ML20151M306

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Notice of Violation from Insp on 880220-0325.Violations Noted:Failure to Perform Functional Test of APRM Flow Ref Thermal Power & APRM Downscale Trips & Failure to Follow Surveillance Procedures 57SV-SUV-007-2S & 57SV-D11-016-1S
ML20151M306
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 04/12/1988
From: Brownlee V
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20151M300 List:
References
50-321-88-07, 50-321-88-7, 50-366-88-07, 50-366-88-7, NUDOCS 8804250023
Download: ML20151M306 (2)


Text

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ENCLOSURE 1 NOTICE OF VIOLATION Georgia Power Company Docket Nos. 50-321, 50-366 Hatch, Units 1 and 2 License Nos. DPR-57, NPF-5 During the Nuclear Regulatory Commission (NRC) inspection conducted on February 20 - March 25, 1988, violations of NRC requirements were identified.

In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1987), the violations ' are listed below:

A. Table 4.1-1 of the Unit 1 Technical Specifications and Table 4.3.1-1 of the Unit 2 Technical Specifications require weekly functional testing of the Average Power Range Monitor (APRM) flow referenced thermal power and APRM downscale trips.

Contrary to the above, prior to February 15, 1988, the APRM flow referenced thermal power and APRM downscale trips were not functionally-tested weekly in either Unit 1 or Unit 2.

This is a Severity Level IV violation (Supplement I). >

B. Technical Specification 6.8.1.c requires that written procedures be established, implemented, and maintained for surveillance and test activities of safety related equipment.

Procedure 57SV-SUV-007-2S, "Analog Transmitter Trip System (ATTS) Panel 2H11-P921 Channel Functional Test and Calibration," requires that the trip unit and isolation logic be reset after injection of a simulated high pressure test signal and verification of proper relay operation but prior to closing the links.

Procedure 57SV-D11-016-1S, "GE NUMAC Main Steam Line Logarithmic Radiation Monitor Functional Test," requires the opening of links 00-23 and DD-24 in panel 1H11P611.

Contrary to the above, plant personnel failed to follow written surveil-lance procedures as noted below:

(1) On February 27, 1988, personnel performing Unit 2 Procedure 575V-SUV-007-2S failed to reset isolation logic for valve 2E11-F009 during functional testing of trip unit 2B31-N679A. This failure to follow the procedure resulted in an inadvertent isolation of shutdown cooling. At the time of this event, Unit 2 was in the REFUEL mode and core reload was in orogress.

(2) On March 7, 1988, personnel performing Unit 1 Procedure 57SV-011-016-1S, opened links in panel 1H11P609 instead of in panel 1H11P611.

This failure to follow the procedure resulted in a power interruption 8804250023 880412 PDR Q ADOCK 05000321 DCD

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Notice of Violation 2 to ATTS panel 1H11P921 which, in turn, resulted in a half-scram and isolation of the Reactor Water Cleanup system. At the time of this event, Unit I was operating in the RUN mode at approximately 100 percent of rated power.

This is a Severity Level IV violation (Supplement I). /

C. Technical Specification 6.8.1.c requires that written procedures be established, implemented, and maintained for surveillance and test activities of safety related equipment.

Contrary to the above, Unit 2 procedure 34SV-C71-005-2S, Revision 1, "Turbine Control Valve Fast Closure Instrument Functional Test", was inadequate in that it did not require the turbine to be reset prior to removing the "less than 30 percent reactor power" scram bypass feature of the logic system. As a result, on March 18, 1988, with the main turbine '

in the tripped mode and the turbine control valve fast closure pressure switches in the open position, a full reactor scram of Unit 2 occurred when the scram bypass feature was removed as specified in the procedure.

At the time of this event, Unit 2 was operating in the STARTUP mode at approximately 5 percent of rated power.

This is a Severity Level IV violation (Supplement I)

Pursuant to the provisions of 10 CFR 2.201, Georgia Power Company is hereby '

required to submit a written statement or explanation to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555, with a copy to the Regional Administrator, Region II, and a copy to the NRC Resident Inspector, Hatch Nuclear Plant, within 30 days of the date of the letter transmitting this Notice. This reply should be clearly marked as a "Reply to a Notice of Violatio1" and should include for each violation: (1) admission or denial of the violation, (2) the reasons for the violation if admitted, (3) the corrective s:eps which have been taken and the 'results achieved, (4) corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time. If an adequate reply is not receiveo' within the time specified in this Notice, an order may be issued to show cause why the license should not be modified, suspended, or revoked or why such other action as may be proper should not be taken.

FOR THE NUCLEAR REGULATORY COMMISSION ORIGINAL SIGNED By VIRGIL L DROWHLEE Virgil L. Brownlee, Chief Reactor Projects Branch 3 Division of Reactor Projects Dated at Atlanta, Georgia this1 > day of April 1988 t

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