ML20153C486

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Notice of Violation from Insp on 851119-860103
ML20153C486
Person / Time
Site: Zion  File:ZionSolutions icon.png
Issue date: 02/10/1986
From: Norelius C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20153C482 List:
References
50-295-85-42, 50-304-85-43, NUDOCS 8602210027
Download: ML20153C486 (2)


Text

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NOTICE OF VIOLATION Commonwealth Edison Company Docket No. 50-295 Docket No. 50-304 As a result of the inspection conducted on November 19, 1985 through  :

January 3, 1986, and in accordance with the " General Policy and Procedures  !

for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1985), the following violations were identified: 1

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1. 10 CFR 50, Appendix B, Criterion XVI, states in part, "Heasures shall be established to assure that conditions adverse to quality . . . are promptly identified and corrected. In the case of significant corditions adverse to quality, the measures shall assure that the cause of the ,

condition is determined and corrective action taken to preclude repetition."

Contrary to the above, on March 14, 1983, a condition adverse to quality, a loss of decay heat removal event, occurred on Unit 2, and the licensee failed to assure that corrective action was taken to preclude repetition, as indicated by a similar event on Unit 1 on December 14, 1985.

This is a Severity Level IV violation (Supplement I).

2. 10 CFR 50, Appendix B, Criterion V, states in part, " Activities affecting quality shall be prescribed by documented instructions, procedures, or Instructions, drawings, of a type appropriate to the circumstances. . . .

procedures, or drawings shall include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished."

Contrary to the above:

a. Procedure MI-6, " Filling and Draining the Refueling Cavity and Fuel Transfer Canal" was inappropriate to the circumstances in that it failed to provide periodic checks between reactor vessel level indicating system recorders and tygon level indication while the

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reactor coolant system loop was in the partially drained condition.

b. Procedure MI-6, step 6.34, failed to include appropriate quantitative or qualitative acceptance criteria for determining that the comparison between reactor vessel level indicating system recorders and tygon level was satisfactorily accomplished.

' c. Procedure MI-6 was inappropriate to the circumstances in that it failed to contain a caution stating that theand refueling vessel level that tygon level 5",

recorders will not indicate below 584' indication should be used exclusively if level is to be held at or below 584' 5".

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Notice of Violation 2 This is a Severity Level IV violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, you are required to submit i to this office within thirty days of the date of this Notice a written statement or explanation in reply, including for each violation:

(1) corrective action taken and the results achieved; (2) corrective action to be taken to avoid further violations; and (3) the date when full compliance will be achieved. Consideration may be given to extending your response time for good cause shown.

February 10, 1986 /tdw Y ek Dated Charles E. Norelius, Director, '

Division of Reactor Projects l

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