ML20154R483

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Insp Repts 50-327/88-34 & 50-328/88-34 on 880606-0711. Violations Noted.Major Areas Inspected:Operational Safety Verification,Including Operations Performance,Sys Lineups, Radiation Protection & Safeguards & Housekeeping Insps
ML20154R483
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 09/15/1988
From: Harmon P, Jenison K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20154R471 List:
References
50-327-88-34, 50-328-88-34, NUDOCS 8810040275
Download: ML20154R483 (32)


See also: IR 05000327/1988034

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NUCLEAR REGULATORY COMMISSION

REGION 11

101 MARIETTA ST., N.W.

$q ', , , , j[ ATLANTA. GEORGIA 30323

Report Nos.: 50-327/88-34 and 50-328/88-34

Licensee: Tennessee Valley Authority

6N38 A Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

Docket Nos.: 50-327 and 50-328 License Nos.: DPR-77 and DPR-79 .

Facility Name: Sequoyah 1 and 2

Inspection Conducted: June 6 - July 11, 1988

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Inspectors:-1 6 M [ A M /iff[

K.mJenyn,seniorRestdentInspector fate /51gned

i A AmAt fri 9kVl88

P. J. Parmon, 5dngr Mesident Inspector Date Signed

Resident Inspectors: D. P. Loveless

W. K. Poertner

P. G. Numphrey

K. D. Ivey I

Approved by: JP[ 7f /E)[

K.fl. J6nisfn Acting Chief, /Date'51gned I

ProjectsStet}on1 l

DivisionofTVAProjects  !

2 OfficeofSpecialProjects

Summary

Scope: This routine, announced inspection involved inspection onsite by the <

Resident Inspectors in the areas of operational safety verification  !

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including o performance, system lineups, radiation i

protection, perations

safeguards and housekeeping inspections; maintenance i

observations * surveillance testing observations; review of previous

inspection Iindings; followup of events; review of licensee

identified items; review of IENs; and review of IFIs.

Results: Three potential violations were identified.

Paragraph 7, 327,328/88-34-02

Paragraph 8, 327,328/88-34-03

Paragraph 9, 327,328/88-34-04

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  • 0ne unresolved item was identified.

Paragraph 4,(327,328/88-34-01)

No deviations were identified.

An Enforcement Conference sur. mary pertaining to Violation 327,328/

88-34-02 is contained in paragraph 7.

"Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or deviations.

There were no Unit I startup items identified in this report.

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REPORT DETAILS

1. Persons Contacted

Licensee Employees

H. Abercrombie, Site Director

J. Anthony, Operations Group Supervisor

  • R. Beecken, Maintenance Superintendent

J. Bynum, Vice President, Nuclear Power Production

M. Cooper, Compliance Licensing Manager

  • 0. Craven, Plant Support Superintendent

H. Elkins, Instrument Maintenance Group Manager

R. Fortenberry, Technical Support Supervisor

J. Hamilton, Quality Engineering Manager

J. La Point Deputy Site Director

L. Martin,$iteQualityManager

R. Olson Modifications Manager

J. Patrick, Operations Group Manager

R. Pierce Mechanical Maintenance Supervisor

  • M. Ray,SIteLicensingStaffManager
  • R.

Rogers,ld, licensing EngineerPlant Reporting Section

8. 3chofie

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  • S. Smith, Plant Manager
  • S. Spencer, Licensing Engineer

C. W11ttemore, Licensing Engineer

NRC Employees

M. Branch

l A. Long

  • Attended exit interview

NOTE: Acronyms and initialisms used in this report are listed in the last

paragraph.

2. Operational Safety Verification (71707)

a. Plant Tours

The inspectors observed control room operations; reviewed applicable

logs including the shif t logs, night order book, clearance hold order

book, configuration log and TACF log; conducted discussions with

control room operators; verified that proper control room staffing

was maintained; observed shift turnovers and confirmed operability

of instrumentation. The inspectors verlfied the operab'lity of

selected emergency systems, and verified compliance with TS LCOs.

The inspectors verified that maintenance work orders had been

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submitted as required and that followup activit es and prioritization

of work was accomplished by the licensee.

Tours of the diesel generator, auxiliary, control, and turbine

buildings, and containment were conducted to observe plant equipment

including potential fire hazards, fluid leaks and

conditions,ibrationsandplanthousekeeping/cleanlinesscondItions.

excessive v

The inspectors walked down accessible portions of the following

safety-related systems on Unit 1 and Unit 2 to verify operability and

proper valve alignment:

SYSTEMS

Auxiliary Feedwater System

Containment Spray System

Residual Heat Removal System

SafetyInjectionSystem

UpperHeadInjectionSystem

No violations or deviations were identified

b. Safeguards Inspection

In the course of the monthly activities, the inspectors included a

review of the licensee's physical security program. The performance

of various shifts of the security force was observed in the conduct

l protected and vital area access

l of daily activities

controls; including:l

searching of personne and packages; escorting of visitors;

badge issuance and retrieval; patrols and compensatory posts.

In addition, the inspectors observed

protected and vital area barrier integr' protectedty. The inspectors area lighting, verified

interfaces between the security organization and operations or

maintenance. Specifically, the Resident Inspectors:

interviewed individuals with security concerns

reviewed licensee security event report

visited central or secondary alarm station

observed power supply test

verified protection of Safeguards Information

verified onsite/offsite communication capabilities

No violations or deviations were identified,

c. Radiation Protection

The inspectors observed HP practices and verified the implementation

of radiation protection controls. On a regular basis, RWPs were

reviewed and specific work activities were monitored to ensure the

activities were being conducted in accordance with the applicable

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RWPs. Selected radiation protection instruments were verified

operable and calibration frequencies were reviewed.

The following RWPs were reviewed:

88-01-12: Unit 1 Containment, All Areas.

88-00-07-01: All RWP Areas (chemistry personnel only).

No violations or deviations were identified

3. Sustained Control Room Observation (71715)

The inspectors observed control room activities and those plant activities

directed from the control room for approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> in each 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

shift for this rnort period. The observation consisted of one shift

inspector per shif; supported by one shift manager per shift and other OSP

management, on 06/28/88 at 1700, 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> on-site shif t coverage by the

NRC was terminated. Normal inspection coverage was resumed at this time,

a. Control Room Activities Including Conduct of Operations

The inspectors reviewed control room activities to determine that

operators were attentive and responsive to plant parameters and

conditions; operators remained in their designated areas and were

attsntive to plant operations, alarms and status; operators employed

cm.nunication, terminology and nomenclature that was clear and

formal; and operators performed a proper relief prior to being

discharged from their watch standing duties,

b. Control Reom Activities Including Response to Transient and Emergency

Conditions

The inspector witnessed the Unit 2 operations emergency aersonnel

respond to adverse plant conditions created by a severe t1under and

electrical storm that occurred on June 25, at 4:50 p.m. The storm

caused a switchyard breaker to trip and resulted in an initiation of

the "carrier received indicator " alarms and various other control

alarms. At essentially the same time, it was reported that damage

had occurred that had disabled the Safety and Security tower and

winds had resulted in a parked semi-trailer overturning at the plant

site In addition, a fire alarm indicated that a fire had occurred

in the turbine building. The responding emergency team determined

the cause of the alarm to be a result of smoke entering the building

from the auxiliary boiler exhaust via the roof ventilation.

The responses and evaluations of these situations by the operators

were well managed by the shift personnel.

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c. Control Room Hanning

The inspectors reviewed control room manning and determined that TS

requirements were met and a professional atmosphere was maintained in ,

the control room. The inspectors found the noise level and working

conditions to be acceptable. The inspectors observed no horse play l

and no radios or other non-job related material in the control room.

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Operator compliance with regulatory and TVA administrative guidelines l

were reviewed. No deficiencies were identified, i

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. In addition, the control room appeared to be clean, uncluttered, and  ;

well organized. Special controls were established to limit personnel '

in the control room inner area.

d. Routine Plant Activities Conducted In or Near the Control Room  !

The inspectors observed activities which require the attention and [

direction of control room personnel. The inspectors observed that t

necessary plant administrative and technical activities conducted in t

or near the control room were conducted in a manner that did not ,

compromise the attentiveness of the operators at the controls. The  !

licensee has established a 505 office in the control room area in i

which the bulk of the administrative activities, including the '

i authorized issuance of keys, takes place. In addition the licensee .

has established H0, WR, SI, and modification matrix functions to t

i release the licensed operators from the bulk of the technical i

i activities that could impact the performance of their duties. These  ;

j matrixed activities were transferred into the WCC. '

j e. Control Room Alarms and Operator Response to Alarms

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i The inspectors observed that control room avaluations were performed

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utilizing approved plant procedures and that control room alarms were

responded to promptly with adequate attention by the operator to the

alarm indications. Control room operators appeared to believe the

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alarm indications. None were identified by the inspectors that were

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either ignored by the operators or timed-out.

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f. Fire Brigade

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j The inspectors reviewed fire brigade manning and qualifichtions on a

j routine basis. Both manning and qualifications were found to meet TS

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requirements.

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, The inspector reviewed the training received by the new fire brigade

crew to ascertain whether an appropriate amount of operations

knowledge is imparted to the crews. The fire brigade is broken into

j a "composite crew" format which naturally lends itself to providing

l plant knowledge. The crew is composed of personnel with the

following experience:

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1 Steamfitter

1 Electrician

2 Firefighters

This crew then receives 12 weeks of intensive training. Two weeks

of this training includes familiarization with all safe shut 0wn

(Appendix R) systems. The training includes comaonents, f h pat i s,

and safety significance. Additionally, the training includos cwo

weeks of intensive training on fire protection systems in the plant.

Following the classroom training the crew completes system

qualification cards for in plant knowledge of the systems. Typical

qualification card items are listed below:

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LocatetheUpperHeadInjectionaccumulatorandsurgetank

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State the cooling medium for the Spent Fuel Pit Cooling System

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State whether there is any radiation associated with the EGTS

and describe how it is contained

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i.ist the emergency supply for the 6900 V Shutdown Boards

The training received by the crews appears adequate and appropriate.

the affected unit A505 will res)ond with the crew and

Additionally,"incident

function as command". This indivicual will control all

non-fire protection plant equipment and make reccommendations

concerning priority of plant equipment to be protected. Operation of

plant equipment other than the fire protection systems by the

compoCte crew is prohibited. This arrangement is consistent with

estaolished plant procedures and policies and appears appropriate to

the fire brigade functions,

g. Shift Briefing / Shift Turnover and Relief

The inspectors observed that U0s completed turnover checklists,

conducted control panel and significant alarm walkuown reviews and

significant maintenance and surveillance reviews prior to tellef.

The inspectors observed that sufficient information was transferred

on plant status, operating status and/or events and abnormal system

alignments to ensure the safe operation of the Unit. ASOS relief was

conducted and sufficient information appeared to be transferred on

plant status, operating status and/or events, and abnormal system

alignments to ensure the safe operation of the Unit. ASOS were

observed reviewing shif t logbooks prior to relief.

Shift briefings were conducted by the offgoing 505. Personnel

assignments were made clear to oncoming o:)erations personnel.

Significant time and effort were expended d scussing plant events,

plant status, expected shift activities, shift training, significant

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surveillance testing or maintenance activities, and unusual plant

conditions,

h. Shift Logs, Records, and Turnover Status Lists

The inspectors reviewed 505, 00, A505 and STA logs and determined

that the logs were completed in accordance with administrative

requirements. The inspectors ensured that entries were legible;

errors were corrected initialed and dated; logbook entries

adequately reflected plant status; significant operational events

and/or unusual parameters were recorded; and entry into or exit from

TS LCOs were recorded promptly. Turnover status checklists for R0s

contained sufficient required information and indicated plant status

parameters, system alignments and abnormalities. The following

additional logs were also revie,wed:

Night Order Log

System Status Log

Configuration Control Log

Key Log

Temporary Alteration Log

No discrepancies or deficiericies were identified,

i. Control Room Recorder / Strip Charts and Log Sheets

The inspector observed operators check, install, mark, file, and

route for review, recorder and strip charts in accordance with the

established plant processes. Control room and plant equipment

logsheets were found to be complete and legible; parameter limits

were specified; and out-of-specification parameters were marked and

reviewed during the approval process.

4. Management Activities

TVA management activities were reviewed on a daily basis by the NRC shif t

inspectors, shift managers, and Startup Manager,

a. Daily Control of Plant Activities (War Room Activities)

The licensee conducted a series of plant activities throughout each

day to control plant routines. These activities were referred to by

the licensee as War Room activities. War Room activities were

observed by the shift manager on a daily basis and were found to be

an adequate method to involve upper level management in the

day-to-day activities affecting the operation of the units,

b. Management Response To Plant Activities and Events

Review of the licensee's corrective actions associated with restart

following the June 8, 1988, reactor trip:

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The reactor trip of June 8,1988, was the fif th in a series of  !

reactor trips that occurred subsequent to the first Sequoyah Unit 2

restart on Ma 13, 1988. Following this trip the NRC requested that

i the licensee'ys post-trip review assess the four previous trips and .

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determine if there were any common factors associated with the trips.  !

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Additionally, on June 13, 1988, the licensee met with the NRC in i

Rockville, MD, at a public meeting for the purpose of presenting t

i their assessment and any corrective action planned. During the -

j meeting, the licensee indicated that a major contributor to several t

of the trips was the material condition of the secondary plant as  :

well as a lack of detailed procedures for steam generator (SG) level  ;

control. t

1988, the Assistant Of rector for Inspection Programs,

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On June 16)NRC,li

TVAPD OSP

detailsofthe

met with the Sequoyah management and discussed the

censee's immediate and long term corrective actions.

3 The licensee committed to the following corrective actions and i

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evaluations prior to plant restart: ,

! Review and reduce the backlog of outstanding work requests (WRs)

on secondary plant equipment aild evaluate their possible  ;

contribution to reducing the risk of balance of plant (80P)

l induced reactor trips. ,

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Revise operating instructions to enhance plant start-up

activities to control feedwater flow and SG 1evels during low  !

level power ascension.

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I * Require the Plant Operations Review Committee (PORC) to evaluate l

future plant trips and recommend procedural changes, where  !

applicable, to reduce the probability of future plant trips. i

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] Shif t operating crews will be trained on the Sequoyah simulator l

1 in using the revised operating instructions for startup of the i

l feedwater control system.

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) The inspectors reviewed the procedural changes and training >

i incorporated as a result of the licensee's commitments. Each was I

l reviewed as to whether the commitment was implemented and that the [

plant would be in compliance with the safety analysis. The following  !

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sumarizes this review and inspector coments: [

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l Training for the operating crews was observed and det. ermined to (

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be acceptable. }

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General Operating Instructions, G01 1, rev. 77, Plant Startup I

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from Cold Shutdown to Hot Standby - Units 1 and 2, and G01-2, i

rev. 56, Plant Startup from Hot Standby to Minimum Load - Units l

l 1 and 2, incorporated the requirement for the shif t operating l

1 supervisor (505) to make a systematic review of all open work

i activities relative to the respective units for the purpose of j

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identifying maintenance activities that could affect system

operability prior to mode change. NRC observation of this

process indicated acceptable condition for Unit 2 operation.

Observation of this review will be conducted by the inspectors

during Unit I startup. Further changes were made to Admin-

istrative Instruction, AI-5, rev 43, Shift Relief and Turnover,

requiring that prior to assuming the watch, the oncoming shift

personnel (505, A505,STA, and representatives from the radio-

logical chemical laboratory radiological control group, and the

waste processing group) ass,emble in the work control center for

a briefing on all work activities in progress and scheduled work

activities to be performed during the upcoming shif t for both

units. The work activities must be approved by the SOS prior to

implementation. The inspectors reviewed the changes pertaining

to the above areas and found them acceptable. The inspector

observed several shift turnovers conducted in the work control

center to verify that proper briefings on work activities were

presented.

GOI-2, rev. 56, incorporated changes for maintaining feedwater

control and SG 1evels during plant startup activities that were

developed through simulator validation. The changes provided

instruction for switching from manual to automatic operation of

the feedwater system. Additionally, the new method changed the

SG 1evels that the operator must try to maintain at low power

levels from the 33% programmed level to 48% in each SG.

The inspectors reviewed these changes and could not determine

that the plant had been analyzed for a condition of a SG water

mass increase of the magnitude required in the G01-2 revision.

The licensee was asked to provide the safety evaluation of this

change. The licensee had only performed a USQD screening and

determined that the FSAR supported the increase in SG 1evel from

33% to 48% level at less than or equal to 3% reactor power. The

inspectors requested that the ifcensee provide a more detailed

analysis to support the level increase. The licensee

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corresponded with the nuclear steam system supplier Westing-

l house, who indicated that they did not have sufficient site

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specific information to support a SG 1evel increase from 33% to

48% at 0% reactor power. Rather, Westinghouse indicated that

the precautions, I'mitations, and sotpoints docutuent indicated

that the control band for SG program level was plus or minus 5%.

G01-2 was again revised (rev. 57) to require the SGs to be

operated at programed level, plus or minus 5%, during startup

and plant operations. The fact that Westinghouse could not

support the licensee position that the plant accident analysis

for a main steamline break was still bounded was of concern to

the NRC. This item is identified as URI 327, 328/88-34-01.

This issue will be reviewed further to determine whether a

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violation of NRC regulations occurred when the initial change

was evaluated for compliance with 10 CFR 50.59 requirements.

The inspector discussed this concern with ifcensee management

prior to the actual implementation of GOI-2. The licensee

agreed that further review was necessary and revised GOI-2 to

delete the change to the programmed level,

i A!-30, rev. 19, Nuclear Plant Conduct of Operation, incorporated

the requirement that experienced dedicated coaching be provided

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by TVA for inexperienced operators during startup and transfer

from manual to automatic operation of the feedwater control

I system. Although this dedicated coaching later appeared to not

I be fully necessary, actions taken by the licensee to allow the

l A505 to directly supervise significant operations by unit

l operators were considered to be appropriate, effective, and

acceptable.

AI-18, rev. 51, Plant Reporting Requirements, incorporated the

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requirement for the PORC to review and approve each plant trip

l report prior to restart of the plant. The inspector considered

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this practice to be a noteworthy improvement.

5. Engineered Safety Features Walkdown (71710)

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The inspector verified operability of the containment spray system on

Unit 1 by completing a walkdown of the system. This inspection was

documented in the SSQE Inspection Report 327,328/88-29.

6. Shift Surveillance Observations and Review (61726)

Lices.see activities were directly observed to ascertain that surveillance

of safety-related systems and components was being conducted in accordance

with TS requirements.

The inspectors verified that; testing was performed in accordance with

adequate procedures; test instrumentation was calibrated; LCOs were met;

test results met accestance criteria reoutrements and were reviewed by

personnel other than "he individual directing the test; deficiencies were

identified, as appropriate, and any deficiencies identified during the

testing were properly reviewed and resolved by management personne :; and

system restoration was adequate. For completed tests, the inspector

verified that testing frequencies were met and tests were performed by

qualified individuals.

The following activities were observed / reviewed:

SI-2: Shift Log - Units 1 and 2.

SI-3: Daily, Weekly, and Monthly Logs - Units 1 and 2.

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SI-79: Power Range Neutron Flux Channel Calibration By

Incore-Excore Axial Imbalance Comparison. This SI is

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required at least once per month when above 15% reactor

l power. The incore axial imbalance is obtained from a

moveable detector flux map which is analyzed by the incore

computer program.

SI-129.1: SafetyInjectionPumpCasingandDischargeVenting.

l 5!-137.1: Reactor Coolant System Unidentified Leakage Measurement.51-137.2: Reactor Coolant System Water Inventory.

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No violations or deviations were identified.

1 7. Shift Maintenance Observations and Review (62703)

a. Station maintenance activities of safety-related systems and

components were observed / reviewed to ascertain that they were

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conducted

industry codesin accordance with

and standards, andapproved procedures,ith

in conformance w TS. regulatory guides

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The following items were considered during this review: LCOs were

met while components or systems were removed from service; redundant

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components were operable; approvals were obtained prior to initiating

l the work; activities were accomplished using approved procedures and

I inspected as appifcable; procedures used were adequate to control the

l activity; troubleshooting activities were controlled and the repair

record accurately reflected what actually took place; functional

testing and/or calibrations were

components or systems to service; performed

QC records prior

were to returning

maintained;

activities were accomplished by qualified personnel; parts and

materials used were properly certified; radiological controls were

implemented- QC hold points were established where required and were

observed; / ire prevention controls were implemented; outside

contractor activities were controlled in accordance with the approved

QA program; and housekeeping was actively pursued,

b. Temporary Alterations

The following TACFs were reviewed:

0-88-08-02: Condensate Storage Tanks. Temporary connections

to drain valves to allow makeup water feed from a

mobile vendor demineralizer.

No violations or deviations were identified.

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c. Work Requests

The inspectors observed work in progress and reviewed work packages

for the following work requests / work plans:

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WR 8245103: Repair of the "A" train main feedwater pump

turbine speed control system to correct pump t

oscillations and provide a more controlled feed -

flow to the SGs.

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WP E437A-01: Testing and repair of all safety-related room

coolers due to the discovery of broken shafts on

certain room cooler motors caused by impro)er fan

belt tensioning. The inspector observed tie work

on the "A" and "B" trains of the Boric Acid ,

Transfer & AFW Pump Coolers.

No violations or deviations were identified.

Subsequent to the management meeting held with TVA on June 13, the

inspectors reviewed the scope of the maintenance work requests for

Unit 2 that were pending when the reactor trips occurred on June 6  :

j and June 8. The purpose of this review was to establish:

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  • Whether the approximately 128 WR's listed as "Startup Priority"
was complete and conservative in bounding all necessary work to

be performed prior to Unit 2 startup.

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Whether the screening criteria used in the "Startup Priority" .

determination was adequate and conservative. l

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  • Selection of a representative sample of those WR's not deter- i

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mined to be "Startup Priority" and apply the screening criteria I

as an independent audit on the process.

I The screening criteria ised was a check list, which was applied to l

> the total outstanding work list of 1308 items listed for Lnit 2 and l

] Comon. Answering "Yes" to any one of the

j sheet placed the WR in the "Startup Priority"questions

category: on the check !

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  • Is the WR a Main Control Room generated WR?

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  • If the WR is not completed, will the operators be required to I

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use remote indications, manual controls or other compensatory i

measures?

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If the WR is not completed, could false indications cause the

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in plant operators (AUO's) to notify the control room? (An l

example is a plugged / dirty sight glass on a drain tank). l

  • If the WR is not completed, could controller problems develop i

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1 that could cause instability in the secondary plant (BOP)? [

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  • If the WR is not completed, could an identified prob 1cm worsen

later and not be isolable / workable at power? (e.g. a minor 1

steam leak that could develop into a serious leak that is not '

isolable with 2 valve protection). i

Is the WR one of those identified by the Operations staff as one

they consider necessary for restart?

The screeninc criteria was considered adequate by the inspector, and I

was then applied to 38 selected WR's that were not on the startup  !

list. Each of the 38 were discussed with TVA staff familiar with the ,

screening process. The inspector agrees with TVA staff's

determination of non-startup category for each of the selected sample  ;

items. TVA completed all Startup Priority WR's prior to Unit 2 '

startup on June 23.

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No violations or deviations were identified

d. Hold Orders

The inspectors reviewed various H0s to verify compliance with AI-3,

revision 38, Clearance Procedure, and that the H0s contained adequate  ;

information to pro)erly isolate the affected portions of the system

being tagged. Adcitionally the inspectors inspected the affected i

equipment to verify that the recuired tags were installed on the  ;

equipment as stated on the H0s. The following H0s were reviewed:  ;

Hold Order Equipment

2-88-516: "A" Train Main Feedwater Pump for work on I

the governor valve positioner.

2-88-463: 28 Annulus Vacuum Fan. I

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2-88-487: 28 690 Elevation Penetration Room Cooler to

repair a broken shaft.

2-88-520: Positive Displacement Charging Pump to I'

replace a plext glass cover gasket.

No violations or deviations were identified. I

,

1

,

e. Maintenance Activities Affecting Plant Operations

On 07/05/88, at 2:30 p.m., Unit 2 operators received indication that  !

the pressure indicator (2-PIS-87-21) for UHI isolation valve 2-87-21  ;

was erratic and indicating high (4000 psig) when all previous '

readings were steady at approximately 3000 psig. The pressure  !

indicator is the sole method on-line to monitor the condition of the i

isolation valve's actuator. The actuator is a hydraulic actuator

pre-charged with nitrogen to 1400 psig, then hydraulically charged to

I

1

__ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ ___ _ _ _____-________-__ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

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13

3000 psig. A bladder separates the nitrogen from the hydraulic side.

A pre-charge of 1400 asig provides sufficient stored energy to stroke

the UHI isolation va:ve silut when the UHI water accumulator reaches

its low level setpoint during a LOCA event. This action assures

delivery of sufficient water inventory to the core and prevents

injectionofUHIsystemnitrogenintothecore.

The pressure indicator was removed from service and re-calibrated.

07/08/88 at 2:30 p.m.,

After reinstalling )the pressure indicator on(a delay of 3 days , the actuato

be reading below the alarm setpoint of 2970 psig. A Westinghouse

analysis had previously been provided to allow a limited number of

rechargings of the hydraulic side of this accumulator. Assuming that

the pressure decrease was due to nitrogen leaks, a maximum of 4

rechargings was allowed before the nitrogen preload was considered

less t,1an that required to properly stroke the isolation valve. This

is based in part on the volume and pressure of the compressed

nitrogen and the assumed nitrogen loss to decrease pressure to the

alarm point. Af ter 4 such recharges, the licensee's procedure (SI

744) requires a stroke test of the isolation valve to verify

operabil lty. An originally installed weight indication method of

determining the volume of nitrogen in the accumulator was unreif able

and ineffective. Since only pressure could be read on-line, the

alternate method of allowing 4 recharges and then providing positive

assurance of operability by a stroke test was developed by the

licensee and Westinghouse. This is considered a compensatory

measure.

Licensee management (plant manager, maintenance manager, operations

among others) met at 4:30 p.m. on 07/08/88 and

manager

decided toand P0RS,ine valve operability by another method.

determ The

decision was to perform a pre-charqe test instead, which was

considered a more reliable method of determining that sufficient

nitrogen was available. The pre-charge test requires declaring the

isolation valve inoperable, draining the actuator's hydraulic side,

and then measuring the nitrogen side pressure.

A plan of action was drawn up which included gathering any spares or

replacement parts, a procedural change to SI 744 to allow the

pre-charge test in lieu of the stroke test, and several contingency

actions. The spares were not found and made available untti

07/09/88, and the procedure was not changed until 07/10/88. By the

time the licensee was ready to implement the test, the accumulator

pressure alarm had been received and recharging accomplished a total

of 7 more times. After the fourth recharge, at 1:30 p.m. on

07/09/88, the still-in-effect requirements of SI 744 required an

immediate stroke test of the isolation valve. This was not done. By

the time the licensee had finally performed an operability test by

checking the pre-charge at 1:55 p.m. on 07/10/88, over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> had

elapsed since an operability determination had been required by SI

744. When the pre-charge test was finally performed, the nitrogen

_ - _ _ _ _ _ _

':0 .'

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14

which is less than the minimum of

pressurewasfoundtobe1165psig}mittoensureoperability.

1300 psig specified as the lower 1

The loss of nitrogen was determined to be due to a leaking nitrogen

charging valve (Schrader valve). This valve was replaced, the

nitrogen side recharged to 1400 psig, and the valve returned to

service at 3:55 p.m. on 07/10/88.

While the management decision to perform a pre-charge test rather

than the required stroke test was probably acceptable and would have

adequately demonstrated operability, the execution of the plan was

not well coordinated. Several dela

parts and changing the procedure. ys were encountered

Althou in locating

several levels of

management were involved in this evolution,ghtbeworkwasdelayedfor

over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> past the point when the valves should have been

repaired or declared inoperable. In conjunction with these delays,

it is considered that the licensee did not take appropriate actions

when conditions (the 4th thru 7th low pressure alarm and recharging

evolutions) indicated potential valve inoperability.

Subsequent to this event, TVA asked Westinghouse to provide an

analysis to determine whether the valve would have performed its

intended function with the as-found pressure of 1165. A Westinghouse

analysis dated 7/12/88, asserted that the valve would have stroked

closed in approximately 8 seconds, as opposed to 4 seconds with a

fully charged accumulator. This asserted condition is stated to

result in an additional injection of 120 cubic feet of t;HI water to

,

the core bringing the total injected volume to 1170 cubic feet.

I This additional volume is within the accident analysis assumption of

I

'

a maximum 1180.5 cubic feet. This sug ests the valve may have been

post facto operable, but does not relieve the licensee of their

commitment to demonstrate operability by compliance with T.S. and

their own procedures.

While the system arrangement provides a second, series valve operated

by the opposite ESF train, which probably would have actuated

properly, single failure criteria require redundant equipment to be

operable.

T.S. 3.5.1.2 requires the UHI system to be OPERABLE (including the

isolation valves) or, to restore the system to OPERABLE in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> or

be in HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. This action statement was

not entered until 12:31 p.m. , on 07/10/88, when work on the valve

began. Since the valve is determined to be operable by performance

of a verification test whenever 4 recharges have occurred, the valve

should have been declared inoperable after the recharge performed at

1:30 p.m. , on 07/09/88, when procedural actions to stroke time test

the valve were not taken. The appropriate action statement was not

entered on a system required for safe shutdown. This is considered a

violation of T.S. 3.5.1.2, for failure to comply with a TS action

statement. This item is identified as Violation 327,328/88-34-02.

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,

On July 28,1988, the NRC held an enforcement conference with TVA at i

the Sequoyah Nuclear Plant to discuss concerns related to the t

l

apparent noncompliance with T.S. 3.5.1.2 described above. Attendees '

at the conference are delineated in the attachment to this report. '

The meeting was opened by J. Partlow, Director, Office of Special

Projects, who along with F. McCoy, Assistant Director for TVA

Inspection Programs, discussed the NRC concerns with this specific ,

event. NRC management stated their concern that the licensee had

failed to comply with procedures established to confirm UHI valve

3

operability when cond'tions indicated a potential for valve >

inoperability. Additionally, given this set of circumstances, the  !

licensee failed to enter the action statement of T.S. 3.5.1.2 until '

operability could be confirmed. NRC management questioned the l

conservatism and safety consciousness of TVA's actions with respect .

j to this event.  !

l

l TVA was asked to address their own investigation into the event and I

] the specific concerns of the NRC. TVA presented their evaluation of (

, the event and their conclusions as to how the the noncompliance with  !

'

! T.S. was allowed to occur.

l

TVA presented background information and details of the event which  !

agreed with the NRC's evaluation in most instances. A copy of the  !

material presented by TVA at this conference has also been included l

in the attachment to this inspection report. The Sequoyah plant -

manager acknowledged at the enforcement conference that the plant had  ;

been in violation of T.S. 3.5.1.2 for a period of approximately 23 i

hours, from 1:30 p.m. on 07/09/88 until 12:31 p.m., on 07/10/88. TVA  ;

presented an analysis performed by Westinghouse that supports their '

.

determination that the safety significance associated wit 1 this event

was minimal and that the valve in question would have functioned if

called upon during the time frame the plant was outside the T.S. TVA

demonstrated at the enforcement conference that the event was caused

by a lack of coordination among various site groups and was not a

result of nonconservative management action.

8. Event Followup (93702, 62703)

At 11:59 p.m., on 6/29, a blackout signal was initiated on Unit 16900

volt shutdown board 1-B-8. The initiating event was the tripsing of the

feeder breaker to the shutdown board from the 6900 volt unit 30ard. The

feeder breaker (#1722) tripped when maintenance workers were attempting to

replace a fuse in the breaker's position indicating light circuit. The

circuit was inadvertantly grounded when maintenance workers were replacing

the blown fuse, causing the breaker trip circuit to actuate. When the

1-8 8 shutdown board was deenergized, all 4 EDG units started. The 1 B-8

shutdown board was reenergized when the 1-B B EDG care up to speed and

tied onto the bus. The other EDG's did not tie on to their respective

buses because those buses continued to be energized from the unit boards.

Af ter resetting the breaker 1722 trip circuit, the unit boards were

paralleled with the 1-B-B EDG, and the EDG's were stopped. All systems

_ _ __________ _-

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16

performed as designed, and an ENS notification made to NRC at 12:08 a.m.

on 6/30.  !

At 7:29 p.m., on June 3,1988, EDG 1A-A was made inoperable for the

performance of SI-307.1, Degraded Voltage Relay Response Time Testing and *

Timer Verification. At that time the Unit 2 00 logged in the LCO log that '

LCO for TS 3.8.1.1 was entered. At 10:40 p.m. on June 3, 1988, SI 307.1

was completed and EDG 1A-A was returned to service. During the subsequent '

shif t turnover meeting at approximately 11:30 p.m. a discussion of the '

work performed for the previous shif t resulted in the 505 realizing that  :

the requirements of TS 3.8.1.1 had not been met. TS 3.8.1.1 requires that

with an EDG inoperable, the operability of the remaining AC sources must ,

be demonstrated by performance of SR 4.8.1.1.1.a and 4.8.1.2.a.4 within  :

one hour and at least once per eight hours thereaf ter. Failure to meet l

the requirements of TS 3. 8.1.1 is identified as Violation  :

327,328/88-34-03, j

s

9. Followup on Previous Inspection Findings (92702)  ;

(Closed) URI 327,328/88-26-03, Resolution of RCS Leak Rate Determination  !

Process.

{

On April 6, at approximately 6:50 a.m., the licensee completed f

Reactor Coolant System Water  !

computations

Inventory. The forresults

Part 1indicated

of SI-137.2,

an initial unclassiffed RCS leak i

rate of 1.09 _gpm which if considered unidentified, would have  :

exceeded the T5 Ifmit of 1 gpm. As required by procedure the i

chemistry laboratory was notified to perform Part 2 of SI-13).2. At  ;

the time, the 505 was at the shif t meeting preparing for turnover of i

the watch to the oncoming shift crew. He informed the Assistant 505  !

by phone, not to enter the LCO for RCS leakage because procedural , i

problems had caused them to enter the same LCO unnecessarily in the  !

past. This decision was made even though the operators had noted

abnormal increases in the reactor building auxiliary floor and  !

equipment drain sump levels throughout the shift. '

At 7:55 a.m., the licensee entered LCO 3.4.5.2 for RCS leakage when a i

gasket on 2-PDT 62-47, the differential pressure transmitter on the r

  1. 4 reactor coolant pump seal return line, was found to be leaking. A [

Notification of Unusual Event was not made within 5 minutes per  !

IP-1, RCS Leakage, which required entry into the Radiological (

Emergency Plan if leakage exceeds the TS limit. At 8:20 a.m. ,  !

licensee management personnel reviewed the decision and issued a [

NOVE. At 8: 42 a.m., the differential pressure transmitter was

isolated utilizing the root valves. At 9:11 a.m. , the licensee ,

notified NRC Headquarters in accordance with the one hour emergency

reporting requirements. Although this notification was made within

one hour of the management decision to enter the NOVE, the inspectors ,

noted that this was accomplished approxiestely 76 minutes af ter entry [

into LCO 3.4.5.2 (which, by the licensee's radiological emergency [

procedures, required a declaration of unusual event) and nearly 2.5 i

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hours after the operators had verifiable indi:ation that leakage l

might be outside of TS limits. l

AOI-6, Small Reactor Coolant System Leak (Modes 1, 2, & 3), had not

been entered. A01-6 states that one pose,ible symptom of a small

reactor coolant leak is receiving the "Reactor Building Auxiliary

Floor and Equipment Drain Sump High" alarm, window 19 of XA 55-5A on

panel 1-M-5. This elarm was received twice during the shif t as  !

stated above. Additionally with the high leak rate as calculated in  !

SI-137.2 and the discovery, of 2-PDT-62 74 leaking the inspector

cont,iders that it would have been prudent to perform the actions of

AOI-6. Although non performance of the recommendations in A01-6 does l

not appear to violate any licensee or NRC requirements, the

inspectors have concern that the licensee's annunciator response t

procedures do not provide an initiation path for the A01 procedures, i

l

-

At 5:45 p.m.dicatedthe

SI-137.2 in an licensee

acceptable exited the NOUE

leakage when

rate of 0.48a gpm.

new performance of

l

Subsequent performance of SI 137.5 Primary to Secondary Leakage via '

Steam / Generators, reflected that 0.16 gpm of this leakage rate was

attributable to the tube leak in steam generator 3 discussed in '

Inspection Report 88-26. The licensee estimated that between 250-300

"

gallons of inventory had leaked during the entire event by estimating

the leakage rate from 2-PDT-62-47 to be 0.61 gpm and by confirmation

i of the pocket sump levels. The licensee issued a statement to the  ;

l press on this occurrence at 11:00 a.m. on April 6. i

! The delays in entering and reportint the NOUE and the LCO on RCS leak  !

j rate and the concerns involving in' tiation of A0! procedures were f

, identified as Unresolved Item 88-26-03.  ;

J

l During this event TVA had used a cumbersome method to calculate I

i unidentified RCS leakage and to determine what part, if any, that a j

i

pricary to secondary leak p, layed in this unidentified leakage value.  :

j the licensee s RCS inventory measurement procedure  !

Specificallyld

SI-137.2 wou perform an inventory balance and if the unclassified

>

1eakage was ebove a specific value they would then recuest that a

, primary to secondary leakage measurement be performed 'n accordance .

with SI-137.5. Performing a primary to secondary leakage calculation ,

only to quantify unidentified leakage resulted in both a delay in l

completing the RCS unidentified 1(akage measurement and a lack of l

'

consistent primary to secondary leakage trending data. The staff  ;

considers that this methodology was a maior contributor to the delays t

, associated with entry into (and applicable reporting of) the NOUE and i

LCO, as identified in Unresolved Item 86-26 03. l

I  !

! Revision 22 of $1-137.2 revised the method to require that primary to l

i secondary leakage measursent be performed every 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and be a  ;

prerequisite to the inventory balance performed by SI-137.2. This j

,

ne method should produce both consistent primary to secondary '

1eakage trending data as well as expedite the determination of RCS

l

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!

leakage. This method also provides adequate corrective action to

preclude raising questions such as those indicated under Unresolved

Item 88-26-03 discussed above.

The NRC staff reviewed the e/ent with respect to the utilization of

SI-137.2. It was determined that the intent of LCO 3.4.5.2 was to

'

consider any known leakage to be unidentified until an identification of

the source was made. Therefore, unclassified leakage is unidentified

leakage and LC0 3.4.5.2 chould have been entered at 6:55 a.m. Although j

the Lispector had earlier discussions with the licensed operaters, it was

determined that not entering the action statement was identi, led and

resolved independently by the licensee management.

At 7:55 a.m. , on April 6, the operators entered LCO 3.4.5.2 when the leak

'

was actually observed. At this time the operations staff still did not l

enter a NOUE as required by the REP because the 505 haf left instructions '

to the contrary. Tne inspector discussed this decision with the operators i

at the time.

The Sequoyah Radiological Emergency Plan IP-1 Emergency Plan  :

Classification Logic which implements these requi,ements,

r requires that t

the operators enter a NOUE if the primary system leak rate is greater than  ;

that allowed in the TS. In addition, REP Implementing Procedure IPel, j

also states, if there is any reason to doubt whether a given condition has '

actually occurred, the shift engineer or Site Emergency Director will

proceed with the required notification without waiting for formal

confirmation. 1

In addition, REP Implementing Procedure IP-1, also states, if there is any  :

reason to doubc whether a given condition has actually occurred, the shift

engineer or Site Emergency Director will proceed with the required ,

notification without waiting for formal confirmation. l

_

IP-2, Notification of Unusual Event, requires that the not'tication of the [

Operations Duty Specialist be made within 5 minutes af ter .he declaration r

of the event.

on A)ril 6,1988 at 7:55 a.m. the licensee entered i

Contrary

LCO 3.4.5.2to the above,ing tlat the RCS leakrate was greater than the TS

acknowledg

allowable limits but did not enter a NOVE until 8:20 a.m. when licensee

and NRC management reviewed the event. This is a violation of the above j

requirements and will be considered Violation 327,328/88-34-04. This

portion of URI 88-26-03 is closed.

The inspector reviewed AI-4, Preparation, Review, Approval and Use of Site I

Procedures / Instructions, for guidance on use of A0Is. Section 16.3 states  !

that:

'

A01s and Els are prepared to act as guides during potential

emergencies. They are written so that a trained operator will know ,

i

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19

i

in advance the expected course of events that will identify the

situation and will provide the immediate action to be taken.

It is the operator's res

particular situation is.ponsibility to analyzethe

Once identified andoperator

determine what

is to takethe

prompt appropriate action to prevent or mitigate the consequences of

a serious condition.

The inspector reviewed the operator training lesson plans associated with

A0I-6 for new license training and requalification training including both

classroom and simulator portions. Also, a selected nurrber of additional

AOI training lesson plans for licensed operators were reviewed. Training

appeared to be adequate and appropriate for the procedure usages. ,

,

Initiating documents for A0Is are not provided at Segouyah. The many

unique situations which could occur in the plant are too numerous to

provide instruction for every scenario. Therefore, the A0Is are designed

as symptom based instructions. The operators are trained on what

parameters may indicate a need to enter the procedure.

The inspector reviewed the event in question and determined that the

operators had handled it in an appropriate manner. There is no

requirement for an entry into the A01. Furthermore, discussions with the '

operators and training personnel have shown that a more significant

leakage event would have prompted A0I entry. This portion of URI 88-26-03

is closed.

,

Additional review of this event and licensee corrective actions and

responses will be reviewed under Violation 88-34-04. Therefore, URI

327,328/88-26-03 is closed.

10. ExitInterview(30703)

The inspection scope and findings were summarized on July 18, 1988, with L

those persons indicated in paragraph 1. The Senior Residents described  ;

the areas inspected and discussed in detail the inspection findings listed

below. The licensee acknowledged the ir,spection findings and did not  ;

identify as proprietar -

during the inspection.y any of the material reviewed by the inspectors

Inspection Findings:  :

Three violations were identified in paragraphs 7, 8, an 9.

One URI was identified in paragraph 4.  :

No deviations or inspector follow-up items were identified.  !

During the reporting period, frequent discussions were held with the Site

Director, Plant Manager and other managers concerning inspection findings. -

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No commitments were made by the plant manager or his designee during the

exit meeting.

11. List of Abbreviations

ABGTS- Auxiliary Buf1 ding Gas Treatment System

ABSCE- Auxiliary Building Secondary Containment Enclosure

AFW -

Auxiliary Feedwater

AI -

Administrative Instruction

A0I -

Abnormal 0)erating Instruction

AU0 -

Auxiliary Jnit Operator

A505 - Assistant Shift Operating Supervisor

BIT -

BoronInjectionTank

C&A -

Control and Auxiliary Buildings

CAQR- Conditions Adverse to Quality Report

CCP -

Centrifugal Charging Pu.sp

CCfS - Corporate Commitment Tracking System

COPS - Cold Overpressure Protection System

CSSC - Critical Structures, Systems and Components

CVI - Containment Ventilation Isolation

DC -

Direct Current

DCN -

Design Change Notice

DNE -

Division of Nuclear Engineering

DTVAP - DivisionofTVAProjects

ECCS - Emergency Core Cooling System

EDG -

Emergency Diesel Generator

EI -

Emergency Instructions

ENS -

Emergency Notification System

ESF -

Engineered Safety Feature

FCV -

Flow Control Valve

FSAR - Final Safety Analysis Report

G0C -

General Design Criteria

GL -

Generic Letter

HIC -

Hand-operated Indicating Controller

H0 -

Hold Order

HP -

Health Physics

IN -

NRC Information Notice

IFI -

Inspector Followup Item

IM -

Instrument Maintenance

IMI -

Instrument Maintenance Instruction

IR -

Inspection Report

KVA -

Kilovolt-Amp

KW -

Kilowatt

KV -

Kilovolt

LER -

Licensee Event Report

LCO -

Limiting Condition for Operation

LOCA - Loss of Coolant Accident

HI -

Maintenance Instruction

NB -

NRC Bulletin

NOV -

Notice of Violation

.

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21

NRC -

Nuclear Regulatory Commission

OSLA - Operations Section Letter - Administrative

OSLT - Operations Section Letter - Training

OSP -

Office of Special Projects

PMT -

Post Modification Test

PORC - Plant Operations Review Committee

P0RS - Plant Operation Review Staff

PRO -

Potentially Reportable Occurrence i

QA

-

Quality Assurance t

QC

-

Ouality Control  !

RCS -

Reactor Coolant System

RG -

Regulatory Guide .

RM -

Radiation Monitor

RHR -

Residual Heat Removal

RWP -

Radiation Work Permit .

RWST - Refueling Water Storage Tank '

SER -

Safety Evaluation Report

SG -

Steam Generator

SI -

Surveillance Instruction

S0I -

System Operating Instructions

SOS -

Shift Ooerating Supervisor

SQM

-

Sequoyah Standard Practice Maintenance ,

SR -

Surveillance Requirements

! SR0 -

Senior Reactor Operator l

STI -

Special Test Instruction

i

TACF - Teworary Alteration Control Room t

TROI - Tr s king Open Items i

TS

-

Technical Specifications I

TVA -

Tennessee Valley Authority

UO -

Unit Operator

URI -

Unresolved Item

.

USQD- Unreviewed Safety Question Determination

'

WCG -

Work Control Group

WP -

Work Plan

WR -

Work Request f

i

{

i Attachment.

Enforcement Conference Attendance (;
List and Licensee Slides

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, ATTACHMENT

,

. TENNESSEE VALLEY

AUTHORITY

.

SEQUOYAH NUCLEAR PLANT

EVENTS SURROUNDING

.

THE 2-FCV-87-21

UHI ISOLATION VALVE

! ISSUE

\ ,

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4

JULY 28,1988

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ATTENDANCE LIST

Enforcement Conference

July 28, 1988

Attendees

TVA

S. A. White R. L. Gridley J. R. Walker Ken Meade

J. R. Bynum N. C. Kazanas M. A. Cooper Ed Vigluicci

J. T. LaPoint M. J. Ray L. E. Martin J. B. Brady

S. J. Smith H. R. Rogers B. Charleson

NRC

J. Partlow B. Pierson

P. Harmon F. McCoy

K. Jenison K. Poertner

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SUMMARY OF EVENTS

UHI ISOLATION VALVE

.

02/15/88 SI 744 WRITTEN TO PROVIDE METHOD OF MONITORING CHARGES TO

ACCUMULATOR BASED ON WESTINGHOUSE ANALYSIS

03/88 PRE-CHARGED 2 FCV 87 21 N2 ACCUMULATOR TO 1382 psig PRIOR TO

ENTRY TO MODE 3 AND VERIFIED VALVE OPERABILITY

07/05/88 OPERATIONS NOTED ERRATIC PERFORMANCE OF 2 PIS 87 21 (HYDRAULIC

SYSTEM PRESSURE INDICATOR). WR B788800 WRITTEN TO REPAIR.

07/08/88 AT 1400, PORS HAD A DISCUSSION WITH NRC ON THE INOPERABLE

PRESSURE INDICATOR (2 PIS 87-21)

07/08/88 AT 1430 EDT, PIS REPA! RED AND HYDRAUUC SYSTEM PRESSURE FOUND

LOW (2647 psig). OPERATIONS RECHARGED TO 3034 psig. SYSTEM

ENGINEER NOTIFIED AT 1530 EDT.

07/08/88 AT 1830 EDT, PLANT MANAGEMENT WAS INFORMED OF THE LOW HYDRAULIC

SYSTEM PRESSURE AND DETERMINED A PRE CHARGE CHECK WAS THE

APPROPRIATE ACTION TO TAKE. MANAGEMENT DIRECTED SYSTEM

ENGINEERING / MAINTENANCE TO ESTABLISH A PLAN OF ACTION

TO PERFORM PRE CHARGE

l

l 07/08/88 AT 1930 EDT AND AT 0450 EDT ON 07/09/88, HYDRAULIC ACCUMULATOR

PRESSURE REACHED LOW SETPOINT (2970 psig) AND WAS RECHARGED

BY OPERATIONS

j 07/09/88 AT 1100 EDT, SCHRADER VALVE N BLADDER WAS CHECKED FOR

2

l LEAKS SMALL LEAKAGE NOTED.

07/09/88 AT 1300 EDT, HYDRAUUC ACCUMULATOR PRESSURE REACHED THE LOW

SETPOINT (2970 psig) AND WAS RECHARGED BY OPERATIONS. THIS

WAS THE FOURTH PHYSICAL CHARGE AND IN HINDSIGHT SI 198

SHOULD HAVE BEEN PERFORMED AT THIS POINT.

ROCUS1. 35

__ ._

*' ;

..

-

\

l

l

SUMMARY OF EVENTS

UH1 ISOLATION VALVE

(cont.)

.

07/09/88 AT 1800 EDT, CALLED NRC RESIDENT AT HOME TO DISCUSS AND

GIVE THE STATUS OF THE ACTION PLAN FOR REPAIR OF 2-FCV 87 21.

07/09/88 AT 1820 EDT, AT 2100 EDT, AND AT 0333 EDT ON 7/10/88,

HYDRAULIC ACCUMULATOR PRESSURE REACHED LOW SETPOINT

(2970 psig) AND WAS RECHARGED BY OPERATIONS.

07/10/88 AT 0930 EDT, PORS TALKED Wi1H THE NRC TO INFORM THEM OF

THE PROGRESS MADE AND THE ACTIONS REMAINING BEFORE VALVE

REPAIR WAS COMPLETED.

07/10/88 AT 1231 EDT, ENTERED LCO 3.5.1.2 TO PERFORM PRECHARGE ON

2 FCV 87-21 AND PERFORM MAINTENANCE ON SCHRADER VALVE.

NITROGEN PRESSURE WAS FOUND TO BE 1164.5 psig. LEAKAGE

FROM THE SCH1ADER VALVE WAS REPAIRED.

07/10/88 AT 1555 EDT, LCO 3.5.1.2 WAS EXITED. THE NITROGEN PRESSURE

WAS LEFT AT 1387 psig.

l 07/10/88 DNE WAS REQUESTED TO EVALUATE AS FOUND AFFECTS OF NITROGEN

PRESSURE ON RESPONSE TIME OF 2 FCV 87 21 AND ACCIDENT ANALYSIS.

07/11/88 WESTINGHOUSE EVALUATED THE CONDITION AND CONCLUDED THE LOW

NITROGEN PRESSURE AND SUBSEQUENT VALVE RESPONSE TIME IS

BOUNDED BY THE CURRENT UNIT 2 CYCLE 3 UHI ANALYSIS.

l

l

ROGERS 7, 35

1

,

-

".' ,

.

-

CONCLUSIONS

  • SI-196 ' PERIODIC CALIBRATION OF UPPER HEAD INJECTION SYSTEM

INSTRUMENTATION" IS THE INSTRUCTION WHICH RESPONSE TIME

HSTS THE SUBJECT VALVES TO PROVE OPERABILITY.

  • SI-744, "MONITORING OF UHI ISOLATION VALVE ACCUMULATOH PRESSURE,"

DID NOT CONTAIN SUFFICIENT INFORMATION TO PERFORM AN

ADEQUATE ASSESSMENT FOR VALVE OPERABILITY.

  • THE LEAKING SCHRADER VALVE CAUSED THE LOW NITROGEN PRESSURE AND

RESULTED IN GEVERAL RECHARGES PRIOR TO VERIFICATION OF PRECHARGE.

  • MANAGEMENT DETERMINED THAT A NITROGEN PRECHARGE WAS THE MOST

ACCURATE AND 5:"alENT WAY TO DETERMINE SYSTEM STATUS WITH

RCTCur TO ACCUMULATOR HYDRAULIC PRESSURE.-

  • MANAGEMENT INTERPRETED SI-744 TO INDICATE THAT A NITROGEN PRECHARGE

CHECK WAS AN ALTERNATIVE TO THE RESPONSE TIME TEST AFTER THE

FOURTH CHARGE.

  • THE NITROGEN PRECHARGE CHECK WAS PLANNED BUT NOT EXPEDITIOUSLY

PERFORMED.

l

( * OPERATIONS PERSONNEL RELY ON SYSTEMS ENGINEERING TO

I DETERMINE THE NUMBER OF CHARGES TO EACH UHI ISOLATION

l VALVE ACCUMULATOR AND WHEN ACTION IS REQUIRED.

  • DASED ON AN EVALUATION FROM WESTINGHOUSE, THE "AS FOUND' CONDITION

OF LOW NITROGEN PRESSURE DID NOT REPRESENT A SAFETY CONCERN.

i

l

P

j KONC.143

l

--- -- . . ---- _ . _ ._ . . . _ - - - - _ . . . _ _ . -- _ _ _ _ _ _

.

.'.

.

ASSESSMENT OF

SAFETY SIGNIFICANCE

  • 2 FCV 87-21 WAS CAPABLE OF PERFORMING iTS INTENDED

FUNCTION.

  • THERE WAS A MINIMAL EFFECT ON UHI ISOLATION VALVE STROKE

TIME DUE TO THE LOW NITROGEN PRESSURE IN THE VALVE

ACCUMULATOR. TESTING ON UNIT I INDICATED THE RESPONSE

TIMES WERE APPROXIMATELY .2 SECONDS SLOWER DUE TO THE

LOW PRESSURE.

  • THE UNIT 2 CYCLE 3 ANALYSIS INDICATES THE "AS FOUND'

CONDITION OF LOW NITROGEN PRESSURE IS BOUNDED EVEN

IF A SINGLE FAILURE OF THE REDUNDANT ISOLATION

VALVE IS ASSUMED.

  • THE REDUNDANT UHI ISOLATION VALVE, 2 FCV 87 22 WAS

OPERABLE DURING THIS EVENT.

  • A SECOND UHI INJECTION PATH WAS OPERABLE DURING

THIS EVENT

,

l

EATETf.143

_

'/. .'

.

.

ACTIONS

1.81-744 IS BEING REVISED TO PROVIDE ACTI

IN THE DETERMINATION OF.AUHI VALVE OPER

NUMBER OF CHARGES, DEPENDENT U

HITROGEN PRECHARGE.

2.

OPERATIONS

INTERPRET THE ACTIONSPERSONNEL

OF SI 744, WILL BE TRAINED

3.

AN EVALUATION WILL BE MADE CONCERNI E

HITROGEN PRESSURE IN THE ACCUMULATO

ADDITIONAL

CHECK CHARGES ARE ALLOWED BEFO

TEST IS REQUIRED.

4.

THE NON TS sis WILL BE REVIEWED AND REVIS

\

BE TAKEN IN THE EVENT THE A

ARE NOT MET.

5.

l

THE UHI SYSTEM REMOVAL PLAN WILL BE PURSU .

WESTINGHOUSE HAS PERFORMED PRELIMINAR

1 WHICH INDICATES THE UHI SYSTEM CAN .

\

i

\

\

\

S744, 143

-_- . --

*

.

.. .

-

.

ACTIONS

i

1.81-744 IS BEING REVISED TO PROVIDE ACTIONS TO AID

IN THE DETERMINATION OF UHI VALVE OPERABILITY. A

RESPONSE TIME TEST WILL BE REOUIRED AFTER A CERTAIN

NUMBER OF CHARGES, DEPENDENT UPON THE ORIGINAL

NITROGEN PRECHARGE.

2. OPERATIONS PERSONNEL WILL BE TRAINED ON HOW TO l

lNTERPRET THE ACTIONS OF SI 744.

3. AN EVALUATION WILL BE MADE CONCERNING INCREASING THE

NITROGEN PRESSURE IN THE ACCUMULATORS SUCH THAT

ADDITIONAL CHARGES ARE ALLOWED BEFORE A PRECHARGE

CHECK TEST IS REQUIRED.

4. THE NON TS sis WILL BE REVIEWED AND REVISED AS

APPROPRIATE TO CLARIFY THE ACTIONS WHICH SHOULD

BE TAKEN IN THE EVENT THE ACCEPTANCE CRITERIA

ARE NOT MET.

5. THE UHI SYSTEM REMOVAL PLAN WILL BE PURSUED.

WESTINGHOUSE HAS PERFORMED PRELIMINARY ANALYSIS

WHICH INDICATES THE UHI SYSTEM CAN BE REMOVED AT SON.

!

l

51744. 143

- _ - - _ - _ _ .

- _ _ _ _ _ _ _ _ _ _ ___ _ _

'

' ' *

.  : '; ;

-

.

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