Similar Documents at Zion |
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LER-1978-078, /01L-0:on 780818:possible Use of Atypical Weld Metal Discovered in Loop 4 of Reactor Pressure Vessel. Interim Heatup & Cooldown Curves Calculated & Used to Provide Adequate Conservatisms Until Issue Resolved |
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| 2951978078R01 - NRC Website |
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]gNM U.S. NUCLL AR HLGULAlOHY COMMlbSION LICENSEE EVENT REPORT CONTROL DLOCX: l l
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60 LVkNT OATE 14 lb HLPOHT 0A1E NO EVENT DESCRIPTION AND PROUAOLE CONSEQUENCES h 1 O I 21 l On Aug. 24, 1978, the station was advised of the possible use of I O Ia I ; atypical weld metal in the manuf acture of Unit 1 and 2 reactor vessels.
io i4i l This would result in the change of the initial RT(NDT) from 27F to
_ l O I 51 l 125F and NDTT from 15F to 70F in Table 3.3. 2-1 of the Tech Specs.
The i o,g i ; pressure and temperature limits of Tcch Spec.
- 3. 3.2 may therefore have i o,,; ; been non-conservatively calculated.
Observation and evaluation show
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40 di 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h Ii10i l The possible use of atypical weld wire in 4-loop PWR Reactor Vessels, l
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Board Nos. N-184 and N-185 as part of West.
Elec. NSSS.
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ATTAC3 MENT TO LER NO. 78-078/01 L - 0 COMMONWEALTH EDISON CO.
j ZION GENERATING STATION 50-295 j
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Description of Event
~
On August 14,J1978, Conunonwealth Edison was advised by the NRC that j
Babcock and Wilcox hadL determined from chemical analysis of archive reactor vessel weldment.. that the nickel and silicon-content of the weld material was outside the specified range.
It has been determined that the weld filler wiro used for that particular we?.d was atypical.. As of -this date it is not known whether or not this atypical weld wire was' used in the manufacture of Zion ' reactor vessels.
It is possible that this atypical weld metal may have been used in the circumferential girth weld of the Zion Unit i vessel and the lower shell longitudinal' weld of the Zion Unit 2 vessel.
Review of the records avallable to date has not enabled the station to discount the possibility that these vessels contain weld metal having an 0
initial RT of 1250F and an initial T of 70 F.
This compares withaninfNal'RT of270FandaninYNa1T 0
of 15 F-as found in Table 3.3.2-1.ogDIhe Technical SpecificatioE The-pressure and temperature limitations' described in Technical Specification 3.3.2 may therefore have been non-conservatively calculated.. No affect to the integrity of the reactor coolant pressure boundary has been observed in-relation ~ to Unit 1 and 2 having operated 2.8 and 2.4 Effective Full Power Years respectively, based on the less conservative limitations.
l Consequences of Occurrence 1
No~ effect to the integrity of the reactor coolant systems has. been
- - observed.
In addition,. evaluations conducted.by Westinghouse Electric,. based oni ASME Section III, Appendix III, has shown that no adverse effects on the integrity or safety of the plant has occurred due to operation using the possibly less conservative limitations.
Additionally, ultrasonic inspections following the Minitial hydrostatic test = indicated the absence of any flaws.
The.
health and safetyf of the : plant and public was unaf fected by this occurrence.
Cause of Occurrence.
The cause of the occurrence is the possible use of atypical weld i
filler. wire in' the, manufacture 'of. Zion Unit 1 and 2 4-loop PWR
- Reactor Vesseis National Board Numbers N-184 and N-185, designed by.
y+
l-e Westinghouse Electric Co. and manufactured by Babcock and Wilcox.
It is unknown at this time how the atypical weld metal could have been introduced. or if it was, in fact, used in these vessels.
Corrective Action
The Unit' l and 2 reactor vessel pressure and temperature limitations have been re-evaluated assuming the atypical metal was included during fabrication.
These limitations were calculated in.accordance with 10 CFR 50, Appendix G and are valid for heatup and cooldown during the first eight Effective Full Power Years of operation.
Interim operating curves representative of-these limitations were implemented as.of August 18, 1978, and will remain in use.until this issue is resolved.
.Use of these curves will ensure continued vessel integrity in the event the atypical weld wire' was used.
If future investigations demonstrate the absence of the atypical weld metal, then the interim curves will have provided excess cons erva tism.
If the metal is in fact present, then the interim curves will continue in use and be periodically updated as necessary to provide adequate conservatism.
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| 05000304/LER-1978-022-03, LER-022/03X-1 on 780222:grab Samples Not Obtained from 4 Tech Spec Rad Monitors Which Were Inoperable.Caused by Personnel Error | LER-022/03X-1 on 780222:grab Samples Not Obtained from 4 Tech Spec Rad Monitors Which Were Inoperable.Caused by Personnel Error | | | 05000304/LER-1978-022, Forwards LER 78-022/03X-1 Update | Forwards LER 78-022/03X-1 Update | | | 05000304/LER-1978-024, Cancelled | Cancelled | | | 05000295/LER-1978-027, Forwards LER 78-027/03X-1 | Forwards LER 78-027/03X-1 | | | 05000295/LER-1978-027-03, /03X-1 on 780402:steam Flow Channel 1F522 Failed Low Due to Plugging of High Side Sensing of Transmitter While Sealing Valve Steam Leak.Valve Was Replaced | /03X-1 on 780402:steam Flow Channel 1F522 Failed Low Due to Plugging of High Side Sensing of Transmitter While Sealing Valve Steam Leak.Valve Was Replaced | | | 05000295/LER-1978-029, Cancelled | Cancelled | | | 05000304/LER-1978-038, Cancelled | Cancelled | | | 05000304/LER-1978-044, Cancelled | Cancelled | | | 05000295/LER-1978-052, Cancelled | Cancelled | | | 05000304/LER-1978-052-01, Cancelled | Cancelled | | | 05000295/LER-1978-055, Cancelled | Cancelled | | | 05000304/LER-1978-055-01, Cancelled | Cancelled | | | 05000295/LER-1978-056, Cancelled | Cancelled | | | 05000304/LER-1978-056-01, Cancelled | Cancelled | | | 05000304/LER-1978-057, Forwards LER 78-057/03L-0 | Forwards LER 78-057/03L-0 | | | 05000304/LER-1978-057-03, /03L-0:on 780811,containment Particulate Ventilation Radiation Monitor Exhibited Spurious Alarms & Detector Would Not Respond to Source Check.Caused by Loose Signal Wire on Selector Switch in Control Room | /03L-0:on 780811,containment Particulate Ventilation Radiation Monitor Exhibited Spurious Alarms & Detector Would Not Respond to Source Check.Caused by Loose Signal Wire on Selector Switch in Control Room | | | 05000295/LER-1978-057, Cancelled | Cancelled | | | 05000295/LER-1978-058, Cancelled | Cancelled | | | 05000304/LER-1978-058-01, Cancelled | Cancelled | | | 05000304/LER-1978-059-01, Cancelled | Cancelled | | | 05000304/LER-1978-060-03, /03L-0:on 780826,air Ejector Rod Monitor 2RTPR26 Failed & Would Not Reset.Caused by Failure of Roots- Connersville Blower.Pump Replaced & Monitor Returned to Svc | /03L-0:on 780826,air Ejector Rod Monitor 2RTPR26 Failed & Would Not Reset.Caused by Failure of Roots- Connersville Blower.Pump Replaced & Monitor Returned to Svc | | | 05000304/LER-1978-060, Forwards LER 78-060/03L-0 | Forwards LER 78-060/03L-0 | | | 05000304/LER-1978-061, Forwards LER 78-061/03L-0 | Forwards LER 78-061/03L-0 | | | 05000304/LER-1978-061-03, /03L-0:on 780905,during Testing,Mcc Tripped Due to Limitorque Case Caused by Jamming.Redundant VLV Operable to Ensure Containment Integrity.Motor Case,Handwheel & Bracket Replaced & VLV Returned to Svc | /03L-0:on 780905,during Testing,Mcc Tripped Due to Limitorque Case Caused by Jamming.Redundant VLV Operable to Ensure Containment Integrity.Motor Case,Handwheel & Bracket Replaced & VLV Returned to Svc | | | 05000304/LER-1978-062-03, /03L-0:on 780906,during Testing,Raw Water Svc Tank to Charging Suction Valve Failed to Open Remotely Causing Sys Degradation Per Tech Specs.Limitorque Model SMB00 Valve Operator Torqued Out & Valve Stroked Three Times | /03L-0:on 780906,during Testing,Raw Water Svc Tank to Charging Suction Valve Failed to Open Remotely Causing Sys Degradation Per Tech Specs.Limitorque Model SMB00 Valve Operator Torqued Out & Valve Stroked Three Times | | | 05000304/LER-1978-062, Forwards LER 78-062/03L-0 | Forwards LER 78-062/03L-0 | | | 05000304/LER-1978-063, Cancelled | Cancelled | | | 05000304/LER-1978-064-03, /03L-0 on 780915:during Normal Oper,Received a Nis Channel Deviation Alarm.Pwr Range Channel N42 Was Reading 93% Instead of 100%.Caused by Defective 25 Volt Pwr Supply in N42 Pwr Range Drawer | /03L-0 on 780915:during Normal Oper,Received a Nis Channel Deviation Alarm.Pwr Range Channel N42 Was Reading 93% Instead of 100%.Caused by Defective 25 Volt Pwr Supply in N42 Pwr Range Drawer | | | 05000304/LER-1978-064, Forwards LER 78-064/03L-0 | Forwards LER 78-064/03L-0 | | | 05000295/LER-1978-064, Cancelled | Cancelled | | | 05000304/LER-1978-065-03, /03L-0 on 780919:during Normal Oper,Channel 2L-547 Had Failed High & Assoc Bistables Were Tripped,Due to Faulty Xmtr(Level,Mode 13D2495K).XMTR Replaced W/Spare & Channel Recalibr | /03L-0 on 780919:during Normal Oper,Channel 2L-547 Had Failed High & Assoc Bistables Were Tripped,Due to Faulty Xmtr(Level,Mode 13D2495K).XMTR Replaced W/Spare & Channel Recalibr | | | 05000304/LER-1978-065, Forwards LER 78-065/03L-0 | Forwards LER 78-065/03L-0 | | | 05000304/LER-1978-066, Forwards LER 78-066/03L-0 | Forwards LER 78-066/03L-0 | | | 05000304/LER-1978-066-03, /03L-0 on 780925:pressurizer Level 2LT-459 Was Found to Be 6% Lower That the Other 2 Channels.No Cause Was Found for Failure | /03L-0 on 780925:pressurizer Level 2LT-459 Was Found to Be 6% Lower That the Other 2 Channels.No Cause Was Found for Failure | | | 05000304/LER-1978-067-03, /03L-0 on781008:S/G Level Channel 2 LI-538 Was Found to Be Indicating 6% Higher than the Other 2 Channels. Caused by Dirt in Xmtr Sensing Lines & a Xmtr Oscillator PN805B27U01 Being Out of Tune | /03L-0 on781008:S/G Level Channel 2 LI-538 Was Found to Be Indicating 6% Higher than the Other 2 Channels. Caused by Dirt in Xmtr Sensing Lines & a Xmtr Oscillator PN805B27U01 Being Out of Tune | | | 05000304/LER-1978-067, Forwards LER 78-067/03L-0 | Forwards LER 78-067/03L-0 | | | 05000304/LER-1978-068-01, Cancelled | Cancelled | | | 05000295/LER-1978-068, Cancelled | Cancelled | | | 05000304/LER-1978-069-03, /03L-0 on 781015:2D MSIV Failed to Close from the Control Room.Caused by Failure of Both DC Solenoid Valves & AC Solenoid Valve.Ac Solenoid Valve Replaced | /03L-0 on 781015:2D MSIV Failed to Close from the Control Room.Caused by Failure of Both DC Solenoid Valves & AC Solenoid Valve.Ac Solenoid Valve Replaced | | | 05000304/LER-1978-069, Forwards LER 78-069/03L-0 | Forwards LER 78-069/03L-0 | | | 05000304/LER-1978-070, Cancelled | Cancelled | | | 05000295/LER-1978-071, Cancelled | Cancelled | | | 05000304/LER-1978-071-03, /03L-0 on 781108:during Monthly Performance Test on Containment Spray Pump 2C,a Cooling Water Hose on Diesel Engine Broke.Caused by a Defective Cooling Water Hose on Diesel Engine | /03L-0 on 781108:during Monthly Performance Test on Containment Spray Pump 2C,a Cooling Water Hose on Diesel Engine Broke.Caused by a Defective Cooling Water Hose on Diesel Engine | | | 05000304/LER-1978-071, Forwards LER 78-071/03L-0 | Forwards LER 78-071/03L-0 | | | 05000304/LER-1978-072, Cancelled | Cancelled | | | 05000304/LER-1978-073-03, /03L-0 on 781114:level Xmtr 2LT-950 Was Out of Tolerance by 6.7% in Its Operating range;2LT-951 Was Out of Svc Due to Water in Xmtr(Dv 22-2-78-141).Magnetrols Series 82 Xmtr Out of Tolerance Due to Instrument Drift | /03L-0 on 781114:level Xmtr 2LT-950 Was Out of Tolerance by 6.7% in Its Operating range;2LT-951 Was Out of Svc Due to Water in Xmtr(Dv 22-2-78-141).Magnetrols Series 82 Xmtr Out of Tolerance Due to Instrument Drift | | | 05000304/LER-1978-073, Forwards LER 78-073/03L-0 | Forwards LER 78-073/03L-0 | | | 05000304/LER-1978-074-03, /03L-0 on 781114:during Surveillance Level Xmtrs 2 LT-956 & -957 Were Found Out of Tolerance.Caused by Magnetrol Series 82 Xmtrs Being Out of Tolerance Due to Instrument Drift | /03L-0 on 781114:during Surveillance Level Xmtrs 2 LT-956 & -957 Were Found Out of Tolerance.Caused by Magnetrol Series 82 Xmtrs Being Out of Tolerance Due to Instrument Drift | | | 05000304/LER-1978-074, Forwards LER 78-074/03L-0 | Forwards LER 78-074/03L-0 | | | 05000295/LER-1978-075, Cancelled | Cancelled | |
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