service by at least 22% compared to the stability ratio for the tube which ruptured. This reduction in stability ratio satisfies the 10% criterion developed by Westinghouse to ensure that alternating stress levels are sufficiently small to preclude fatigue crack initiation for the re-maining lifetire of the plant.
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, In addition to the above corrective actions, the iicensee comitted to and implemented an enhanced primary-to-secondary leak rate monitoring program which provides added assurance that the plant will be shut down in a timely fashion before a leaking through-wall crack can propagate to failure. In addition, by letter dated December 4, 1987 the licensee submitted c license amendment request to incorporate this enhanced monitoring program as part of the Technical Specifications.
By letter dated December 11, 1987 (Reference 4), the staff issued its Safety Evaluation authorizing North Anna Unit 1 to return to 100% of licensed power.
The staff concluded in the Safety Evaluation that the licensee had implemented acceptable diagnostic and corrective actions to prevent a similar fatigue f ailure in the future. The licensee's actions and the staff's December 11, 1987 Safety Evaluation pre-dated issuance of Bulletin 88-02 on February 5, 1988.
Although the December 11, 1987 Safety Evaluation endorsed the licensee's enhanced leak rate monitoring program, it did not address the licensee's !
proposal to include this enhanced program as part of the Technical Specifications. The staff expects to complete action on the requested change to the Technical Specifications within the next few weeks.
As part of its March 24, 1988 response to Bulletin 88-02, the licensee enclosed Revision 2 of its "Steam Generator Tube Rupture Report" (Reference 5). The licensee concludes that the actions documented in the Revision 2 report (Reference 5) and WCAP-11601 (Reference 3) resolve the issues identified in Bulletin 88-02.
l 2.2 Evaluation The staff has reviewed the above-mentioned Revision 2 report (Reference 5) and finds that the updated inforhtation contained in this report does not affect the essential facts upon which the staff relied in its December 11, 1987 Safety Evaluation (SE) authorizing North Anna Unit 1 to return to 100% of licensed power operation.
A discussed earlier, the staff's conclusions in its December 11, 1987 SE were based in part on information contained in Westinghouse reports WCAP-11601 and WCAP-11602 (Reference 3). Information contained in more recent Westinghouse reports issued on behalf of other plants (e.g., Reference 6) indicate that local flow peaking effects associated with certain "as built" AVB insertion depth configurations play a more important role in causing high stability ratios than was recognized in Reference 3. The staff's generic evaluation of the more recent Westinghouse studies of local flow peaking effects is documented in Reference 7. ,
However, the staff's review of Reference 3 indicates that regions of the most ;
significant flow peaking effects were included in the licensee's preventive '
plugging program at North Anna Unit 1. Therefore, the staff finds that direct consideration of the higher flow peaking effects now being estimated by Westinghouse would further increase the estimated stability ratio reductions !
which have been achieved i.t North Anna Unit 1 through preventive plq ging. Thus, the more recent information which has become available concerning flow peaking effects does not impact the staff's conclusions in the Decerber 11, 1987 Safety Evaluation.
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- 3. NORTH ANNA UNIT 2 3.1 Discussion The program implemented at North Anna Unit 2 to minimize the likelihood of rapidly propagating fatigue cracks is described in Westinghouse report SG-88-03-016 (Reference 8) which was enclosed with the licensee's March 24, 1988 submittal.
This program is very similar to that implemented at Unit 1. This included installation of downcomer flow resistance plates and preventive plugging of all tubes beyond row 8 which are not effectively supported by AVBs. These actions are estimated to reduce the stability ratios for the most limiting tubes remaining in service (i.e., tubes in row 8) by 24% compared to the tube which ruptured at North Anna Unit 1. This reduction satisfies the 10% reduction criteria developed by Westinghouse for North Anna Unit 1 and which was reviewed by the staff in its December 11, 1987 SE. The estimated reduction assumes flow peaking factors for tubes remaining in service equal to the 1.47 value exhibited by the tube which ruptured at North Anna Unit 1. Westinghouse states that row 8 tubes remaining in service have negligible potential for flow peaking and thus can be expected to exhibit stability ratios significantly smaller than 76% of that associated with the tube rupture at Unit 1.
The licensee's program for Unit 2 also included implementation of the enhanced primary-to-secondary leak rate monitoring program implemented at North Anna Unit 1. The licensee's request to incorporate this enhanced monitoring program as part of the Technical Specificatinns, dated December 4, 1987, applies to Unit 2 as well as Unit 1.
3.2 Evaluation The licensee's program for Unit 2 is essentially the same as that implemented for North Anna Unit I which was reviewed and approved in the staff's SE dated December 11, 1987. The staff's review of the Westinghouse report for Unit 2, however, indicates that several tubes in row 8 may in fact exhibit a degree of flow peaking, contrary to the finding reached by Westinghouse. Although Westing-house did not specifically address the flow peaking factors for these tubes, it is the staff's judgement, based on its review of flow peaking factor test data published in more recent Westinghouse reports (e.g., Reference 6) that the finw peaking factor for these row 8 tubes would be well within the 1.64 upper bound obtained from Westinghouse test data for the most limiting AVB configurations observed at any pWR to date. Naking the extrerely conservative assumption that certain row 8 tubes exhibit a flow peaking factor of 1.64, the staff estimates that the maximum stability ratios for row 8 tubes would still be 15% smaller than the stability ratio for the tube which ruptured at North Anna Unit 1.
This still satisties the 10% acceptance criteria developed by Westinghouse.
Thus, the staff finds that the licensee's program for North Anna Unit 2 is acceptable.
- 4. CONCLUSION Corrective actions at North Anna Units 1 and 2 in the form of installation of downcomer flow resistance plates and preventive plugging effectively minimize the likelihood of rapidly propagating fatigue cracks of the type which led to
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O the SGTR event in July 1987. The enhanced primary-to-secondary leak rate monitoring program implemented at both units provides added assurance that rapidly increasing leaks will be detected, ensuring tinely plant shutdown before rupture occurs. The staff concludes that the licensee has satisfactorily resolved the issues identified in Bulletin 88-02. Consistent with conclusions reached by the staff for other plants (see Reference 7), these findings are subject to the development of administrative controls by the licensee to ensure that updated stability ratio and fatigue usage calculations are performed in the event of any significant changes to the steam (e.g., steam flow and pressure, circulation ratio) generator relativeoperating parameters to the reference parameters assumed in References 3 and 8 for Units 1 and 2, respectively.
REFERENCES
- 1. Licensee's letter dated March 24, 1988, "North Anna Power Station Units 1 and 2, Response to Bulletin 88-02." NRC Accession No. 8803300328.
- 2. Licensee's letter dated September 15, 1987, enclosing licensee's report "North Anna Unit 1 July 15, 1987, Steam Generator Tube Rupture Report,"
Revision 1. NRC Accession No. 8709160239,
- 3. Westinghouse report WCAP-11601 (Proprietary Version) and WCAP-11602 (Non-Properietary Version), "North Anna Unit 1 Steam Generator Tube Rupture and Remedial Actions Technical Evaluation," September 1987. NRC Accession Nos.
8710050087 and 8710050084.
- 4. NRC letter dated Decerrber 11, 1987 to tir. W. L. Stewart, Virginia Electric and Power Company, enclosing proprietary and non-proprietary versions of staff's Safety Evaluation authorizing 100% power operation of North Anna Unit 1 following steam generatur tube rupture event on July 15, 1987.
- 5. Licensee's report, "North Anna Unit 1 July 15,1987, Steam Generator Tube Rupture Report," Revision 2. (This report is docketed as part of Reference 1above).
- 6. Westinghouse Report WCAP-11799 (Proprietary Version) and WCAP 11800 (Non-Proprietary Version), "Beaver Valley Units 1 and 2 - Evaluation for Tube Vibration Induced Fatigue," April 1988. NRC Accession t;u. 88051600'3.
- 7. NRC staff memorandum dated August 19, 1988, C. Cheng to D. Neighbors, "Evaluation of Westinphouse Pethodology to Address item C.2 of NRC Bulletin 88-02."
- 8. Westinghouse report STD-7.2.2.1-8079, SG 88-03-016. "North Anna 2 Steam i Generator Tube fatigue Evaluation and Retredial Actions Report," dated j March 16, 1988. NRC Accession No. 8803300330.
Dated: November 29, 1988 Principal Contributor:
I E. Ilurphy ;
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