ML20149E787

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Revised Safety Evaluation for Amends 185 & 216 to Licenses DPR-71 & DPR-62,respectively.Rev Presents Better Description of Design Feature
ML20149E787
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 07/08/1997
From:
NRC (Affiliation Not Assigned)
To:
Shared Package
ML20149E789 List:
References
NUDOCS 9707210069
Download: ML20149E787 (6)


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NUCLEAR ~ 10ULATORY COMMISSION ilNGTON, D.C. SteeHo01 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO' AMENDMENT NO. 185 TO FACILITY OPERATING LICENSE NO. DPR-71 AND AMENDMENT NO. 216 TO FACILTY OPERATING LICENSE NO. DPR-62 CAROLINA POWER & LIGHT COMPANY BRUNSWICK' STEAM ELECTRIC PLANT. UNITS 1 AND 2 DOCKET NOS. 50-325 AND 50-324

1.0 INTRODUCTION

By letter dated Marc'n 5,1997, as supplemented May 9,1997, the Carolina Power

& Light Company (the licensee) submitted a request for changes to the

< Brunswick Steam Electric Plant (BSEP), Units 1 and 2, Technical Specifications (TS). The requested changes would incorporate new TS for instrumentation associated with a reinstated automatic isolation of a pathway for release of non-condensible gases from the main condenser in the event of a control rod drop accident (CRDA). At power levels of 5 percent or less, mechanical vacuum pumas are used to remove non-condensible gases from the condenser using a pat 1way to the release stack that bypasses the normal holdup and filter train.-

The proposed TS will require that four channels of the main steam line radiation - high radiation function be capable of tripping the mechanical vacuum pumps and closing an isolation valve for each ) ump in tte release pathway. Surveillance Requirements are included in-tie TS to ensure the isolation instrumentation will-perform its intended function.

l By letter dated September. 30, 1994, and supplemented March 24, 1995, the licensee requested elimination of the main steam line radiation monitor trip signal to the condenser vacuum pumps and closure of the associated isolation f

i valves. This request was based on the General Electric Company Licensing Topical Report NEDO-31400 which was approved by the NRC staff by the Safety l

Evaluation dated May 15, 1991.

Further, a plant-s)ecific calculation by NUS (NUS Calculation 8T12-M-02) demonstrated that in tie event of a CRDA the 4

l radiation level in the control room would be below the permissible levels of General Design Criterion 19 and Standard Review Plan (SRP), Section 6.4.

By L

letter dated March 31, 1995, the NRC. approved the change request for BSEP, eliminating the above signal.

On December 19, 1996, the licensee determined that the NUS calculation was in error, and.in the event of a CRDA without isolation of the condenser vacuum pumps, the doses in the main control ~ room would exceed the SRP, Section 6.4 guidance. To resolve this deficiency, the' licensee proposes to restore to the

. original plant' design and reinstall the main steam high radiation signal to-tri the condenser vacuum pumps and close the isolation valve associated with eac pump.

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'9707210069 970716 DR ADOCK 0 4

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j. The May 9,1997, letter provided clarifying information that did not change the initial proposed no significant hazards consideration determination.

2.0 EVALUATION In the March 5, 1997,-letter the licensee stated that with the proposed changes, the probability of the vacuum pumps discharging contaminated steam a

into the main stack is very low for several reasons.

First, the condenser vacuum pumps are used for a limited time period when the plant is below 5 percent power in Operational Condition 1 and 2.

When a condenser vacuum pump is not in operation, fission product release through this path would not occur. Second, the isolation of the vacuum pump system is required only when there-is a CRDA. The licensee stated that a highly improbable combination of events have to happen for a CRDA to occur. These events include erroneous selection and withdrawal of an out-of-sequence rod by an oprator, a failure of the rod worth minimizer to block withdrawal of the out-of-sequence rod, and

' failure of the rod-to-drive cou)1ing. The lic.ensee probabilistic safety i

analysis indicates that the pro) ability of a CRDA is below 1E-6 per reactor year over a 40-year time period. Third, in the event of a CRDA, the high radiation monitors in the main steam lines are designed to trip the condenser vacuum pumps in 5 seconds and close the associated isolation valves.

In other words, the condenser vacuum pumps can discharge contaminants only for 5 seconds.

Fourth, the safety-related main steam line radiation monitors provide a highly reliable means to automatically trip the respective condenser i

vacuum pump and close the associated isolation valve. The main steam line radiation-high logic consists of two independent trip systems, each with two channels operating nn one-out-of-two logic.

Furthermore, both trip systems must operate to generate the isolation signal. This logic design is consistent with the original approved plant design.

The licensee's submittal includes a calculation of main control room doses in the event of a CRDA, assuming that the main steam line radiation monitors isolate the condenser vacuum pumps in conformance to the SRP, Section 15.4.9.

The calculation indicates that the operator doses from a postulated CRDA are i

23.2 rem thyroid and 0.05 rem whole body in the main control room area.

H General Design Criterica (GDC) 19/SRP Section 6.4 permits 30 rem thyroid and 5 L

rem whole body. Dcses of 0.16 rem thyroid and 0.015 rem whole body were calculated in the 2-hour exclusion area, and I rem thyroid in the low population zone. The calculated control room doses meet the indicated acceptance criteria, and the offsite doses are well below the acceptance criteria in the SRP and 10 CFR Part 100.

1 The amendment proposes a 12-hour time limit for the following Actions in new proposed TS 3/4.3.8, Condenser Vacuum Pump Isolation Instrumentation:

j a.

With one or more channels of the Main Steam'Line Radiation-High Function for condenser vacuum pumps inoperable, restore the inoperable channel to 1

operable status or place the inoperable channel or associated trip system ~in trip or isolate the condenser vacuum pumps or isolate the main steam lines or be in hot shutdown.

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. b.

With condenser vacuum pump isolation capability not maintained, isolate the condenser vacuum pumps or isolate the main steam lines or be in hot shutdown.

It further states that when a channel is placed in an inoporable status solely for the surveillance tests, entry into associated actions may be delayed for up to 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> provided the condenser vacuum pump isolation capability is maintained.

The amendment also proposed Surveillance Requirements which state that each channel of the Main Steam Line Radiation-High Function for condenser vacuum pump isolation shall be demonstrated operable by:

a.

Performance of a channel check at least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> b.

Performance of a channel functional test at least once per 92 days c.

Performance of a channel calibration and logic system functional test at least once per 18 months These requirements are in conformance with the original plant design for BSEP, Units 1 and 2, which included the condenser vacuum pump trip, and NEDC-30851P-A, Supplement 2, " Technical Specifications Improvement Analysis for BWR Isolation Instrumentation Common to Reactor Protection System and Emergency Core Cooling System Instrumentation," dated March 1989, which was previously approved by the NRC staff.

The staff performed an independent analysis to determine plant conformance with the criteria that the CRDA results in consequences less than 10% of the 10 CFR Part 100 guidelines even with conservative assumptions.

In its analysis, the staff utilized the assumptions contained in SRP Section 15.4.9.

The staff computed the offsite doses and the control room operator doses for BSEP, Units 1 and 2, using the assumptions described in Table 1 of this safety evaluation and the NRC's ACTICODE computer code. The staff computed that offsite and control room doses are within the acceptance criteria given in SRP Section 15.7.4 and GDC-19. The resulting CRDA calculated values are listed in Table 1.

.. Table 1 INPUT PARAMETERS AND RESULTS FOR BRUNSWICK UNITS 1 AND 2 EVALUATION OF A CONTROL ROD DROP ACCIDENT

. Parameters Power. Level 2550 Number of Rods Perforated 850 Number of Rods Melted 0

Number of Rods In-Core 33600 Power Peaking Factor 1.5 Condenser Leak Rates (%) day 1.0 Fraction of fission product inventory release to coolant:

Iodines, percent 50 Noble gases, percent 100 Receptor Point Variables' l

Exclusion Area Boundary (EAB) 3 Atmosphere Relative Concentration, X/Q (sec/m )

0-2 hours 1.0E-3 Low Population Zone (LPZ) 3 Atmosphere Relative Concentration, X/Q (sec/m )

0-8 hours 2.8E-4 Control Room (CR) 3 Atmosphere Relative Concentration, X/Q (sec/m )

0-2 hours 1.5E-2 Thyroid Doses EAB-1.3 rem LPZ-1.4 rem l

CR-13.0 rem In summary, the staff has reviewed the licensee's evaluation and justification for reinstating the main steam line radiation monitor signal to isolate the condenser vacuum pumps and close the associated isolation valves.

Based on that review, the staff concludes that the licensee has performed a plant-specific calculation that confirms that the reestablishment of the original plant design, which includes the above feature, will maintain the worst-case plant CRDA release below the acceptance criteria in the SRP, 10 CFR Part 50, Appendix A, GDC-19, and 10 CFR Part 100. The staff further concludes that the proposed TS changes for the condenser vacuum pump trip and isolation are consistent the with BWR Improved Standard (S and are, therefore, acceptable.

1 Reference for EAB and LPZ, " Safety Evaluation of the Brunswick 1

. Steam Electric Station Units 1 and 2," November 1973.

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3.0 STATE CONSULTATION

In accordance with the Commission's regulations, the State of North Carolina

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official was notified of the proposed issuance of the amendments.

The State official had no coments.

4.0 ENVIRONMENTAL CONSIDERATION

The amendments change a requirement with respect to installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20 and changes the Surveillance Requirements. The NRC staff has determined that the amendments involve no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that'there is no significant increase in individual or cumulative occupational radiation exposure. The Comission has previously issued a proposed finding that the amendments involve no significant hazards consideration, and there has been no public coment on such finding (62 FR 17224). Accordingly, the amendments meet the eligibility criteria for categorical exclusion set forth in 10 CFR S1.22(c)(9).

Pursuant to 10 CFR 51.22(b) no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendments.

The NRC staff has reviewed the licensee's evaluation and justification for reinstating the main steam radiation monitor signal to isolate the condenser i

vacuum pump and to close the associated isolation valves.

Based on that review, the staff concludes that the licensee has performed a plant-specific calculation which confirms that reestablishment of the original plant design, which inclucas the above feature, will maintain the worst-case plant CRDA release below the acceptance criteria in the SRP and 10 CFR Part 100. The NRC staff further concludes that the proposed TS changes for the condenser vacuum i

pump trip and isolation are consistent with the BWR improved Standard TS and are, therefore, acceptable.

5.0 CONCLUSION

The Comission has concluded, based on the considerations discussed above, that (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, (2) such 4

activities will be conducted in compliance with the Comission's regulations, and (3) the issuance of the amendments will not be inimical to the comon defense and security or to the health and safety of the public.

4 Principal Contributors:

S. Mazumdar and J. Minns Date: July 8, 1997 1

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REVISED SAFETY EVALUATION FOR AMENDMENT N0. 185 TO FACILITY OPERATING LICENSE

'NO. DPR BRUNSWICK, UNIT 1 REVISED SAFETY EVALUATION FOR AMENDMENT-NO.-216 T0 FACILITY OPERATING LICENSE:

NO. DPR BRUNSWICK, UNIT-2 DISTRIBUTION:.

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