ML20154P978

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Insp Repts 50-324/88-15 & 50-325/88-15 on 880401-30. Violation Noted.Major Areas Inspected:Followup on Previous Enforcement Matters,Maint & Surveillance Observations, Operational Safety Verification & in Ofc LER Review
ML20154P978
Person / Time
Site: Brunswick  
Issue date: 05/20/1988
From: Fredrickson P, Levis W, Ruland W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20154P965 List:
References
50-324-88-15, 50-325-88-15, NUDOCS 8806060144
Download: ML20154P978 (20)


See also: IR 05000324/1988015

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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101 MARIETTA STREET, N.W.

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ATLANTA, GEORGI A 30323

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Report No. 50-325/88-15 and_50-324/88-15

' Licensee: Carolina Pcwer and Light Company

P. O. Box 1551

Raleigh, NC 27602

' Docket No. 50-325 and 50-324

License No. DPR-71 and=DPR-62

Facility Name: Brunswick 1 and 2

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Inspection Co uc ed: April 1 - 30, 19 8

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Inspectors:

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Accompanying Pe son el:. S. Schaeffer

Approved by:

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P. E. Fredrickson,3ec~tWChWf

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Division of Reactor Projects

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SUMARY

Scope:

This routine safety inspection by the resident inspector involved the

areas of followup on previous enforcement matters, maintenance observation,

surveillance observation, operational safety verification, onsite review

comittee, in office Licensee Event Report (LER) review, followup cn inspector

identified and unresolved items, information meeting with local officials,

plant startup from refueling, and onsite followup of events.

]

Results:

One violation. was identified - Improper change in operational

condition during startup of Unit 2.

Several examples of failure to follow

procedure were included as part of the overall violation. Two unresolved items

were identified:

questions concerning procurement of comercial grade items

for safety-related applications; questions concerning qualification of

Victoreen Radiation Detector Cable.

A significant safety issue concerning cracking of silicon bronze bus bar bolts,

first identified in Inspection Report 324,325/88-05, was inspected further.

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REPORT DETAILS

1.

Persons Contacted

' Licensee Employees

-W. Biggs, Principal Engineer

  • E. Bishop, Manager - Operations

T. Cantebury, Mechanical Maintenance Supervisor (Unit 1)

G. Cheatham, Manager - Environmental & Radiation Control

R. Creech, I&C/ Electrical Maintenance Supervisor (Unit 2)

C. Dietz, General Manager - Brunswick Nuclear Project

P. Dorosko, Administrative Supervisor

W. Dorman, Supervisor - QA

  • R. Eckstein, Manager - Technical Support

K. Enzor, Director - Regulatory Compliance

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R. Groover, Manager - Project Construction

W. Hatcher, Supervisor - Security

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A. Hegler, Superintendent - Operations

  • R. Helme, Director - Onsite Nuclear Safety - BSEP
  • J. Holder, Manager - Outages

P. Howe, Vice President - Brunswick Nuclear Project

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L. Jones, Director - Quality Assurance (QA)/ Quality Control (QC)

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R. Kitchen, Mechanical Maintenance Supervisor (Unit 2)

J. McKee, Supervisor - QC

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J. Moyer, Manager - Training

G. Oliver, Manager - Site Planning and Control

  • J. O'Sullivan, Manager - Maintenance
  • B. Parks, Engineering Supervisor
  • R. Poulk, Senior NRC Regulatory Specialist

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  • A. Richards, Project Engineer - QA
  • S. Scharff, Operations Engineer
  • J. Simon, Operations Engineer

J. Smith, Manager - Administrative Support

V. Wagoner, Director - IPBS/Long Range Planning

R. Warden, I&C/ Electrical Maintenance Supervisor (Unit 1)

D. Warren, Acting Engineering Supervisor

B. Wilson, Engineering Supervisor

  • T. Wyllie, Manager - Engineering and Construction

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Other licensee employees contacted included construction craftsmen,

engineers, technicians, operators, office personnel, and security force

members.

  • Attended the exit interview

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2.

ExitInterview.(30703)

The inspection scope-and findings were summarized on April 29, 1988, with

those persons indicated in paragraph 1.

The inspectors described the

areas- inspected and discussed in detail the inspection findings listed

below.

Dissenting coments were not received from the licensee.

Proprietary information is not contained in this report.

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Item Number

D e s cL p_t i o n1R e fe r_e_n c e_ Pa ra g ra p h

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324/88-15-01

VIOLATION - Improper Change In Operational

Condition (paragraph 11.b.(2)

325/88-15-02 &

  • URI - Procurement of Conrnercial Grade Items

324/88-15-02

Intended for Safety-Related Applications

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(paragraph 4.a)

324/88-15-03

URI - Qualification of Victoreen Radiation

Detector Cable (paragraph 11.b.(1)

325/88-15-04 &

IFI - Failures of GE 305 Auxiliary Contact Adder

324/88-15-04

Blocks (paragraph 12.a)

325/88-15-05

IFI - Normal Position for SW-V117, Nuclear Header

to Vital Header Isolation Valve'(paragraph 4.a)

325/88-15-06 &

IFI - Silicon Bronze Bolts in Safety-Related

324/88-15-06

Switchgear(paragraph 12.b)

Note:

Acronyms and abbreviations used in the report are listed in

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paragraph 13.

3.

Followup on Previous Enforcement Matters (92702)

(CLOSED)

Violation 325/87-20-04 and 324/87-20-04, Failure to Implement

Procedures.

The inspector reviewed the licensee's response dated

September 25, 1987.

The inspector verified that the licensee implemented

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the required corrective actions.

All procedure documentation changes as

well as procedure adequacy reviews were completed.

In addition, for

example b, of this violation, the inspector _ also interviewed selected

engineering and training personnel and concluded that appropriate emphasis

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was placed on increased procedural training in the area of OP-19, High

Pressure Coolant Injection System Operating Procedure, Section 5.3, Manual

Startup.

  • An UnresoWd'Ttem is a matter about which more information is required to

determine whether it is acceptable or may involve a violation or deviation.

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4.

MaintenanceObservation(62703)

The inspectors observed maintenance activities, interviewed personnel, and

reviewed records to verify that work. was conducted in accordance with

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approved procedures, Technical Specifications, and applicable industry.

codes and standards.

The inspectors also verified that:

redundant

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components were operable; administrative controls were followed: -tagouts

were adequate; personnel were qualified; correct replacement parts were

used; radiological controls were proper; fire protection was adequate;

quality control hold points were adequate and observed; adequate

post-maintenance testing was performed; and independent verification'

requirements were implemented. The inspectors independently verified that

selected equipment was properly returned to service.

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Outstanding work requests were reviewed to ensure that the licensee gave

priority to safety-related maintenance.

The inspectors observed / reviewed portions of the following maintenance

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activities

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Oil changeout on HPCI booster pump - ticket 88-QMK205.

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Troubleshooting efforts of F004,1-SW-V117, F041 valves.

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Troubleshooting efforts of Unit 1 Recirc. MG set field break'er.

a.

While watching oil changeout of Unit 1 HPCI booster pump on April 21,

1988, the inspector questioned licensee personnel as to which

documents specified the lubricant type and what controls were in

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place to ensure that the proper lubricant was used.

Th'e inspector

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found that the oil type for this component is specified in OPM -

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LUB500ATT211.

This document states that DTE 797 is the proper

lubricant with an annual changeout' requirement.

The' inspector then

verified that DTE 797 was used and traced down the purchase order of

the lubricant to determine how the lubricant was procured.

The

inspector noted that purchase order 3720588A, dated February 2, 1987,

specified that the item be procured as an "Off the Shelf" item, which

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rreant that the vendor was not required to be on the approved

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supplier's list.

The receipt inspection performed en this purchase

verified only that the part ordered matched the part received.

No

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other quality requiremer ts were specified.

ENP-42.2, Revision 1, dated January 6, 1988, Purchase Requis'ition and

Data Base Review Procedure, defines a Q-0TS (Off the Shelf) item as a

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comnercial grsde item used in safety-related applications.

ENP-42.3,

Revision 1,

aud January 6,1988, Material Engineering Evaluation

Procedure, 'tep / 2.3.4, requires that a documented evaluation, which

includes idt< *it, ing the components critical characteristics, be

perfonned, when it is decided to procure an item comercial grade

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that is. intended for safety-related applications. Step 7.2.9 of the

same procedure requires that special receipt instructions,- which

should verify the component's critical characteristics, be specified.

The inspector then questioned licensee personnel concerning why these

requirements were not followed with respect to the DTE 797 oil as no

documented engineering evaluation was found and no special receipt

inspection requirements were noted.

The licensee responded that

these requirements only went into effect in October 1987, and that

any items procured prior to this time would not have been subject to

these procedures.

However, the licensee .was able to provide

information to the inspector which showed the lubricant used in the

HPCI booster pump to be of the proper type.

The possibility exists

though, that there are commercial grade items presently in stores

intended for safety-related applications in which a proper

engineering evaluation has not been performed.

The licensee had

previously -identified programmatic procurement deficiencies in NCR

No. A-87-023 which is still ope 1.

This item is Unresolved pending-

NRC review of the licensee's corrective action for the NCR:

Procurement of Commercial Grade Items Intended for Safety-Related

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Applications,(325/88-15-02and324/88-15-02),

b.

On April 20, 1988, during maintenance surveillance testing, the

licensee experienced a failure of 1-E41-F041, the HPCI Outboard

Suppression Pool Suction Valve. Under accident conditions this valve

is required to open on low CST level or high suppression pool level

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to provide an alternate suction path for HPCI.

Troubleshooting

revealed that the series field had been shorted to ground.

No

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evidence of actuator or valve problems were found that may have

caused the failure.

The motor was then sent to Harris E&E for

analysis.

It should be noted that the licensee has experienced other DC motor

failures (see LER 1-87-23) and has committed to a followup report on

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the above LER by July 1,1988, to explain any root cause of these

motor failures. The inspectors will continue to followup on licensee

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tctivities in this area.

c.

On April 23, 1988, while performing maintenance activities on the

Nuclear Service Water Vital Header, the Vital Header Motor Operated

Isolation Valve, 1-SW-V117, failed to open when manually activated by

the control switch.

Under accident conditions this valve opens to

provide Nuclear Service Water to the Core Spray Pump room cooling

units, the RHR Pump room cooling units and to each RHR Pump Seal

Cooling Heat Exchanger.

Troubleshooting efforts by the licensee

which included motor checks and control logic checks showed a limit

switch problem.

The contacts on limit switch rotor No.1 were

cleaned after which the valve was satisfactorily cycled from the RTGB

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and also with the remote keylock switch.

The inspectors will

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followup licensee activities withlespect to their determinatdin if

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the valve should be open rather than closed, duping nonnal oMration.

141s is an Inspector Followup Item:

Nonnal Positinn for 5If117, /

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Nuclear Header to Vital Header Isolation Val 77(ry/%-154W.

No signif cant.s'afety matters, violations or devit dgns dre identified.

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5.

Surveillarge Jhservation (61726).

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The inspectors observed surveillance testing required by Technical

Specifications.

Through observation, intfrviews, and record review, the

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inspectors verified that:

tests conformed ^.w Tych leal Specification

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requirements; adQistrative1 controls were'

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qualified; lipstruuqtation was calibrated; 'an

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complete.

lhe inspectors independently verified he ected pf

esults and-

proper return to service of equipment.

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The inspectors witnessed / reviewed portions of the' following ^ t'est

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activities:

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HP'CI Operability Test

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PT-10.1.3

RCIC' System Operability Tes:' N Flow Rates at 150 PSIG

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Control Rod Coupling Check and CRD Testing .'

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', .(?gquence Critical Shutdown MarginMlculation, Rev. 4

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PT-20.8

AI,N.rosen' Backup System Operability Test

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PT-71.0

' General Atomic Stack Radiatija Monitor Channel dlibration ,,(f s

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No significant safety matters, violations, or deviations were 1/jptified.

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6.

OperationalSNetyVerification(71707)

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The inspectors perified that Unit 1 and Unit 2 were operated in ,cabYiance

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withTechnical,.SpecificationsandotherreguJatoryrequirementsbydirect

observations of lactivities, ucility tours.; discussions with personnel.

reviewingofrecordstrv}independentverificationofsafetysystemstatus,

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The inspectoh verified that control room manning requirements of 10 CFR 50.54 and the Technical Specifications were met.

Control operator, shift

supervisor, clearance, STA, daily and

landing instructions, and

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jumper / bypass logs were reviewed to obtait information concerning

operating trends and out of service safety systems to ensure that there

~ were no conflicts with Technical Specifications Limiti79 Conditions foh

Operat' ions .

Direct observations were conducted of co rol room panels,

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rin trtdientation and recorder traces important to safety to verify

operability and that operating parameters were within Technical

Specification limits.

The inspectors observed shift turnovers to verify

that continuity of system status was maintained. The inspectors verified

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the status of selected control room annunciators.

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Operabilit

weekly by'y of a selected Engineered Safety Featur'e division was verified-

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insuring that:

each accessible valve in the flow path was in

its correct- position; each power supply and breaker was closed' for

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components that must activate upon an initiation signal; the RHR subsystem

cross-tie valve- for cach unit was closed with the power removed from the

valve operator; there was no leakage of major components; there was proper-

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lubrication and cooling water available; and a condition did not exist

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which might prevent fulfillment of the system's functional requirements.

Instrumentation essential to system actuation or performance was verified

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operable by observing ori-scale indication and proper instrument valve

lineup, if accessible.

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The

insrctors -verified

that the licensee's health physics

policies / procedures were followed.

This included observation of HP

practices and a review of area surveys, radiation work permits, posting,

and instrument calibration.

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The inspectors votified that:

the security organization was properly

manned and security personnel were capable of performing their assigned

functions; persons' and packages were checked prior to- entry into tN

protected area; vehicles were properly authorized, searched and escorted

within the PA; persons within the PA displayed photo identification

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badges; personnel in vital areas were authorized; and effective

compensatory measures were employed when required.

The inspectors also observed plant housekeeping controls, verified

position of certain containment isolation valves, checked a clearance, and

verified the operability of onsite and offsite emergency power sources.

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The inspector found the limit switch cover not completely screwed down for

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valve 1-CAC-V7, the Inboard Suppression Pool Purge Exhaust Valve.

This

installation is not in accordance with the design drawings or normal

installation practices which require the cover to be tightened

sufficiently to ensure the

"0" ring is seated. The licensee has generated

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NCR A-88-012 to track and resolve this issue.

The inspector will continue

to followup in this area in future routine inspections.

No significant safety matters, violations, or deviations were identified.

7.

Onsite Review Comittee (40700)

The inspector attended -pre-startup Plant Nuclear Safety Comittee meeting

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88-047 conducted on Apdl 13, 1988.

The inspectors verified that the

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meeting was conducted in accordance with Technical Specification

requirements regarding quorum membership, review process, and personnel

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qualifications.

lieeting minutes were reviewed to confirm that

decisions /reconmendations were reflected in the minutes and followup of

-corrective actions was documented.

No significant safety matters, violations, or deviations were identified.

8.

In Office Licensee Event Report Retiew (90712).

The listed LER was reviewed to verify that the information provided met

NRC reporting requirements.

The verification included adequacy of event

description and corrective action taken or planned, existence of potential

generic problems and the relative safety significance cf the event.

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(CLOSED) LER 1-88-09, Accidental Deenergization of Unit 2 Process Off-Gas

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Radiation Monitor and Reactor Building Ventilation Exhaust Radiation

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Monitors During Maintenance.

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No significant safety matters, violations, or deviations were identified.

9.

Followup on Inspector Identified and Unresolved Items (92701)

a.

(CLOSED)

Unresolved Item 325/87-11-02, Mispositioned Equalizing

Valve for IB RHR/SW HX DPT.

The inspector reviewed OER-87-20,

approved on June 26, 1987, which adequately detailed the events

concerning the mispositioned valve.

The licensee has revised AI-58

and ENP-03 in order to improve clearance tag sheet verification as

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well as requiring independent verification in the acceptance test

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section of the plant modification, as opposed to BESU's past practice

of taking credit for the clearance and/or system lineup at the

completion of the unit outage. The inspector concluded that the root

causes of the event have been identified and corrected, including

action to prevent recurrence.

Since the licensee has met all the

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conditions of 10 CFR 2, Appendix C, regarding licensee identified

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violations, no notice of violation will be issued,

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b.

(CLOSED)

Inspector Followup Item 325/86-24-05 and 324/86-24-05,

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Review RHR Room Cooler Operation.

The inspector reviewed EER No.

86-0460, completed on July 24, 1987, which included detailed RHR Room

Cooler Operation Analysis.

The licensee has issued TSI-87-02, dated

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August 28,

1987, which provides

operator

instruction for

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administrative equivalent TS LC0 implementation.

The inspector has

no further concerns with this issue.

c.

(OPEN)

Inspector Followup Iten 325/86-33-01 and 324/86-33-01, IRM

Fuse Testing and Subsequent Required Modifications.

The inspector

reviewed the content and results of SP-86-068, Revision 2 (Unit 1),

which was performed on January 19, 1987.

The test results

SP-86.073 (Unit 2) proved the

concerns in GE SIL No. 445 were valid.

, was not

run because the licensee concluded that plant modifications were

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required.. To assure pre-modification operability, SP-87-014 was

performed on February 12, 1987, and verified that applicable portions

of surveillance procedures MST-IRM11W and 12W would-detect a blown -

-24 volt DC fuse (F2) in the IRM.

EWR-04527 and PID No. 5400A have

been -issued and completed to- develop the plant modification.

The

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licensee plans to modify the system by December 8, _1989.

The

inspector concluded that the _ licensee's actions to address the SIL

issues have been appropriate.

This item will remain open pending

completion of the modifications,

d.

(CLOSED)

Inspector Followup Item 325/87-03-03, Review 'of IMST-DG12R

Procedure Violation OER.

The' inspector reviewed- the licensee's

OER-87-09, dated -' April 28, 1987, which addressed the root cause of-

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'the communication failure between the I&C personnel in charge of the

test and the control operator.

The licensee concluded that the test

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director had been given too many tasks.

The DG Load Test MSTs 11R

through 14R for Units 1 and 2 were revised on May 4,1987, to

incorporate lessons learned and a ~ redistribution of the-procedural

steps to allow verifications to be done in other locations separate

from the Control Room.

The inspector concluded that the licensee's

corrective actions were appropriate,

e.

(OPEN)

Inspector Followup Item 325/87-03-04, Inadequate Board

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Walkdown and Review.

The licensee has issued Standing Instruction

87-014, dated February 13, 1987, which requires the shift foreman or

the shift operating supervisor to walk the Control Board with the

respective control operator in order to double check RTGB indication

and enhance SR0 awareness of plant status.

The licensee has also

secured general business activity at the shift foremar, window for an

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hour during shift turnover, to reduce distractions.-

The initial

cause of the mispositioned valve has been corrected via procedure

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revision OP-17, Revisions 12 and 68, respectively. for Units 1 and 2.

This item will remain open until the requirements specified in

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SI-87-014 are incorporated into the licensee's permanent procedures.

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(CLOSED)

Inspector Followup Item 325/87-06-01. Review Motor-Driven

Fire Pump Breaker Misalignment OER.

The inspector reviewed the

completed OER-87-10 and concluded that the root cause~ determination

and corrective actions taken were appropriate.

The licensee issued

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an LC0 declaring the motor-driven fire pump inoperable for over 38

hours.

No LC0 Action Statement time limitation was exceeded during

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the event.

The 4160 breaker misalignment occurred because OP-41,

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Fite Protection and Well Water System, was unclear.

The positions in

OP-41 have been revised as of May 19, 1987, to include a more

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specific description of nonnal breaker position.

This problem

appears to be unique at Brunswick to the motor-driven fire pump.

g.

(OPEN)

Inspector Followup Item 325/87-06-02, Repair of Diesel

Generator Exhaust Silencers.

The inspector examined the rusted

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bottom of the exhaust silencers and does not consider the condition

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to adversely affect the operability of the diesels at this time. The

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licensee plans to replace the silencers by December 1,1988, to

prevent any potential problems.

This item remains open pending

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installation of the new silencers.

h.

(CLOSED)

Inspector Followup Item 325/87-06-03, Documentation of

Welding Associated with LER 1-84-02.

The inspector was unable to

obtain any information regarding additional. welding records

associated with the repair of the EHC.

The inspector reviewed the

as-is LER package which contained the EWRs, trouble tickets, design

drawings, and certain portion; of the welding documentation.

Appendix'B does mot apply to the non-safety EHC system,

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(CLOSED)

Inspector Followup. Item -325/87-20-01 and 324/87-20-01,

Enhancement of PID Tracking.

The licensee has developed a .PID

tracking program which includes identification through acceptance -

milestones and the accompanying research of- late itens.

The

inspe'ctor reviewed DI-LRP-21, Revision 0, dated December 21, 1987,

which provides the procedural documentation of the administrative

controls relative to the PID tracking system, and found them to be

adequate.

The new system also identifies and tracks PIDs that have

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been accepted, but remain open for completion of the defined scope.

Site procedure BSP-14, BSEP Project Identification, is currently

being revised to incorporate the changes to the PID process.

This

revision is to be completed by June 30, 1988.

No significant safety matters, violations or deviations were identified.

10.

Information Meeting With Local Officials (94600)

The inspectors and the project section chief explained the NRC's role and

inspection program to local officials. Meetings were held with members of

the New Hanover County Commission on April 14, 1988, and with the Chairman

of the Brunswick County Commissioners on April 15, 1988.

The project

section chief described the NRC inspection progrco to the City of

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Southport board of aldermen at their regularly scheduled monthly meeting

on April 14, 1988.

2

The inspectors and section chief visited the local public document room at

the University of North Carolina at Wilmington.

The collection was well

4

maintained and in order.

The cognizant librarian stated that collection

4

use averaged 1 person per month. The inspectors had no further questions.

11. Plant Startup from Refueling - Unit 2 (71711)

,

The inspectors reviewed / observed activities associated with Unit 2 startup

after the refueling outage to determine if activities were conducted in

,

accordance with approved procedures.

The inspection included a review of

the changes to GP-01, Revision 105, Startup Checklist; direct observation

of startup and approach to criticality; observation of selected

.

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10

surveillance -tests; . review of licensee's drywell closecut inspection '

'

results with independent drywell inspection; examination of selected

systems to assure startup readiness; and review of selected modification

training packages.

,

a.

Specific inspection items included:

(1) Training

During the refueling outage for Unit 2, the Alternate Rod

.

Injection system was installed under PM-86-035 to comply with 10 CFR 50.62, the:ATWS rule.

The purpose of the ARI system is to

initiate a reactor _ scram by' a means independent of 'the Reactor

Protection System.

Four_ additional vent paths have been

~ installed on the scram outlet valve air header, with each of the

four vent paths consisting of two solenoid valves in series.

The system is automatically initiated from ARI logic or can be

manually initiated, if required.

The inspector reviewed the modification-training package, sample-

examinations and examination test results to determine the

adequacy and completeness of the training conducted for those

operators licensed on Unit 2.

(2) Valve Lineups

The completed valve lineup sheets for the Control Rod Drive and

the Standby Liquid Control System were reviewed to assess their

completeness.

In addition, the inspector physically verified

the valve positions of the SLC system valves.

(3)

Inspection

'

Several areas were inspected that are normally high radiation

areas to look for housekeeping and general material conditions.

1

The areas inspected included the HPCI roof, RCIC steam tunnel

and the 66 foot penetration room.

,

(4) Drywell Closeout

j

The inspector reviewed licensee preparations for closing out the-

drywell. Administrative Procedure, AP-96, Drywell Closecut, was

the governing procedure.

The inspector reviewed those

>

discrepancies identified by the licensee along with their

corrective action.

In addition, a physical inspection of the

i

drywell was performed to verify that licensee actions were

adequate.

)

i

j

1

.

.

..

.-

.

1-

11

b.

Inspection findings were as follows:

(1) Victoreen Radiation Detector Cable

During the drywell inspection closecut, the inspector noted that

i.he installed configuration of the Victoreen high range

radiation monitor differed from the tested configuration as

documented in Victoreen report 950.301.

Specifically, the

<

method of terminating the cable to the detector, the cable

manufacturer and lack of a sealed conduit system for the

detector cable, all differ from that which was tested.

The

termination method and use of a sealed conduit system by

Victoreen in their test program was crucial to the successful

completion of the test as evidenced by the numerous - test

failures experienced in previous testing without -this

configuration.

The licensee did provide some information to the

inspector describing the differences between their termination

means and that which was tested and the specific measures taken

to preclude moisture entry to the connector area.

No

information has been provided which demonstrates that the

installed cable which is supplied by a different manufacturer

and is not installed in sealed conduit, is acceptable for this

application.

This item is unresolved and is listed as

Unresolved Item: Qualification of Victoreen Radiation Detection

Cable,(324/88-15-03).

(2)

Improper Change In Operational Condition

l

While observing startup preparations being made for Unit 2

startup on April 26, 1988, the inspector first noted at about

2:45 p.m. that the Reactor Mode Switch was in the Startup/ Hot

Standby position.

Licensee personnel explained that the switch

was in this position because of previous testing performed on

the Rod Sequence Control System and the Rod Worth Minimizer and

that it was left in this position because their procedures

-

allowed this if reactor startup would commence shortly.

The

testing was completed at 9:45 a.m.

Startup commenced at 4:00

p.m.

A detailed sequence of events for both the control room

'

personnel and the NRC inspector is contained in enclosure 2.

This enclosure also addresses appropriate procedures and steps

utilized during the evolution.

The Rod Worth Minimizer Periodic Test 1.6.2-2, Step 7.1.23,

states to place the mode switch in SHUTDOWN unless the shif t

foreman verifies that the prerequisites are met for leaving the

{

mode switch in START /H0T STANDBY pending reactor startup.

The

,

Rod Sequence Control System Operability Periodic Test 1.6.1,

which was performed after the Rod Worth Minimizer Test, did not

]

contain this step. - At 9:45 a.m., following completion of the

testing, the following prerequisites had not been met for

i

etartup:


--

.

.

12

o

RHR Division II not lined up for automatic LPCI initiation.

The "B" RHR loop was in the shutdown cooling mode at this

time and not lined up for automatic LPCI initiation.

At

2:03 p.m., the licensee stopped the RHR "B" pump to secure

the shutdown cooling mode of RHR and line it up for LPCI

initiation in accordance with Section 7.2 of OP-17.

The

licensee completed steps through B.4 in this procedure

(starting recirculation pumps) at 2:53 p.m.

Steps 5

through 16, which would have completed the restoration and

lined up the system for automatic LPCI initiation, were not

continued at this time.

At 3:03 p.m., GP-1 was signed off

by the SF and SOS stating that all prerequisites for

startup had been met.

A PA announcement was made that

primary and secondary containment was in effect and that

reactor startup was commencing. GP-2 was entered and steps

5.2.4, 5.2.5 and 5.2.6 were completed. The next step, step

5.2.7, states to withdraw control rods.

At this time the

NRC inspector noted that the RHR system had still not been

restored.

Specifically, he noted that the suppression pool

suction valves F0208, F004B and F004D were shut.

These

valves do not receive an open signal during LPCI

initiation.

When questioned about this configuration, the

SF directed his people to restore the lineup.

Steps

7.2.B.5 through 16 of OP-17 were completed at 3:46 p.m.

GP-1 was then signed off at 3:46 p.m. and reactor startup

commenced at 4:00 p.m.

i

o

Nitrogen backup system inoperable.

The nitrogen backup system supplies a pneumatic source to

selected safety-related loads.

Following a LOCA and

subsequent containment isolation, the normal air supply to

the drywell will be isolated and supply will be from the

nitrogen backup system to the suppression pool to reactor

building vacuum breaker and the SRVs.

This system was

tagged out in accordance with the requirements of OG-3,

Primary Containment Access Control, which describes the

requirements for allowing personnel entry into the drywell.

This procedure requires that RNA-SV-V5251 and RNA-SV-V5253

be closed and placed under SF clearanc- if the plant is in

Condition 1, 2, or 3 or that the nitrereu backup isolation

s

valves, RNA-V347 and RNA-V348 be tagged closed if the plant

is in Condition 4 or 5.

Clearance 2-13578 was hung at 4:25

a.m. on April 25, 1988, placing a tag on the control

switches (closed) to 2-RNA-SV-V5251 and 2-RNA-SV-V5253.

These valves supply air to the non-interruptible air header

which supplies the SRVs.

These valves open on loss of

power.

The plant was in Condition 1 at the time the

clearance was hung.

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13

.

Although the safety significance of this clearani.e being in

effect during the mode change is small, since the plant was

not at pressure and the'SRVs were not required, the system

was part of an active LC0 (A2-88-0716) and should have:been

cleared prior to any mode-change .

o

Primary Containment - Airlock Door Surveillance .Not

Completed.

PT-2.6.6 was completed at 11:11 a.m.

This test verifies

,

that the drywell airlock is operable.

It was necessary to

1

perform this test since the airlock was previously made-

inoperable to support welding work . performed in the

drywell.

During this mode change period, therefore,

primary: containment was not in effect as required by the

plant's Technical Specifications.

!

This startup showed several examples of failure to follow

!

procedures, e.g., signing off OP-1 before it was complete, not

J

finishing 0P-17, not following the' instructions of PT-1,6.2-2.

In addition, it showed an inccrrect interpretation of their

t

Technical Specifications regarding testing the Rod Worth

Minimizer and the Rod Sequence Control System.

The Technical Specifications, Section 3.1.41 and 3.1.4.2, state that "Entry

into Cor.dition 2 and withdredal of selected control rods is

permitted for the purpose of determining operability of the RWM

i

(RSCS) prior to withdrawal of control rods for the purpose of

.

bringing the reactor to criticality."

The licensee interpreted

this statement as allowing the mode switch to be placed in

,

"startup" for testing purposes.

This requirement addresses

l

entry into Condition 2 which means that the prerequisites for

t

meeting that mode change must be satisfied.

,

The licensee's position was that, although procedurally

f

permitted, they would not have pulled control rods with' the

Division II RHR system not lined up for automatic LPCI

-

s

i

initiation.

During startup evolutions, the licensee stations an

,

j

additional SR0 in the control room to oversee startup

activities.

Although his tasks are not administratively

,

1

defined, the licensee states that this individual was aware that

l

the LPCI lineup had not been restored and he would have

i

prevented pulling control rods without the system lined up for

automatic initiation.

1

This matter is a Violation of the licensee's Technical

1

i

Specifications: Improper Change In Operational Condition,

'

(324/88-15-01).

i

One violation and no deviations were identified.

A failure in the

l

licensee's administrative control of startup prerequisites was identified.

.

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- 14

12. Onsite Followup of Events (93702)

a.

Auxiliary Contacts in Motor Control Centers Breakers

GE _has found a potential-failure +. ode of an auxiliary contact block

assembly used with contractors 'in safety-related motor. control

'

centers.

The licensee had previously -identified a problem with

auxiliary contAt blocks (CR-205 device) in early _1987 (see LER

,

1-87-01).

The CR-205 ' devices were sticking,-preventing

. motor-operated valve operation.

The licensee replaced all CR-205

-devices in important safety-related applications with a newer design

'

CR-305 device which was not susceptible to the CR-205 failure mode.

However, .the licensee has found three sticking--305 devices since

-

April 6,1988; two failed during replacement installation.

GE -

.L

Bloomington's initial assessment indicates that- the manufacturing

process was creating small burrs on the moving parts, resulting in

the failures.

GE has modified the process and slightly re-designed

the part to fix the problem.

,

The licensee immediately inspected .133 important safety-related

breaker compartments and verified that no installed 305 device was

'

,

sticking.

On April 29, 1988, in a conference call.with Region Il

management, the licensee reported that they had again inspected (a

week from previous inspection),133 important safety-related breaker

compartments and verified that no installed 305 device was sticking.

In addition, they described their test program of the- 305 devices

being conducted jointly with General Electric. The testing began on

April 28 to verify the failure rate of the old and new 305 devices.

The testing results will determine if the licensee's intention to

-

replace the old 305 devices with new 305 devices on an "as failed"

,

basis or during preventative maintenance should be modified.

The inspectors will continue to follow the licensee's actions

regarding auxiliary contractors.

This is an Inspector Followup Item:

Failures of GE 305 Auxiliary Contact Adder Blocks (325/88-15-04 and

324/88-15-04).

b.

Silicon Bronze Bolts in Safety-Related Switchgear

The licensee infomed the inspector on April 19, 1988, that the

broken and cracked bolts (see report No. 325,324/88-05) had failed'

due to intergranular stress corrosion cracking instead of excessive

torque.

This determination was made through metallurgical analysis

conducted by the Harris E&E Center.

The licensee, in a conference

call with NRC personnel on April 29, 1988, stated that they would be

replacing the 5/16 inch silicon bronza carriage head bolts with mild

steel bolts in all safety-related electrical panels except the DC

switchbeards by May 17, 1988; the DC switchboard plan would be ready

in 30 days.

This is an Inspector Followup Item:

Silicon Bronze

BoltsinSafety-RelatedSwitchgear(325/88-15-06and324/88-15-06).

.

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No significant safety matters, violations or' deviations were identified.

13. List of Abbreviations for Unit 1 and 2

AI

Administrative Instruction

A0.

Auxiliary Operator

ARI-

Alternate Rod Injection

ATWS

Anticipated Transient Without Scram

,

BESU

Brunswick Engineering Sub Unit

BSEP

Brunswick Steam Electric Plant

+

BSP

Brunswick Site Procedure

C0

Control Operator

CP&L

Carolina Power and Light Company

CRD

Control Rod Drive

CST

Condensate Storage Tank

,

DC

Direct Current

DG

Diesel Generator

DPT

Differential Pressure Test

-

E8E

Energy and Environmental

EER

Engineering Evaluation Report

EHC

Electro Hydraulic Control System

ENP

Engineering Procedure

ERFIS

Emergency Response Facility Information System

ESF

Engineered Safety Feature

EWR

Engineering Work Request

,

F

Degrees Fahrenhtit

'

,

i

GE

General Electric

j

GP

General Procedure

,

lj

HP-

Health Physics

HPCI

High Pressure Coolant Injection

'

HX

Heat Exchanger

I&C

Instrumentation and Control

IE

NRC Office of Inspection and Enforcement

,

IFI

Inspector Followup Item

IPBS

Integrated Planning Budget System

IRM

Interrediate Range Monitor

i

i

LC0

Limiting Condition for Operation

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

LPCI

Low Pressure Coolant Injection

MG

Motor Generator

,

MST

Maintenance Surveillance Test

.

NCR

Non-Conformance Report

4

NRC

Nuclear Regulatory Conrnission

OER

Operating Experience Report

j

OP

Operating Procedure

i

OPM

Operating Procedure Manual

PA

Protected Area

!

PID

Project Identification

PM

Plant Modification

.

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16

PNSC

Plant Nuclear Safety Committee

PSIG

Pounds per Square Inch Gauge

PT

Periodic Test

QA

Quality Assurance

QC

Quality Control

RCIC

Reactor Core Isolation Cooling

RHR

Residual Heat Removal

RSCS

Rod Sequence Control System

RTGB

Reactor Turbine Gauge Board

RWM

Rod Worth Minimizer

RX

Reactor

SF

Shift Foreman

SI

Standing Instruction

SIL

Service Information Letter

SLC

Standby Liquid Control

SOE

Sequence of Events

SOS

Shift Operating Supervisor

SP

Special Procedure

SR0

Senior Reactor Operator

STA

Shift Technical Advisor

S/U

Startup

SW

Service Water

TS

Technical Specification

TSI

Technical Specification Interpretation

URI

Unresolved Item

j

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4

ENCLOSURE _2

U-2 Startup Sequence of Events for 4/26/88

Initial Conditions: All rods in, Reactor temperature 180 degrees F Reactor

Coolant System depressurized with manual head vents open.

Procedure _ Step

Time

Action

Mode switch in S/U for testing) pts

0435

1.6.1 and 1.6.1-2 (from C0's log

2041

PT-1.6.1 complete (RSCS - from SF log)

(0945 from GP-1, Attachment 1)

1046

PT-1.6.2-2 complete (RWM - from SF log

(0912 from GP-1, Attachment 1)

1406

Secured Shutdown Cooling (from C0's

log)

1419

Drywell LC0 cancelled (SF log)

1430

NRC inspector asks U-2 SF about status

of RHR Loop

"B" and why it was not

lined up for auto LPC1 initiati n.

o

Informed by SF that procedure was in

progress and that following start of

"B" Recirc. Pump the lineup would be

restored.

(Note:

OP-17, Step 7.2.b.4

shows this to be the correct sequence.)

1445

NRC inspector asks U-2 SF why mode

switch is in S/U.

Informed that it was

placed in that position earlier for

testing and that their procedures allow

them to keep it there if S/U expected

shortly.

(Note:

Step 7.1.23 of

PT-1.6.2-2 states to place mode switch

in shutdown, unless the SF verifies

that the prerequisites are met for

leaving the mode switch in START-HOT

STBY pending reactor startup.)

Step 7.2.B.4 of OP-17

1453

Started 2B Rx Recirc. MG set (from

Step 5.1.16 of GP-1

C0's log)

-

.

.

.

.

.

Enclosure 2

2

Procedure _S,tep

Time

Action

1503

Primary and Secondary Containment in

effect(CO' slog)

1503

GP-01 Startup Checklist complete (time

later changed to 1546)

Step 5.1.13 of GP-1

1505

PA announcement that Primary and

Secondary Containment

in effect,

commencingRxS/U(fromChemistrylog)

Step 5.2.4 of GP-2

1507

Verified Rx Vessel Shell temperature to

5.2.5

right of criticality line (C0's log)

1510

(After PA announcement)

NRC inspector

again asks about status of RHR

"B"

Loop.

U-2 SF talks with U-2 operators

and then flush begins on RHR "B" Loop

per Step 7.2.B.5 of OP-17,

1516

Commenced Reactor Startup (SF log, time

later changed to 1600)

Step 5.2.6 of GP-2

1519

Chemistry informed of U-2 mode change

to mode 2 at 1516 (time later changed

to 1600 - Chemistry log)

1530

When leaving Control Room, NRC

inspector overhears SOS asking U-2

operators why rods are not being

pulled. He was told that RHR flush was

in progress, to which he asked, why

can't one operator do the flush while

the other pulls rods?

The operators explained that the flush

had to be done in order to restore the

RHR

"B" Loop for auto LPCI initiation

and rod pull would begin after LPCI "B"

was lined up.

Step 7.2.B.13 of OP-17

1546

RHR B Loop in standby per OP-17 (CO's

Step 5.1.15 of GP-1

log)

Step 5.2.4 of GP-2

1559

Verified Rx Yessel Shell temperature to

right of criticality line (C0's log)

Step 5.2.7 of GP-2

1600

Cormenced Rx S/U, first Rod out (SF,

C0's log)

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4

Enclosure 2

3

APPLICAB_LE _PROCEDU_R_ES_

_

PT-1.6.2-2

Rod Worth Minimizer System Operability Test

PT-1.6.1

Rod Sequence Control System Operability.

OP-17

Residual Heat Removal System Operating Procedure

GP-01

Startup Checklist

GP-02

Approach to Criticality and Pressurization of the

Reactor

!

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!

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1