Letter Sequence Approval |
---|
|
|
MONTHYEARML20140D1911986-01-22022 January 1986 Proposed Tech Specs,Clarifying Station Review Board Duties & Responsibilities Project stage: Other ML20140D1741986-01-22022 January 1986 Application for Amend to License NPF-3,changing Tech Specs to Clarify Station Review Board Duties & Responsibilities Project stage: Request ML20140D1451986-01-22022 January 1986 Forwards Application for Amend to License NPF-3,changing Tech Specs Clarifying Station Review Board Duties & Responsibilities.Separate Amend Application Being Prepared to Address Addl Administrative Changes.Fee Paid Project stage: Request ML20215K3801987-05-0404 May 1987 Requests Reissuance of Table 3.6-2, Containment Isolation Valves of Tech Spec 3/4.6.3,correcting Typos in 840911 Application to Amend License NPF-3 Project stage: Request ML20237K8441987-08-28028 August 1987 Requests That Revised Tech Spec 6.5.1.6,submitted w/870122 License Amend Request,Reflects Station Review Board Responsibility to Review safety-related Aspects of Proposed Procedures,Mods,Tests & Experiments,Per NUREG-0103,Rev 4 Project stage: Other ML20150B9711987-09-11011 September 1987 Discusses Plant Organizational Changes.Meeting W/E Butcher & Bryan Should Be Set Up Project stage: Meeting ML20237A6881987-12-0808 December 1987 Informs of Changes Necessary to Support Fifth Refueling Outage in Feb 1988.Key Amend Requests Placed Into 1 of 3 Listed Categories.Nrc Should Allocate Necessary Resources to Provide Timely Support for Review & Issuance of Amends Project stage: Other ML20238E5701987-12-28028 December 1987 Provides Clarification to 860122 Application for Amend to License NPF-3 Re Station Review Board Responsibilities,Per 871127 & 1202 Telcons W/Aw Deagazio & Staff,Respectively, Revising Tech Specs 6.5.1.6(b) & 6.5.3.1(a),(b),(d) & (E) Project stage: Supplement ML20149J0571988-02-17017 February 1988 Provides Addl Clarification of License Amend Request Submitted on 860122 Involving Proposed Tech Spec 6.5.3.1(c). Clarified Administrative Control Will Require Technical Reviews on Each Mod Affecting Nuclear Safety Project stage: Other ML20150C4511988-03-0909 March 1988 Amend 109 to License NPF-3,revising Responsibilities & Authority of Station Review Board & Adding Section to Technical Review & Control Project stage: Other ML20150C4621988-03-0909 March 1988 Safety Evaluation Supporting Amend 109 to License NPF-3 Project stage: Approval ML20150C4731988-03-0909 March 1988 Notice of Denial of Amend to License NPF-3 Re Deleting Requirement in Tech Spec 6.5.1.6.e Concerning Station Review Board Responsibility to Investigate & Rept Tech Spec Violations Project stage: Other ML20150B9671988-03-11011 March 1988 Requests That Encl 870911 Memo from J Scinto Be Included in Docket Files.Memo Relates to 870122 Application for Amend to License NPF-3 Re Organization Changes Project stage: Other 1987-08-28
[Table View] |
|
---|
Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 ML20249A7661998-06-11011 June 1998 Safety Evaluation Supporting Amend 222 to License NPF-3 ML20249A7551998-06-11011 June 1998 Safety Evaluation Supporting Amend 223 to License NPF-3 ML20216B9401998-04-15015 April 1998 Safety Evaluation Supporting Amend 221 to License NPF-3 ML20216B8381998-04-14014 April 1998 Safety Evaluation Supporting Amend 220 to License NPF-3 ML20202C6131998-02-0303 February 1998 Safety Evaluation Supporting Amend 219 to License NPF-3 ML20199J9511998-01-30030 January 1998 SER Related to Exemption from Section Iii.O of App R,To 10CFR50,for Davis-Besse Nuclear Power Station,Unit 1 ML20198R4771998-01-13013 January 1998 SER Approving Second 10-year Interval Inservice Inspection Program Plan Requests for Relief for Davis-Besse Nuclear Power Station,Unit 1 ML20203C1401997-12-0202 December 1997 Safety Evaluation Supporting Amend 217 to License NPF-3 ML20203B2141997-12-0202 December 1997 Safety Evaluation Supporting Amend 218 to License NPF-3 ML20203C2701997-12-0202 December 1997 Safety Evaluation Supporting Amend 216 to License NPF-3 ML20138L0491997-02-11011 February 1997 Safety Evaluation Supporting Amend 214 to License NPF-3 ML20128L3001996-10-0202 October 1996 SER Supporting Dbnp IPE Process of Identifying Most Likely Severe Accidents & Severe Accident Vulnerabilities ML20058M9591993-09-28028 September 1993 SE Accepting Licensee Response to GL 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants.' ML20057A3791993-08-20020 August 1993 SE Concluding That Second 10-yr Interval Inservice Insp Program Plan for Plant Has Unacceptable Exam Sample as Discussed in Encl Inel TER ML20056G4301993-08-18018 August 1993 Safety Evaluation Re Inservice Testing Program Requests for Relief.Licensee Made Changes to Subj Program to Include Exercising & fail-safe Testing of Auxiliary Feedwater Valves AF-6451 & AF-6452,in Response to TER Anomaly 8 ML20126A3051992-12-0808 December 1992 Safety Evaluation Supporting Amend 176 to License NPF-3 ML20056B2721990-08-20020 August 1990 Safety Evaluation Granting Relief from ASME Code Repair Requirements for ASME Code 3 Piping ML20248H6371989-10-0303 October 1989 Safety Evaluation Supporting Amend 139 to License NPF-3 ML20248D8271989-09-29029 September 1989 Safety Evaluation Accepting Util 890228 & 0630 Submittals Presenting Proposed Designs to Comply w/10CFR50.62 ATWS Rule Requirements ML20248E2771989-09-20020 September 1989 Safety Evaluation Supporting Amend 138 to License NPF-3 ML20248B3801989-09-20020 September 1989 Safety Evaluation Supporting Amend 137 to License NPF-3 ML20247E6901989-09-0505 September 1989 Safety Evaluation of Audit of Facility Design for Resolution of IE Bulletin 79-27 Re Loss of non-Class IE Instrumentation & Control Power Sys Bus During Operation.Preventive Maint & Testing Program Should Be Developed for Bus Power Sources ML20245K1871989-08-15015 August 1989 Safety Evaluation Supporting Amend 136 to License NPF-3 ML20245F5791989-08-0404 August 1989 Safety Evaluation Supporting Amend 134 to License NPF-3 ML20245H9531989-08-0404 August 1989 Safety Evaluation Supporting Amend 135 to License NPF-3 ML20247J8731989-05-18018 May 1989 Safety Evaluation Supporting Amend 133 to License NPF-3 ML20245G0371989-04-25025 April 1989 Safety Evaluation Supporting Amend 131 to License NPF-3 ML20245F0631989-04-25025 April 1989 Safety Evaluation Supporting Amend 132 to License NPF-3 ML20244D4031989-04-13013 April 1989 Safety Evaluation Supporting Amend 130 to License NPF-3 ML20196D9601988-12-0808 December 1988 Safety Evaluation Re Util Response Concerning Auxiliary Feedwater Sys Reliability Study.Util Should Ensure That Sys Mods Do Not Result in Net Reduction in Sys Reliability ML20207K7911988-10-0404 October 1988 Safety Evaluation Supporting Operation in Cycle 6 W/O Removing Flaws in Cracked HPI Nozzle ML20207K1071988-09-19019 September 1988 Safety Evaluation Supporting Amend 120 to License NPF-3 ML20207H9271988-08-24024 August 1988 Safety Evaluation Supporting Amend 117 to License NPF-3 ML20207H3891988-08-19019 August 1988 Safety Evaluation Supporting Amend 116 to License NPF-3 ML20207E3931988-08-0202 August 1988 Safety Evaluation Supporting Amend 114 to License NPF-3 ML20207D5171988-08-0202 August 1988 Safety Evaluation Supporting Amend 115 to License NPF-3 ML20150C4621988-03-0909 March 1988 Safety Evaluation Supporting Amend 109 to License NPF-3 1999-08-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
[Table view] |
Text
_ _ _ _ _ _ _ _ _ _ _
i l
'd UNITED STATES 1
NUCLE AR REGULATORY COMMISSION wassiNotoN. o. c. rosss SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION j
RELATED TO AMENDMENT NO. 109 TO FACILITY OPERATING LICENSE NO. NPF-3 TOLEDO EDISON COMPANY l
AND THE CLEVELAND ELECTRIC ILLUMINATING COMPANY DAVIS-BESSE NUCLEAR POWER STATION. UNIT NO. 1 DOCKET N0. 50-346
1.0 INTRODUCTION
By letter cated January 22, 1986, as clarified by letters dated August 25 and December 28, 1987 January 15, 1988, and February 17, 1988, Toledo Edison Company (TED or the licensee) submitted an application for amendment to Facility Operating License No. NPF-3 for the Davis-Besse Nuclear Power Station, Unit No.1.
The application proposed certain revisions to the Technical Specifications (TS's) which would revise and clarify the duties and responsibilities of the Station Review Board (SRB). This would be accomplished by adding a new Section 6.5.3 which would specify how activities affecting nuclear safety should be conoucted and by revising Sections 6.5.1.6 and 6.5.1.7 which would identify SRB responsibilities and SRB authority, respectively.
Additionally, Section 6.8.2 would be modified and Section 6.8.3 would be deleted to eliminate material which would be included in the new Section 6.5.3 and modified Sections 6.5.1 and 6.5.1.7.
In addition to these proposed changes, the licensee also proposed deletion of an uncefined tem in Section 6.5.1.3 and a number of position title changes in various sections. With regard to the position title changes, the Comission issued Amendment No. 98 (February 18,1987) which approved the proposed title changes.
2.0 EVALUATION The licensee proposed that a new Section 6.5.3, "Technical Review and Control,"
be added to provide for technical review of changes to procedures and facilities and for the review of tests or experiments not covered in the Updated Safety AnalysisReport(USAR)whichaffectthenuclearsafetyoftheDavis-Besse facility.
The new section would specify that procedures and facility changes or tests / experiments be reviewed by an individual or group different from the one which prepared the change or test. The new section would also specify that the individuals designated by the Plant Manager to perform the reviews rost meet the qualification requirements of Sections 4.2, 4.3.1, 4.4 or 4.6 of ANSI Standard 18.1, 1971.
Each review will include a determination of whether en unreviewed safety question as defined in 10 CFR 50.59 is involved. The new section would also provide for inter-disciplinary reviews when such reviews are deemed necessary.
h bK 6
P
I The specification for temporary approval of changes to procedures, presently i
in TS Section 6.8.3, would be moved to this new Section 6.5.3 and reworded, but the approval authority would retrain as before for changes which do not change the intent of the procedure. The proposed section would delet the specific requirement for SRB review of such changes.
The licensee has stated that final review and approval by the SRB and Plant Manager is required within 14 days by station procedure.
The NRC staff has reviewea this new section and finds that it rieets the require-ments for indepenaent reviews of f acility cMnges of ANSI Standard N45.2.11-1974, Section 6. Design Verification, which is endorsed by the Comission in Regulatory Guide 1,64 and is comitted to in the Toledo Edison Nuclear Quality Assurance Program. The same independent reviews of procedures and changes thereto, and i
of tests and experiments would also enhance the assurance of safety in these a reas. The staff, therefore, finds this new section on technical review and control to be acceptable, on the condition that station procedures reoutring final SRS review and approval within 14 days for temporary approvals to procedures are maintained in force.
The licersee also proposed to modify the responsibilities (Section 6.5.1.6) of the SRB and authority (Section 6.5.1.7) to bring them into agreement with the new Section 6.5.3.
This woulo eliminate the SRB review of the strictly technical content of the proposed changes, but would retain SRB review of the safety related aspects of the change, including any unreviewed safety question detemined during the technical review or during the SRB review.
For changes where an unreviewed safety question exists, the SRB would perfom a technical review as well as a safety review. The staff has reviewed these proposed changes and has found thet the licensee's proposed deletion of existing item e of Section 6.5.1.6 is not acceptable, however, the remaining proposed changes to Section 6.5.1.6 are found to be acceptable. Therefore, the following changes are approved for
]
incorporation into the TS's.
-Replacement of existing items a through d with the licensee's proposed items a through d.
-Deletion of existing items f through j(and replacement with thebut relettered f thro licensee's proposed items e through i i
-The licensee's proposed item f is modified to delete a redundant reference to Technical Specifications because this specific requirement is retained in item e.
-Incorporation of proposed items j through m (but relettered k j
throughn).
]
-Relettering of existing items k through o as items o through s.
-Modification of Section 6.8.2 relating to changes to procedures to 1
delete the specification of review and approval requirements (which are now included in the new Section 6.5.3) and add reference to the i
requirements of Section 6.5.3.
I l
3
-Deletion of Section 6.8.3 dealing with changes and approvals to temporary procedure changes, since these requirements are specified in new Section 6.5.3.
The licensee proposed modifications to Sections 6.5.1.7.a and 6.5.1.7.b to be consistent with the revised responsibilities proposed in Section 6.5.1.6.
The staff finds the licensee's proposed changes acceptable except that, consistent with the staff's denial to delete item 6.5.1.6.e. that item is retained in Section 6.5.1.7.b.
(The licensee's proposal is also relettered to be consistent with the relettering of the items in Section 6.5.1.6.)
The licensee proposed to add an additiunal SRB Authority.
Specifically, the SRB would recomend to the Plant Manager that an action n! viewed uncer Section 6.5.1.6.b does not constitute an unreviewed safety question. The staff finds the additional reautrement acceptable.
The licensee proposed to delete the undefined phrase "to serve on a temporary basis" from Section 6.5.1.3.
The staff finds the deletion acceptable.
The staff has compared the licensee's proposed changes to the acceptance criteria set forth in Section 13.4 of the Standard Review Plan (h0 REG-0800) and finds that the proposed changes are consistent with those criteria. These changes are similar to changes previously approved by the staff for other facility TS's.
The denial to delete item e Section 6.5.1.6 by the staff is tased upon the concern that there shculd be adequate assurance that the results of investiga-tions of Technicsl Specification violations are brought to the attention of responsible corporate management.
The licensee's preposal to delete this require-ment would be inconsistent with TS's recently approved for other facilities by the NRC and is inconsistent with current Standard Technical Specifications.
3.0 EhVIR0hPENTAL CONSIDERATION This amendment relates to changes in recordkeeping, reporting, er administrative procedures or requirements. Accordingly, this amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(10).
Pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of this amendment.
4.0 CONCt.USION The staff has concluded, based on the considerations discussed above, that:
(1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, and (2) such activities will be conductec tr. compliance with the Comunission's regulations, and the issuance of this amendment will not be inimical to the comon defense and security or to the health and safety of the public.
Prinicipal Contributors:
D. S. Butler, A. W. De Agazio Dated:
March 9, 1988