ML20141D909

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Safety Insp Rept 50-289/86-01 on 860110-0207.Violation Noted:Fire Brigade Members Responded to Fire Drill W/O Required Respiratory Protection Apparatus.Portions Deleted (Ref 10CFR73.21)
ML20141D909
Person / Time
Site: Crane Constellation icon.png
Issue date: 03/24/1986
From: Blough A, Conte R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20141D894 List:
References
50-289-86-01, 50-289-86-1, NUDOCS 8604080312
Download: ML20141D909 (41)


See also: IR 05000289/1986001

Text

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U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Report No.

50-289/86-01

Docket No.

50-289

License ho.

DPR-50

Priority --

Category C

Licensee:

GPU Nuclear Corporation

Post Office Box 480

Middletown, Pennsylvania 17057

Facility At:

Three Mile Island Nuclear Station, Unit 1

Inspection At:

Middletown, Pennsylvania

Inspection Conducted:

January 10, 1986 - February 7, 1986

Inspectors:

W. Baunack, Project Engineer, Region I

R. Conte, Senior Resident Inspector (TMI-1)

J. Dunlap, Physical Security Inspector, Region I

A. Krasopoulos, Lead Reactor Engineer, Region I

W. Madden, Security Inspector, Region I

C. Tavares, Physical Security Inspector, Region I

R. Urban, Reactor Engineer, Region I

A. Weadock, Radiation Specialist, Region I

F. Young, Resident Inspector (TMI-1), Region I

3d d

^

Reporting Inspector:h [R. Conte, Seni# Resident Inspector (TMI-1)

Date

[A.' Blojufh, Chief

d

t/ T,

Aporoved By:

Da'te

Reactor Projects Section No. lA

Division of Reactor Projects

Inspection Summary:

Resident and region-based NRC staff conducted routine safety inspections (388

hours) of power operation, focusing on plant and personnel performance.

Specifically, items reviewed in detail in the operations area were: control

rod drive position indication switches; decay heat relief valve actuation;

makeup demineralizer hot spot flush; waste gas routine release; and heatup/

startup activities.

Special focus occurred on licensee event actions for a

reactor protection system breaker shunt trip malfunction and for a partial

loss of ICS/NNI power. Other review items included:

independent technical

and safety review; radiation protection program implementation; security plan

and implementation procedures; fire protection plan and implementation proce-

dures; and licensee action on previous inspection findings.

8604080312 860402

PDR

ADOCK 05000289

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PDR

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Inspection Results:

Licensee personnel exhibited good control of operations and of shutdown and

startup activities. Operators were responsive to off normal events and

properly implemented facility procedures.

Licensee management continued an

aggressive attitude on conducting corrective maintenance and in implementing

an ambitious preventive maintenance program. However, some recent events

revealed poor irterface between the maintenance and fire protection personnel.

Enhanced job planning could have improved licensee activities on the makeup

system demineralizer hot spot flush.

The fire protection program was adequate, except as noted below, and personnel

properly implemented respective procedures.

The inspection identified an

apparent violation on the adequacy of fire brigade response actions (det:lls,

paragraph 7.6.3.1).

The inspection identified a number of other unresolved

issues for which more information is needed.

The security program was adequate and personnel properly adhered to respective

implementing procedures.

The licensee properly implemented the independent technical and safety review

program in accordance with Technical Specifications. The program required

reports on such reviews could be enhanced with more consistent methodology

among divisions. The TS program elements were met despite the diversity and

complexity of the system. This area will continue to be reviewed by NRC's

Region I with respect to review adequecy.

The licensee appears to be properly planning the eddy current outage f:om a

modification and health physics viewpoint.

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DETAIL}

1.

Introduction and Overview

1.1 NRC Staff Actitities

The overall purpose of this inspection was to assess licensee

actiaties for the power operation mode as they related to reactor

sdfety, worker radiation protection, and security / safeguards

measures. Within each area, the inspectors documented the specific

purpose of the area under review, and the scope of inspection

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activities and findings, along with appropriate conclusions. The

inspectors made this assessment by reviewing information on a samp-

ling basis through actual observation of licensee activities, inter-

views with licensee personnel, measurement of radiation levels, or

independent calculation and review of listed applicable documents.

.

1.2 Licensee Activities

The licensee operated the facility at full power during this inspec-

,

tion, except for one week. At the beginning of this period, the

licensee completed residual startup testing for the 100% power

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(startup testing) plateau.

This test was Refueling Procedure (RP)

1550-09, Unit Acceptance Tests. The data were reviewed by the NRC

staff and the review was documented in NRC Inspection Report No.

50-289/85-30.

Between January 27 and February 3,1986, the licensee placed the

plant in cold shutdown in order to break vacuum in the main condens"

,

er to repair leaking pipe expansion bellows on the eighth stage

extraction steam lines. The licensee entered the "C" condenser

through an opening cut in the side of the main condenser.

The

licensee found both eighth stage expansion bellows to be signifi-

cantly deteriorated; both were replaced.

The licensee performed a

,

search of the main condenser and extraction steam lines to locate

and remove pieces of the damaged expansion bellows. A visual

inspection of the remaining tenth and twelfth stage expansion

bellows in the "C" condenser was conducted and no apparent deterio-

,

ration was found.

Based on what was found in the "C" condenser, the licensee decided

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to examine the other eighth, tenth, and twelfth stage expansion

bellows in the "A" and "B" condensers. A visual inspection found

cracking on all four of the eighth stage expansion bellows; they

were replaced.

No apparent deterioration was found on the tenth and

twelfth stage expansion bellows.

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Repair work was completed on February 2.

The damaged expansion

bellcws were sent off site for metallurgical examination to deter-

mine the cause of the failure.

Following restart of the plant, an

approximate 35 MW(e) increase in power was noted.

At the end of the inspection period, the plant was at full' power at

normal operating pressure (2155 psig) and temperature (579 F).

2.

Plant Operations

2.1 Scope of Review

The TMI-1 Resident Office inspectors periodically inspected the

facility to determine the licensee's compliance with the general

operating requirements of Section 6 of the Technical Specifications

(TS) in the following areas:

review of selected plant parameters for abnormal trends

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plant status f roni a maintenance / modification viewpoint, includ-

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ing plant housekeeping and fire protection measures

' control of cngoing and special evolutions, including control

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rcam personnel awareness of these evolutions

cor. trol .of documents including logleeping practices

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implementation of radiological controls

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implementation of the security plan, including access control,

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boundary integrity, and badging practices

The inspectors focused their attention en the areas listed below.

cor.trel roota operations during regular and backshif t hours,

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including frequent obseryation of activitie's in progress, and

periodic reviews cf selected sections of the shift foreman's

log and centrol rcom operator's log and other control roem

claily logs

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followup items on activities that could affect plant safety or

impact plant operations

areas outside the control room

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selected licensee planning teetings

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Because of additional resident inspector coverage at this facility,

special attention was given to those areas listed in Attachment I

to the report. As a result of this review, the inspectors reviewed

specific events in more detail as described in the sections that

follow.

2.2 Findings

2.2.1

General

Licensee management continued their presence and involve-

ment in daily activities. The quality assurance depart-

ment sustained their presence and detailed involvement in

licensee activities.

Positive control and adequate

preparations were demonstrated during the week-long forced

outage for steam line expansion bellows replacement. The

plant shutdown and subsequent startup went smoothly

without significant problems.

2.2.2

Malfunction of CRD Reed Switches

Two methods of control rod position indication are used --

relative and absolute.

Relative position indication

monitors input pulses to the control rod drive (CRD) motor

while absolute position indication monitors the position

of the control rod through the use of reed switches.

There are 45 equally spaced reed switches mounted in a

fiberglass housing that is strapped to the motor tube of

the control rod drive mechanism (CRDM).

These reed

switches are closed by a magnet attached to the torque

taker; as the control rod moves in and out of the core,

the magnet passes by the reed switches. A reed switch is

held closed whenever the magnet is within 1.5 inches above

or below it.

As the reed switch closes, electrical

contact is made varying the resistance of the circuit,

which is then translated to position indication. Once the

magnet passes by, the reed switch opens and electrical

contact is broken.

Occasionally, the licensee experiences problems with these

reed switches.

This is indicated by a " fault" light on

the position indication panel and an asymmetric rod alarm

when the magnet on the torque taker passes a defective

reed switch.

The problem occurs when a film forms on the

surface of the reed switch contacts, preventing the switch

from closing electrically. The film apparently forms on

the reed switches from impurities that leach out from the

glass tubes.

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In the past, the licensee would remove defective reed

switches and send them to the vendor (Diamond Power

Corporation) for repair. The vendor would apply 5 volts at

100 milli-amps to the defective reed switch to " burn-off"

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the film. The success rate was approximately 75%. The

licensee decided to implement this simple method on site

to repair the defective reed switches.

The inspector reviewed corrective maintenance procedure

1430-CRD-19, "CR0 PI Tube Troubleshooting, Repair or

,

Replacement," Revision 3, dated December 11, 1985, Attach-

ment 2, " Repair of a Defective Position Indicator Reed

Switch." The inspector also reviewed the machinery

history file for the CRD system to review job tickets

associated with this procedure.

The inspector found no discrepancies in the procedure.

If

the " burn-off" method fails to solve the problem, the

procedure states tha+ the reed switch will probably need

to be replaced. The ,spector determined the success rate

to be approximately 7C. with respect to the onsite refur-

bishment.

The inspector had no further questions in this

area.

2.2.3

Decay Heat Removal (DHR) System Leakage

During a reactor coolant system (RCS) cooldown on January

29, 1986, when the decay heat removal system was placed

into operation, a relief valve (DH-V57B) lifted spilling

water on the auxiliary building floor and into the floor

drain system. (The relief valve is mounted on the DHR

pump suction line between the BWST suction valve and a

downstream check valve (DH-V148)). The lifting of the

relief valve was attributed to leakage past the check

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valve. This leakage caused a buildup of pressure between

the check valve and the closed BWST suction valve.

Technical Specification (TS) 4.5.4 states that the maximum

allowable leakage from the DHR system components as

<

measured during refueling tests shall not exceed 6 gallons

per hour.

Since this leakage via the lifted relief valve

during system operation was in excess of 6 gallons per

hour, the inspector requested the Plant Review Group (PRG)

to review this occurrence to verify compliance with the TS

requirement.

The PRG met to review this information in relation to TS 4.5.4 on February 4, 1986.

The PRG concluded the piping

which contains the leaking check valve is required by TS

to be tested at no less than 55 psig. The relief valve

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setpoint is much greater than 55 psig (150 psig) and,

therefore, would not and did not lift under conditions

where the R.CS pressure was less than the relief valve

setpoint. The PRG also concluded that under accident

conditions at which RCS high activities might be experi-

enced, the pressure in the OHR suction side piping would

be low.

For these reasons, the PRG concluded the TS was

being met.

Additionally, the PRG reviewed the situation from an

operational point of view and concluded that in order to

avoid radioactive spills and generation of radwaste,

lifting of the relief valve should be avoided. Accord-

ingly, operations will review the decay heat removal

procedure and will provide appropriate cautions against

establishing decay heat removal at RCS pressures that

could challenge the relief vzlves when RCS activity could

cause a significant release.

It was also noted that the leaking check valves (only

DH-V14B leaked during this event; however, OH-V14A is also

known to be leaking) are scheduled for repairs during the

next refueling outage.

The NRC will verify the repair of

these valves at that time. This item is unresolved

(289/86-01-01).

The inspector agreed that, in the interim, until the

valves are repaired during the next refueling outage, the

procedural controls recommended by the PRG were adequate.

2.2.4

Makeup Demineralizer Hot Spot Flush

On January 10, 1986, the licensee decided to flush a hot

spot out of the resin fill line to the makeup and purifi-

cation mixed bed demineralizer (MU-K1A) for ALARA consid-

erations.

The hot spot was located in a Icw section of

piping between CA-V129A and the demineralizer; the dose

rate of the hot spot was 175 R/hr. The valv'e and assoc-

iated piping is located in " mini-valvo alley" on the

305' elevation of the auxiliary building.

Licensee representatives believed the hot spot was com-

posed of contaminated resin that apparently lifted-off the

demineralizer bed and cettled out in a low section of

piping next to CA-V129A. An ALARA review was conducted on

January 8,1986 to determine RWP requirements and the

manner in which the flush would be carried out. Opera-

tions personnel were to line up and vent the demineralizer

to the spent resin storage tank. By using reclaimed water

from the chemical addition room, the flushing water would

pass through the piping, CA-V-129A, demineralizer bed and

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into the spent resin storage tank. The objective was to

move the contaminated resin beads from the piping into the

demineralizer bed.

The licensee depressurized and drained MU-KIA slightly to

allow room for flushing water. Using applicable sections

of OP 1104-54, " Makeup and Purification Demineralizer

Resin Replacement," a'pproximately 50-100 gallons of' water

were used for the flush.

The flush appeared to be suc-

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cessful because the hot spot dose rate was reduced to 500

mR/hr. To return the system to operation, it needed to be

vented and filled with water. During the venting opera-

tien, contaminated resin beads were carried into vent

piping outside of the cubicle along an adjacent pas.sageway.

Because of the r.ew hot spot, the passageway had to be

posted as a radiation area.

During the ALARA review, licensee representatives thought

that there was a resin trap at the exit of the demineral-

12er tank prior to entering the vent header. Based on

this assumption, licensee representatives did not think

that contaminated resin could be swept into the vent

header. A subsequent review of the system drawings by the

licensee revealed that there was no resin trap installed.

A licensee representative stated that almost every resin

tank similar to this one has a resin trap at thG vent

exit; this was the basis for their assumption.

Licensee representatives used poor judgement in assuming

that a resin trap was present at the exit of the

demineralizer tank. The inspector noted that OP 1104-54

contained a caution statement that resin could be observed

in the vent sight glass during the venting operation.

This should have keyed licensee representatives to

the fact that there was no resin trap present. Normally,

small amounts of resin observed in the sight glass is not

a major probles; because it is clean resin. Other aspects

of this flushing operation were carried out well and in

accordance with procedures.

The inspector also reviewed licensee surveys and posting

of the radiation area to determine if they were in accor-

dance with procedural requirements. Current surveys of

mini-valve alley and the adjacent hallway refletting the

new radiological conditions were available at the control

point and the technician performing the survejs appeared

knowledgeable in general survey practices and techniques.

Shielding and posting efforts in the hallway outside

mini-valve alley were found to be adequate. The inspector

had no further questions in this area.

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By mid-February 1986, radiation dose rates inside the vent

header had decayed significantly; the highest reading was

100 mR/hr contact. The inspector agreed with the

licensee *s conclusion that the vent header would not need

to be flushed as long as dose rates from the vent header

continued to decrease and ' remained low.

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The inspector expressed his concern to licensee management

that future hot spot flushing operations of contaminated

resin could be enhanced with better iob planning. The

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licensee representatives acknowledged the inspector's

concern.

The inspector had no further questions in this

area.

2.2.5

Waste Gas Release

d

During release of the

B" waste gat decay tank to the vent

stack on Saturday, January 18, 1986, tne discharge caused

the vent stack radiation monitor to reach the icwcr of two

clarn setpoints.

In response to this alarm, the release

was stopped and c sample was taken tc determine activity

levels in the tank. This sample confirmed the original

calculaticns, and the release, which totaled about 2.8

curies, was completed.

Later that day, approximately five hours after the release

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was completed, one of the offsite radjation monitoring

stations about one-half mile west of the plant alarmec

me.mentarily. The two events were reviewed by the licensee

and were determined to be unrelated.

The offsite

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vadiation monitor alarm was concluded to be a spurious

alarm.

This particylar station transmits its data via

radio signal. No other stations alarmed.

T.he inspector reviewed the licensee's actions to ensure

thet the 6 volution had been conducted in accordance with

applicable station procedures and that the release did not

exceed any discharge limits. The inspector independently

reviewed the antlytical results of the grab samples taken on ths

waste gas tanks to determine the amount of activity baing

discharged and reviewed the meteorological conditions at

the time of the release and the subsequent five hours.

The neteorological dat.a demonstrated that the discharges

from the plant would have been swept f n the direction of

the detector in question.

However, at th9 time of the'

alarm, the licensee had termi.nated the release several

hours prior tc the alarm from tha offsite detectof. Due

to the amount of activity discharged and the dispersion of

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this material that would have occurred, the inspector

concurred with the licensee's characterization of the

event.

2.2.6

Reactor Plant Heatup and Startup

_

On Janua y 27, 1986, the licensee commenced a shutdown of

TMI-1 for a forced outage to repair a leating expansion

bellows on a feed heater extraction steam line (see

paragraph 1.2).

On February 2,1986, the licensee completed repair work

and commenced a plant startup. The plant was returned to

full power by February 6, 1986.

Following restart of the

plant, an approximate 35 MWe increase in power was noted.

The inspector was,present and witnessed major portions of

the forced shutdown and subsequent startup.

In addition,

visual inspection of the ruptured bellows and other

maintenance related work was conducted. The inspector

noted work was being performed in accordance with station

procedures and personnel performing the work were knowledge-

able about their tasks. Discussions with control room

operators demonstrated that they were . aware of plant

status. Porticns of the startup witnessed were perfo.rmed

in accordance with applicable procedures. Actual middle

management presence in the control room and in the plant

was noted on a continuous basis during plant shutdown and

startup.

Presence of management appeared to aid in allow-

ing the licensee to complete the repairs in a timely and

,

safe manner.

2.3 Cor.c.l usi on

Operators continued to conduct themselves in a competent manner and

their performance-orf ented actions reflected a strong training

program. Licensee management and the quality assurance department

continued their presence and involvement in daily activities.

Final

preparation for forced outage work was conducted at a fast pace, but

management control ensured ao adverse regulatcry or safety condi-

tions resulted.

In general, operators were responsive to daily

plant problems as they arose. Overall, procedures were properly

implemented. Radiological control practices were gued.

.

As eculpment problems became evident, appropriate corrective mainte-

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nance was planned, scheduled, and implemented as evidenced by the reed

switch problem. The licensee continued to implement an aggressive

preventive maintenance program. One job, the flush of the makeup

demineralizer hot spot, could have been better theyght out prior to

implementation. Overall, personnel acted cautiously when abnormal

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situations arese, such as during the identification of a hot spot

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immediately after flushing.

Personnel awareness and caution were

also exhibited when the lifted DH relief valve was seated in order

to minimize the spread of contamination and minimize liquid radwaste

generation.

3.

Event Followup

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3.1 Failure of RPS Shunt Trip Breaker

3.1.1

Event Chronology

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At 2:26 p.m. on Jarciary 14, 1986, during monthly Reactor

ProtectionSystemNRPS)surveillancetesting,oneofthe

two a.c. reactor trip breakers (CB-11) failed to open when

its shunt trip feature was tested. The plant was at

normal temperature and pressure at 100% power. Just

prior to the failure, the breaker's undervoltage (UV) trip

feature had been tested successfully.

Subsequent to the init'ial failure of the breaker to open,

the test switch was placed in the shunt trip position two

or three additional times; the breaker still failed to

open.

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In accordance with Technical Specifications (TS 3.5.1.6),

the licensee tested the other a.c. breaker, four d.c.

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breakers, and tagged open CB-11. A faulty circuit board

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was replaced with a unit from stock and CB-11 subsequently

passed the surveillance test at 7:00 p.m. that day.

3.1.2

Event Review

The inspector reviewed the event to determine the follow-

ing information:

'

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details regarding the cause of the event and event

chronology;

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consistency of licensee actions with license require-

ments, approved procedures, and the nature of the

event; and,

proposed licensee actions'to correct the cause of the

--

event.

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The inspector's review of the breaker malfunction included

discussions with cognizant licensee personnel and review

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of the following documents:

system electrical drawings;

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surveillance procedure (SP) 1303-4.1, " Reactor

Protection System;"

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temporary procedure (TP) 400/0.1, "ITE-27H Solid

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State Relays Calibration CRDM Circuit Breaker Modifi-

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cation," Revision 0, MXT 5.3.5.1.2.

The inspector also examined the failed ITE undervoltage

relay to assess the licensee's conclusions.

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3.1.3

Licensee Findings

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The licensee began troubleshooting the ITE/ Brown Boveri

undervoltage relay and discovered that K1 (output relay)

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was not closing when the undervoltage relay was

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de energized.

Subsequent troubleshcoting revealed that a

48/125 VDC control voltage jumper on the undervoltage

relay was plugged in the 48 VDC position instead of the

125 VDC position.

Therefore, the undervoltage relay was

set to operate at an input voltage of 48 VDC instead of

the applied input voltage of 125 VDC. An overheating

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condition was created and was evidenced by yellow discol-

oration and deformation of the originally clear plastic

cover for Kl. Overheating was also indicated on one other

resistor.

The licensee determined the cause of the failure to be

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improper voltage set-up of the ITE undervoltage relay due

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to an incorrectly located control voltage jumper.

The

faulty undervoltage relay was calibrated and checked for

proper control voltage jumper placement. The shunt trip

portion of RPS breaker CB-11 was retested and was found to

be operable.

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As a preventive measure, the licensee inspected the

undervoltage relay for RPS breaker CB-10 and two other

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undervoltage relays in the plant and determined that the

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control voltage jumpers were in the proper location. The

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licensee also functionally tested the shunt trip portion

of CB-10 and verified it to be operable.

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The licensee decided that the event was not reportable;

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but when requested by the inspector, the licensee agreed

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to submit a special report.

3.1.4

NRC Staff Findings

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The licensee's initial actions in response to this event

were timely and consistent with license requirements,

approved procedures and the nature of the event.

The

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inspector agreed with the licensee's conclusion that an

incorrectly located control voltage jumper caused the

output relay (K1) to overheat and fail.

The licensee bought the undervoltage relays from ITE/ Brown

Boveri but had their subsidiary -- Metropolitan Edison,

Lebanon Relay Department -- calibrate then using TP

400/0.1. A QC inspector from the licensee's QC department

witnessed testing of three pridervoltage relays and re-

viewed the data associated with four other undervoltage

relays. Therefore, QC receipt inspection was not per-

formed.

The inspector's review determined that TP 400/0.1 did not

adequately check for the proper location of the control

voltage jumper nor require an independent verification of

that jumper.

From discussions with licensee personnel and

review of calibration data, the inspector determined that

data obtained during calibration was not affected by the

position of the control voltage jumper; therefore, a

visual inspection was the only means to ensure proper

placement of the control voltage jumper.

The licensee has agreed to write a special report concern-

ing this event. Preliminary discussions with the licensee

indicated that corrective actions to prevent recurrence

consist of writing a permanent procedure with a check-off

to ensure proper placement of the control voltage jumper

and performing the calibrations on site. This area will

remain unresolved until the inspector reviews the special

report that is expected to be issued in February 1986

(289/86-01-02).

3.2 Partial Loss of ICS/NNI power

3.2.1

Event Chronology

At 11:24 a.m. on January 24, 1986, a 30 amp Integrated

Control System (ICS) auto power (subfeed) breaker tripped

open causing a loss of auto power to all ICS Bailey

control stations. The plant was at 100% power

steady-state conditions with the ICS in auto control.

At the time, maintenance was being performed on a feed-

water flow transmitter that is powered from ICS auto at

the time.

Both feedwater pumps ran back to approximately 4100 rpm as

designed, causing a small reduction in feedwater flow to

the Once-Through Steam Generators (OTSGs). As feedwater

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flow and OTSG level decreased slightly, Reactor Coolant

System (RCS) pressure and Tave began to increase while

main steam / turbine header pressure decreased.

Numerous alarms in the control room sounded, including a

" Reactor Trip" alarm. A determination was made that the

reactor and turbine had not tripped, but a loss of ICS

auto power had occurred.

RCS pressure was reduced by manually opening the pressur-

izer spray valve and loss of main steam header pressure

was reduced by manually closing the turbine control

valves. After the plant was stabilized, EP 1202-42,

" Total or Partial Loss of ICS Auto Power," was reviewed to

ensure that all immediate and followup actions were

performed. As a result, in accordance with the procedure,

the pressurizer heater low level interlock was bypassed

for RCS pressure control.

Personnel were then dispatched

to determine which breaker had tripped. Work on the flow

transmitter was terminated.

The breaker was closed at 12:38 p.m. and ICS auto power

was restored, after the ICS demand signals for the main

feedwater pumps (MFPs) had been readjusted so that a plant

transient would not occur when the breaker was closed.

All ICS stations were placed in automatic and the plant

was returned to 100% power.

3.2.2

Event Review

The inspectors reviewed the event to determine the follow-

ing information:

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details regarding the cause of the event and event

chronology;

consistency of licensee actions with license require-

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ments, approved procedures and the nature of the

event;

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operator response to the event; and,

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follow-up licensee actions to prevent or reduce

recurrence of the event.

As part of the review, the inspectors had discussions with

cognizant licensee personnel, reviewed various emergency

and alarm response procedures, and reviewed Plant Incident

Report No. 1-86-01.

.

15

.

3.2.3

Licensee Findings

The first indication of a plant transient was a reactor

trip alarm, loss of ICS auto power alarm, and several

other alarms. The loss of ICS auto power causes the

reactor trip alarm; the alarm response procedure also

reminds the operator that a reactor trip alarm occurs when

ICS auto power is lost. By training, operators are

instructed to determine the validity of the reactor trip

alarm before entering ATP 1210-1, " Reactor Trip."

Stooilizing turbine header pressure at a lower pressure

was a significant action because sufficient reduction in

feedwater flow to the OTSGs was realized when the MFPs ran

back to 4100 rpm. Therefore, power was stabilized at 97%

with an elevated Tave. Opening the pressurizer spray

valve restricted increase in the RCS pressure to 2285

psig.

(Reactor trip setting was 2300 psig.)

Design features of the ICS enabled the operators to stabi-

lize the plant quickly. Operators were able to switch

certain transmitters to hand power so that indication

would not be lost, while other ICS control stations failed

as is when the 30 amp breaker opened.

EP 1202-42

adequately identified the failed indicators and other

alternate indicators available for plant control.

During the event, a PORV tailpipe temperature alarm was

received along with indication of a perturbation in the

RCS drain tank level.

The licensee believes a spurious

signal caused the PORV to open for approximately 0.2

seconds. No significant RCS depressurization was ob-

served.

After controlled and deliberate troubleshooting of the 30

amp ICS auto power breaker was performed, it was closed.

Verifying MFP ICS demand signals prior to closing the

breaker ensured a minimal system perturbation.

In addi-

tion, the sliding links for the feedwater flow transmitter

were verified open in case it hao caused the breaker to

trip. When the breaker was closed, test equipment indi-

cated normal current readings.

Initially, licensee representatives believed that the

feedwater flow transmitter caused the 30 amp ICS auto

breaker to open because the transmitter was being powered

!

- up when the transient occurred and it was also located

in the same cabinet as the breaker. However, subsequent

l

testing of the transmitter did not reveal any problems.

After additional troubleshooting was performed, a loose

wire on the 30 amps ICS auto breaker was found. This

i

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,

.

16

apparently caused the breaker to open. As an additional

measure, the licensee checked other breakers for loose

wires.

The licensee stated that there it a potential for ICS

failures during maintenance activities in the ICS cabi-

nets. Therefore, when work is to be performed on the

ICS, the following will be observed:

the shift supervisor will be shown the scope of work

--

using appropriate prints;

headphone communications will be established between

--

the control room and the ICS work location; and,

at least four main areas of the console will be

--

continuously manned.

The licensee's initial review of the transient has pro-

posed the following corrective actions.

--

Review of the light indications for a loss of ICS

auto power. The licensee felt there was an inconsis-

tency in the design logic of the system.

Develop ICS maintenance procedures that identify

--

upstream fuses and/or breakers that could be affected

by the maintenance activity.

Initiate an engineering change so that MFP ICS signal

--

shaping modules are powered from hand rather than

auto.

--

Review and revise, if appropriate, the power supply

for the reactor trip alarm relay.

Incorporate any lessons learned from the incident

--

into the emergency procedures (EP 1202-40,41,42).

--

Provide clear guidance on restoring ICS to auto from

hand while at power in OP 1105-4.

--

Test and replace, as necessary, the 30 amp ICS auto

breaker.

Technical Functions Division will provide an indepen-

--

dent review of the plant incident.

.

- _,

---

.- - .

.

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17

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3.2.4

NRC Findings

The operators' performance during the transient was very

good. There were a number of times when inappropriate

operator action, had it occurred, would have worsened the

transient. Good operator performance reflects proper

training and preparation.

Careful planning by the

licensee before closing the 30 amp ICS breaker prevented a

transient from occurring due to runup of the MFPs.

Modifications to the ICS performed dur ng the last several

i

years were very important to the successful response of

the plant to the transient.

Except for the MFPs running

back to 4100 rpm, all other major ICS equipment failed as

is; also, indicators. automatically had backup power

available.

Procedures were good and provided adequate guidance to the

operators during the transient. However, several proce-

dural improvements are planned to be incorporated by the

licensee.

The inspector's review of licensee corrective action

revealed that the operators understanding of the light

indications associated with the ICS were deficient. By

training, the operators believed that the subfeed au-

to/ hand light should have been out, not the ICS auto

light. A memorandum from the Plant Operations Supervisor

to shift supervisors, dated February 6,1986 (Serial No.

3210-86-0038), discussed a console indication labeling

upgrade for a loss of ICS/NNI power.

In this memorandum,

specific information dealing with the ICS light indication

response to the various breaker trips was discussed. The

memo supported the light-out indication for the ICS auto

light.

The information contained in the memo was dis-

cussed with all the operating crews. The inspector

considered this action adequate.

The licensee agreed to provide a special report on this

event.

The remaining open licensee actions, including the

special report to the NRC, will remain unresolved and will

be reviewed in a subsequent inspection (289/86-01-03).

3.3 Conclusion

These events, in particular the loss of ICS power event, confirm

previous NRC conclusions of excellent operator performance as a

result of a substantial training program.

There apparently was

still some confusion among licensed operators on the proper response

of the loss of ICS/NNI power indicating light system, but this did

.

_

.

18

.

not affect the response to avoid a safety system challenge.

Pending a review of the subject reports, appropriate corrective

actions were proposed or implemented by the licensee.

The RPS breaker event substantiated already identified weaknesses in

the licensee's program for independent verification of equipment

control activities (re: NRC Inspection Report No. 50-289/85-27).

4.

Independent Technical and Safety Review

Facility Technical Specifications (TS) 6.5.1 and 6.5.2 specify the

requirements for Responsible Technical Reviews (RTR) and Independent

Safety Reviews (ISR) of various activities identified in these TS.

During this inspection, the licensee's compliance with these requirements

was reviewed. The specific requirements reviewed and the results of the

review are as follows.

4.1 Division Review and Approval Responsibility

The TS require that each division within the GPU Nuclear Corporation

be responsible for performing RTR and ISR of areas assigned in the

GPUN Review and Approval Matrix. To implement this requirement, a

number of procedures have been developed. The Corporate Procedure

1000-ADM-1291.01, GPU Nuclear Safety Review and Approval Procedure,

has been prepared to control and implement the GPUN safety review

and approval process.

This procedure applies to each division /

facility of GPUN. This procedure makes each Division Vice President

responsible for the development and implementation of divisional

procedures to support the requirements of the corporate procedure.

These divisional procedures have been developed and are identified

as follows:

--

Technical Functions Division, Procedure 5000-ADM-1291.02,

Independent Safety Review;

Nuclear Assurance Division, Procedure 6000-ADM-1291.01, Perfor-

--

mance of Safety Reviews;

Radiological and Environmental Control Division, Procedure

--

9000-ADM-1291.01, Radiological and Environmental Controls

Division Safety Review and Approval Procedure; and,

Three Mile Island Division, Procedure 1034, Plant Review Group.

--

A review of the corporate procedure verified that adherence to this

procedure would ensure compliance with the TS requirements for RTR

and ISR. No specific review was performed on each of the individual

division procedures (except in the area of reports to the division

vice presidents), nor were any requirements of the procedures which

are in addition to TS requirements verified by the inspector.

I

.

19

.

Many of the specific review requirements of the TS are specified in

a GPUN review and approval matrix which is a part of corporate

procedure 1000-ADM-1291.01.

Specific activities described by the

review and approval matrix were selected for review in order to

verify that each division was performing as required. The following

specific subjects requiring review were verified:

Gener al Plant Operating Procedures -- Verified procedures

--

1103 1, " Reactor Coolant Inventory Tracking System" and

1104-45J, " Combustible Gas / Heat Activation Device," received

RTR and ISR by cualified THI-1 and Technical Function Division

personnel, as recuired;

Emergency Operating Procedures -- Verified procedures 1202-12,

--

" Excessive Rad Levels" and 1202-40, " Total Loss of Power to

ICS/NNI," received RTR and ISR by qualified TMI-1 and Technical

Functions Division personnel, as required;

--

Fire Protection Operating Procedures -- Verified procedure

1104-45E, " Fire Service Protection System," received RTR and

ISR by qualified TMI-1 Division personnel;

--

Calibration Procedures -- Verified Procedure 1430-MU-1, " Seal

Leakoff Transmitter Flow Calibration," received RTR and ISR by

qualified TMI-1 Division personnel.

Preventive Maintenance Procedures -- Verified procedure IC-133,

--

" MAP-5 Post-Accident Iodine and Particulate Samples," received

RTR and ISR by qualified TMI-1 Division personnel;

Corrective Maintenance Procedures -- Verified Procedure

--

1410-P-9, " Adjusting MU Pump Mechanical Seals,: received RTR

and ISR by qualified TMI-1 Division personnel.

Surveillance Procedures -- Verified Procedures 1302-17.4,

--

"RM-L-12 Calibration," and 1303-11.39, " Emergency Feedwater

Pump Auto Start," received RTR and ISR by qualified TMI-1

Division personnel.

--

Radiological Controls -- Verified procedures 9100-ADM-4000.06,

9100-PLN-4200.01, and 9100-IMP-4250.08 and Procedure Change

Requests (PCRs) 1-RC-85-0103,1-RC-85-0088, and 1-RC-85-0045

received RTR and ISR by qualified radiation controls personnel;

--

Environmental Monitoring Procedures -- Verified procedures

9420-SUR 4523.05, " Determination of REMP Investigational Levels

and Subsequent Actions," 9420-IMP-4522.12. "REMP Sample Collec-

tion Procedure," and 9420-SUR-4570.01, "TMINS Hydrographic

Survey," received RTR and ISR by qualified radiological con-

trols personnel;

-

..

20

Emergency Plan Implementing Procedures -- Verified TCN

--

1-86-0002 to 1004.2, " Emergency Directions," TCN 1-85-0179 to

1004.4, "Callout of Duty Roster Personnel," TCN 1-85-0193 to

1004.5, " Communications and Record Keeping," and PCR

1-EP-86-0008 to 6415-IMP-1300.10, "Onsite/0ffsite Radiological

and Environmental Monitoring," received RTR and ISR by quali-

fied members of the Emergency Preparedness Department;

Security Plan and Implementing Procedures -- Verified the

--

security plan and procedure 7000-ADM-1291.01, " Performance of

Safety Reviews," received RTR and ISR by qualified security

personnel;

Quality Assurance Plan and Implementing Procedures -- Verified

--

the GPUN Operational Quality Assurance Plan and procedures

1000-ADM-7215 01, "Important-to-Safety Material Nonconformance

Reports," anc 1000-ADM-7215.02, "GPUN Quality Deficiency

Reports" received RTR and ISR by qualified Nuclear Assurance

Division personnel;

Process Control Program Implementing Procedures -- Verified

--

procedure 1104-281, " Process Control Program - Hittman," and

1104-28D, " Packaging Non-Compactible Trash," received RTR and

ISR by qualified TMI-1 division personnel;

Offsite Dose Calculation Manual Implementing Environmental

--

Controls Procedures -- Verified procedures 9420-IMP-4522.02,

"REMP Sample Collection Procedures TLDs," and 9420-IMP-4522.03,

"REMP Sample Collection Procedure Fish, Aquatic Sediment,

Aquatic Plants," received RTR and ISR by qualified

Environmental Controls personnel;

--

Special Temporary Procedures (STP) -- Verified STP No.

1-85-0048, " Main Generator Manual Excitation Test," and STP No.

1-85-0050, "0TSG A/B Blowdown," received RTR and ISR by

qualified TMI-1 Division personnel;

Technical Specifications / License Change Requests -- Verified

--

Technical Specifications Change Requests 127, 128, and 133

received RTR and ISR by qualified Technical Functions personnel

or by qualified reviewers from other divisions as permitted by

procedure 1034, " Plant Review Group;"

--

Licensee Event Report (LER) -- Verified LER 85-001-0,

" Inadvertent ESAS Actuation," and LER 85-002, " Manual Reactor Trip Due to Fire in the Control Rod Drive Transfer Switch,"

received RTR and ISR by qualified TMI-1 and Technical Functions

.

Division personnel;

!

_

.

21

-

Review of Written Summaries of Audit Reports -- Verified GPUN

--

Audit Reports S-TMI-85-03, "TMI-1 and TMI-2 Radwaste

Management," and S-TMI-85-11, TMI-1 Operations," received

reviews as required by Section IV of the TMI-1 Review and

Approval Matrix;

--

Investigation of Violations of Technical Specifications -- The

Plant Review Group (PRG) is currently reviewing violations of

TS. Examples of violations of TS being reviewed by the PRG are

Quality Deficiency Report SRC-049-85, dealing with oxygen

concentration in the reactor coolant system, TCN 1-86-0005 not

being reviewed within 14 days as required, and a missed

surveillance requirement on RM-A5.Section IV of the TMI

Review and Approval Matrix specifies certain specific

documentation requirements associated with the investigation of

violations of TS.

There appears to be no question that

violations of TS are being reviewed by qualified TMI-1 division

personnel as evidenced by PRG meeting minutes. However, the

documentation of these reviews is not as required by the notes

associated with Section IV of the Review and Approval Matrix.

Additional information relative to documentation is identified

in the following paragraph.

--

Review of Every Unplanned Release of Radioactivity to the

Environment -- The inspector reviewed Radiological

Investigation Report No.85-008, dealing with a small release

(.7 Ci) on October 28, 1985, resulting from makeup pump 1A

maintenance, Plant Incident Report No. 1-85-19, dealing with a

release (46.3 C1) on December 30, 1985, also resulting from

makeup pump 1A maintenance and Radiological Investigation

Critique minutes dealing with a small release (1.4 C1) on

December 17, 1985, resulting from gas compressor maintenance.

These documents show that releases of radioactivity to the

environment are being reviewed by qualified TMI-1 Division and

Radiation Controls Division personnel. As discussed above,

Section IV of the TMI Review and Approval Matrix specifies cer-

tain specific documentation requirements for reviews of every

unplanned release of radioactivity to the environment and

investigations of violations of TS.

Reviews of these items are

being conducted.

However, the documentation of these reviews

does not entirely satisfy the documentation requirements

specified in the matrix.

The licensee will more clearly define the method for documenting

the review of TS violations and unplanned releases. This item is

unresolved pending completion of licensee action as noted above and

subsequent NRC Region I review (289/86-01-04).

Also, included in

this unresolved item is that the licensee will also more clearly

define what constitutes an unplanned release of activity to the

__

.

22

.

environment which requires review under Section IV of the Review and

Approval Matrix and Section 6.5.1.10 of the Technical Specifica-

tions.

4.2 Reviewer Qualifications and Designation

The TS specify the qualifications for RTR and ISR.

Step 4.1 of

corporate procedure 1000-ADM-1291.01 requires "each divisional vice

president will be responsible for having ISR and RTR identified

within his organization."

The inspector serified that reviewers for RTR and ISR were designat-

ed in writing as follows.

Memo dated November 1,1985, from the PRG Chairman, TMI-1

--

designates the RTR and ISR for the THI-1 division.

--

Memo dated December 19, 1984, from the security manager desig-

nates the. Security Department RTR and ISR.

Memo dated October 7, 1985, from the safety review coordinator

--

designates the Quality Assurance Department, Training and

Education Department, Nuclear Safety Assessment Department, and

the Emergency Preparedness Department RTR and ISR,

--

Memo dated December 18, 1985, from a senior licensing engineer

identifies the safety reviewers for the Technical Functions

Division.

Memo dated December 5, 1985, from the Direct m.

Radiological

--

and Environmental Controls Division, designat,4 the Radiation

Controls - THI-1, Environmental Controls - TMI-1, Environmental

Controls - Corporate, and Radiation Engineering - Corporate

Technical and Safety Reviewers.

The TS specify safety reviewer qualifications. The corporate safety

Review and Approval Procedure specifies the same qualification

requirements and in addition requires training and retraining for

RTR and ISR.

The formal records documenting the qualifications and training of

reviewers are being maintained at the corporate office in

Parsippany. Sample unofficial records being maintained at the site

indicate that reviewer qualifications and training requirements are

being met.

For each of the specific items reviewed by the inspec-

tor, the RTR and ISR were verified as being on the list of qualified

reviewers.

i

23

.

4.3 Review Records

Technical Specification 6.5.1.13 requires records of RTR be main-

tained. Step 4.13.1.2 of the corporate procedure 1000-ADM-1291.01,

states " records of documents prepared, reviewed, and approved in

accordance with the GPU Nuclear Safety Review and Approval Matrix

will be maintained for the life of the operating license."

The format of the records maintained show that reviews are being

parformed in accordance with the Review and Approval Matrix vary

considerably among the various groups involved in performing re-

views. However, the inspector found that, for the specific items

reviewed, sufficient records are being maintained to show RTR and

ISR are being performed as required by the matrix. The quality of

these reviews will be subject to inspection in the future. Qualifi-

cation records were reviewed as noted in paragraph 4.2.

Technical Specification 6.5.2.7 requires that reports of ISR be

prepared, maintained and transmitted to the cognizant division vice

president. The corporate Safety Review and Approval Procedure

1000-ADM-1291.01 in Step 4.13.1.3 requires " Reports of all technical

reviews and independent safety reviews will be prepared and trans-

mitted to the responsible division vice president. They will be

maintained for the life of the operating license."

Neither the TS or the corporate procedure specify any time period

for submitting the report. Also, each of the division procedures

differ somewhat in their requirements relating to reports to the

division vice presidents. The requirement of each divisional

procedure and how each division complies with the requirement for

submitting a report to the vice president is as follows.

--

TMI-1 Division -- Procedure 1034 specifies " Reports of re-

views...shall be transmitted periodically to the vice presi-

dent, the Operation? and Maintenance Director, and the Plant

Engineering Directoe of TMI-1."

Reports of reviews by the

TMI-1 division are transmitted to the vice president by the

forwarding of Plant Review Group meeting minutes and by Weekly

Plant Review Group supplementary reports.

--

Technical Funct'.ons Division - The Technical Functions Proce-

dure 5000-ADM-1291.02 specifies " Engineering Services shall

prepare reports of reviews for each plant annually.

These

reports shall be retained at the corporate storage area and

copiet, transmitted to the vice president, Technical Functions,

and tre cognizant plant vice president. Each report shall be a

summary of Independent Safety Reviews conducted; it will

include irregularities and a listing of all reviews conducted

during the period, by subject, as listed in the Review and

Approval Matrix." One report of reviews was prepared by a

.

24

.

senior licensing engineer. This report, dated April 19, 1984,

covers the period August 28, 1982, to April 1984.

The report

is approximately 75 pages in length and, basically, lists

the procedures and other items reviewed by Technical Functions.

Also, a report dated March 15, 1985, identified as 1984 Annual

Report - Safety Review Process is a two page report which

summarizes the reviews conducted during 1984.

The report also

summarizes minor administrative deficiencies noted.

Nuclear Assurance Division -- The Nuclear Assurance Division

--

Procedure 6000-ADM-1291.01 in the Records Section, Step,

4.13.1.3 states " Copies of all safety evaluations developed by

Nuclear Assurance or where Nuclear Assurance performed the

Independent Safety Review will be sent to the Nuclear Assurance

Safety Review Coordinator (NASRC).

The NASRC will assure they

are maintained for the life of the operating license."

In

accordance with this procedural requirement, the site QA and

Emergency Preparedness groups forward reports of reviews they

perform to the Nuclear Assurance Safety Review Coordinator.

Although the Nuclear Assurance Division Procedures do not

require a report to the responsible division vice president, a

report dated April 11, 1984, was submitted to the responsible

vice president.

This report summarized reviews performed since

the process started in August 1982 until April 1984. This

report stated it was submitted in accordance with the corporate

procedural requirement. Although no procedural guidance was

provided, the report summarized the reviews that were done by

document type and number and also identified certain trends

and/or problems identified.

Administration Division - The Administration Division Procedure

--

7000-ADM-1291.01 requires " Reports of all Technical Reviews and

Independent Safety Reviews will be prepared and transmitted to

the Division Director - Administration. They will be main-

tained for the life of the operating license." A report which

lists all safety reviews vhich have been performed of

Administration Division documents since the inception of the

safety review system in August 1982 was submitted to the respon-

sible vice president on February 19, 1985.

Radiological and Environmental Control Division - The Radio-

--

logical and Environmental Controls Division Procedure

9000-ADM-1291.01 in Step 5.7 requires "A summary of the respon-

sible technical reviews and the independent safety reviews

performed by THI-1 and Oyster Creek R&EC Division personnel

shall be forwarded to the vice president, R&EC, on a semi-annual

oasis." Although the procedure specifies a summary of RTR and

ISR be forwarded to the vice president on a semi-annual basis,

the Radiological Controls Group lists reviews performed in a

Radiological Controls Monthly Status Report. Also, a different

group in the same division, the Radiological and Environmental

i

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.

25

.

Controls Group, in response to an April 1984 audit finding

which identified the group's failure to provide the required

report to the vice president, committed to providing a summary

report of reviews to the vice president on a semi-annual basis

as the division procedure requires. During this inspection, it

was noted these semi-annual reports had not been submitted.

Prior to the conclusion of the inspection, a report of Technical

and Safety Reviews performed by TMI Environmental Controls

personnel during 1985 was submitted. This three page report

only listed the procedures / documents reviewed. The licensee

felt this report satisfied the TS requirement.

As can be seen from the above, in the absence of any specific

guidance, the frequency at which the required report is submitted to

the responsible vice president varies considerably from division to

division and also the content of the reports varies from a

listing of documents reviewed to an analysis of the reporting

division's review process.

These problems were discussed with licensee representatives. The

licensee representatives stated the Corporate Safety Review and

Approval Procedure 1000-ADM-1291.01 is currently in the process of

being reviewed and that to correct the problems identified during

this inspection, the revision to the procedure will address both the

frequency and the content of the reports to the cognizant division

vice president. This revision to the procedure will be issued by

June 30, 1986. This item is unresolved (289/86-01-05).

4.4 Conclusion

The licensee's review and approval system is complex; but, overall,

TS requirements are satisfied by each of the divisions. How that

goal is achieved is diverse among the divisions. The reports of

reviews could be enhanced by a more consistent and unified approach

based on corporate guidance. NRC Region I will continue to

review this area with respect to unresolved items noted above and

with respect to quality of these reviews.

5.

Outage Planning and preparation

As part of the health physics programmatic review, the inspector reviewed

the special preparations for the next outage that will involve signifi-

cant health physics related work. Presently, the next scheduled evolu-

tion is an eddy current inspection scheduled in March 1986.

Discussions with the Radiological Field Operations supervisory staff

indicate that planning and preparations for the upcoming March outage

have been initiated in a timely fashion.

Representatives from the

Radiological Controls department have been involved in preliminary outage

planning meetings.

i

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_

_ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ _____ _ _ _ _ _ _ _ _ __

-

.

26

'

The licensee indicated that in plant health physics (HP) technician staff

will not be augmented with contractor personnel during the outage. The

HP staff will be supplemented by discontinuing the cyclic training shift,

which normally requires a percentage of the staff to be in training.

Shift coverage during steam generator work will be split into two 10-hour

work shif ts and a single 4-hour cleanup shif t.

The cleanup shift will be

devoted to decontamination and housekeeping efforts in support of outage

activities.

Additional licensee preparatory effort has included:

designation of a responsible individual establishing an outage

--

control point on the 306-foot elevation of the intermediate

building;

scheduling a pre-outage calibration of instrumentation that will

--

become due for calibration during the outage; and,

scheduling pre-outage qualification boards for all technicians who

--

will become due for requalification during the outage.

The inspector reviewed licensee surveys and posting of several

newly-developed hot spots in the hallway adjacent to mini-valve alley

in the auxiliary building. The hot spots were created when radioactive

resin from a makeup and purification system demineralizer was inadver-

tently introduced into a waste gas header (see paragraph 2.2.4).

Current surveys of the alley and hallway reflecting the new

radiological conditions were available at the control point and the

technician performing the surveys appeared knowledgeable in general

survey practices and techniques. Shielding and posting efforts in the

hallway outside the alley were found to be adequate.

6.

Security Program and Implementation

6.1 MC 81018 - Security Plan and Implementing Procedures

The licensee was adhering to the Modified Amended Physical Security

Plan (MAPS) for Three Mile Island Nuclear Station, Units 1 & 2,

Revision 21, dated January 7, 1986.

Implementing procedures were

reviewed and were adequate to satisfy the general performance

requirements and objectives of 10 CFR 73.55. No unauthorized

changes were identified.

6.2 MC 81020 - Management Effectiveness

The inspectors interviewed and observed members of the security

force and found that they were knowledgeable of their duties and

appeared very professional.

Since the last inspection, the licensee

has made the following changes or upgrades to security equipment:

.

27

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THIS PARAGRAPH CONTAINS SAFEGUARDS INFORMATION

AND IS NOT FOR PUBLIC DISCLOSURE, IT IS

INTENTIONALLY LEFT BLANK.

.

Quarterly management meetings are held between the two GPU Nuclear

sites and the corporate headquarters in Parsippany, New Jersey.

These meetings aid in keeping upper level management aware of

current issues and problems so that they may assist lower level

management and keep them informed of current trends and future

plans.

6.3 MC 81022 - Security Organization

The licensee's security management structure and chain of command

were reviewed by the inspectors and found to be in conformance with

the approved physical security plan, contingency plan, and imple-

menting procedures. The licensee's response to several actual

contingencies and one simulated contingency was observed by the

inspectors and was found to be adequate.

6.4 MC 81038 - Records and Reports

Weekly and quarterly security equipment test records were reviewed

by the inspectors and found to have been accomplished in accordance

with the physical security plan. A review of Security Event Report

No. 85-01, dated January 20, 1985, disclosed that it was timely and

complete.

6.5 MC 81042 - Testing and Maintenance

The testing and maintenance program for security equipment conformed

to the physical security plan and implementing procedures. The

inspectors observed the testing of intrusion and access control

equipment and found the systems acceptable.

.

.

28

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6.6 MC 81046 - Locks, Keys, and Combinations

The inspectors observed the key and lock custodian conduct a securi-

ty key inventory and a test of the card key system. All security

keys were accounted for in accordance with the security plan and

licensee procedures.

6.7 MC - 81052 - Physical Barriers (Protected Areas)

The inspectors verified by observation that the PA physical barriers

were maintained by the licensee in accordance with the physical

security plan.

6.8 MC 81054 - Physical Barriers (Vital Areas)

The inspectors toured the vital areas and verified by observation

that the licensee was maintaining the physical barriers surrounding

the vital areas in accordance with the physical security plan.

THIS PARAGRAPH CONTAINS SAFEGUARDS INFORMATION

AND IS NOT FOR PUBLIC DISCLOSURE

IT IS

INTENTIONALLY LEFT BLANK.

6.9 MC 81058 - Security System Power Supply

The inspectors determined that the licensee was maintaining an

adequate uninterruptible power supply system to provide emergency

power to physical security equipment in accordance with the physical

security plan.

The inspectors verified, through a review of weekly

and quarterly test and maintenance records, that the power supply

system was tested at periodic intervals.

6.10 MC 81064 - Compensatory Measures

The inspectors determin1d by reviewing records that compensatory

measures conformed to the physical security plan and implementing

procedures.

Security personnel demonstrated adequate knowledge of

compensatory measures when interviewed by inspectors.

THIS PARAGRAPH CONTAINS SAFEGUARDS INFORMATION

AND IS NOT FOR PUBLIC DISCLOSURE, IT IS

INTENTIONALLY LEFT BLANK.

.

.-

.

_. .

. -.

.-

.

.

29

.

6.12 MC 81070 - Access Control (Personnel)

The inspectors determined that the licensee was maintaining

personnel access control to the PA and VA in conformance with the

physical security plan and implementing procedures.

6.13 MC 81072 - Access Control (Packages)

The inspectors observed the search process at the entry control

points into the PA and verified that packages and material were

being processed into the PA in conformance with the physical securi-

ty plan and implementing procedures.

6.14 MC 81078 - Detection Aids (Protected Areas)

The licensee demonstrated to the inspectors that the intrusion

detection system (IDS) would detect penetration tests of the PA in

conformance with the security plan and implementing procedures.

6.15 THIS PARAGRAPH CONTAINS SAFEGUARDS INFORMATION

AND IS NOT FOR PUBLIC DISCLOSURE, IT IS

INTENTIONALLY LEFT BLANK.

6.16 MC 81084 - Alarm Stations

Observation by the inspectors of the operations and tests of equip-

ment in the central and secondary alarm stations verified that the

licensee was maintaining them in accordance with the security plan

and implementing procedures.

6.17 MC 81088 - Communications

The inspectors confirmed by observing tests and by interviewing

central and secondary alarm station operators that the licensee was

maintaining internal and external communications in conformance with

the security plan and implementing procedures.

6.18 MC 81501 - personnel Training and Qualification

The licensee's training and qualification (T&Q) program was found by

the inspectors to be implemented as outlined in the T&Q plan.

However, Enclosure 2 to Revision 6, dated August 7, 1984, omits the

conditions or standards for task 1.3, " Directs Site Protection

Force," which is a task listed in Enclosure 1.

The licensee advised

that the omission has been identified and is included in a proposed

.

30

.

revision (No. 7). The revision is currently in the review process

and it will correct this omission. A random review of 25% of the

training records reflected that training and qualification or

requalifications were current.

6.19 MC 83601 - Safeguards Contingency Plan

The inspectors determined that the licensee's program for responding

to security threats and other contingencies as outlined in the

Safeguards Contingency Plan (SCP) and its implementing procedures

was adequate. The inspectors observed the security force respond,

in accordance with the SCP, to several alarms and to one simulated

contingency.

No deficiencies were noted.

6.20 Conclusion

Based on this sampling review, the licensee has complied with the

plan and is adhering to implementing procedures.

7.

Fire Protection / Prevention

,

The inspector reviewed several documents in the below listed .reas of the

program to verify that the licensee had developed and implemented ade-

quate procedures consistent with the Fire Hazard Analysis (FHA), Final

Safety Analysis Report (FSAR), and Technical Specifications (TS). The

documents reviewed, the scope of review, and the inspection findings for

each area of the program are described in the following sections.

7.1 Program Administration and Organization

'

The inspector reviewed the following licensee documents:

Technical Specifications, Section 6, Administrative Controls;

--

Administrative Controls - Fire Protection Program Procedure

--

No., 1038, Revision 11; and,

Fire Protection Evaluation, Procedure 5000-ADM-7370.01

--

(EP-013), Revision 2.

The scope of review was to ascertain that:

personnel were designated for implementing the program on site;

--

and,

qualifications were delineated for personnel designated to

--

implement the program.

No unacceptable conditions were identified.

w-

-

w

31

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7.2 Admir.istrative Control of Combustibles

The ,r.spector reviewed the following licen ee documents:

" Control of Transient Combustible Materials," Administrative

--

Procedure No. 1035, Revision 11; and,

(

" Good Housekeeping," Administrative Procedure 1008, Revistor.

--

14.

The scope of review was to verify that the licensee had developed

administrative centrols which included:

special authorization for the use of combustible, flammable, or

--

explosive hazardous material in safety-related areas;

prohibition on the storage of combustible, flammable, or

--

explosive hazardous material in safety-related areas;

the removal of all wastes, debris, rags, oil spills, or other

--

combustible materials resulting from work activities or at

3

the end of each work shift, whichever is sooner;

all wood used in safety-related areas is to be treat;d with

--

flame retardant;

periodic inspection for accumulation of combustibles;

--

transient combustibles to be restricted and controlled in

--

safety-related areas; and,

housekeeping to be properly maintained in areas containing

--

safety-related equipment and components.

No unacceptable conditions were identified.

7.3 Administrative Control of Ignition Sources

The inspector reviewed Maintenance Procedure 1410-Y-26, " Control of

Hot Work," Revision 12. The scope of review was to verify that the

licensee had developed administrative controls which included:

requirements for special authorization (work permit) for

--

activities involving welding, cutting, grinding, open flame ,

or other ignition sources and that they 3re properly safeguard-

,

ed in areas containing safety-related equipment and components;

i

and,

. . . . .. _

__

_

_

.

32

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prohibition on smoking in safety-related areas, except where

--

" smoking cormitted" areas had been specifically designated by

plant management.

The inspector observed that the referenced procedure is not clear in

the requirement for fire watchers to stay on location 30 minutes

aftGr the hot work is completed. The licensee stated that this is

the case at TMI. A procedure change was issued that clearly states

this requirement.

7.4 Other Administrative Controls

The inspector reviewed the following licensee documents:

Technical Specifications, Section 6, Administrative Controls;

--

and,

'

General Employee Training - Module IV, Fire Protection, Revi-

--

sion 1.

The scope of review was to verify that the licensee had developed

administrative controls which require:

work authorization, construction permit, or similar arrangement

--

is provided for review and approval of modification, construc-

tion, and maintenance activities which could adversely affect

the safety of the facility;

fire brigade organization and qualifications of brigade members

--

are delineated;

fire reporting instructions for general plant personnel are

--

developed;

periodic audits are to be conducted on the entire fire protec-

--

tion program; and,

fire protection / prevention program is included in the

--

Itcensee's QA program.

No unacceptable conditions were identified.

7.5 Equipment Maintenance, Inspection, and Tests

The inspector reviewed the following randomly selected documents to

determine whether the licensee had developed adequate procedures

which established maintenance, inspection, and testing requirements

for the plant fire protection equipment:

" Fire Pump Capacity Testing," Surveillance Procedure (SP)

--

3303-R2, Revision 6;

.

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.

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. _ _ _ -

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33

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"Hese Station Inspection," SP 1301-12.2, Revision 5;

--

" Fire Pump Periodic Operation," SP 3303-M1, Revision 13;

--

" Diesel Fire Pumps Battery Check," SP 3301-Q2, Revision 8;

--

" Fire System Diesel Battery Check," SP 33Cl-W2, Revision 4;

--

" Fire Protection Instrumentation Non-Supervised Circuits Test,"

--

SP 1303-12.14, Revision 3;

" Fire System Valve Line Up Verification," SP 3301-hl,

--

Revision 20; and,

" Fire Pump Diesel Fuel Sampling," SP 3303-Q1, Revision 9.

--

In addition to reviewing the above documents, the inspector reviewed

the maintenance / inspection / test records of the procedures listed

above to verify compliance with Technical Specifications and estab-

lished procedures.

No unacceptable conditions were identified.

7.6 Fire Brigade Training

7.6.1

Procedure Review

The inspector reviewed the following licensee procedures:

" Fire Brigade Training Administrative Program,"

--

Administrative Procedure 6210-ADM-2620.03;

" Administrative Controls, Fire Protection Program,"

--

AP 1038; and,

Amendment 44 to Facility Operating License No.

--

ORP-50.

The scope of review was ',o verify that the licensee had

developed administrative procedures which included:

requirements for announced and unannounced drills;

--

requirements for fire brigade training and retraining

--

at prescribed frequencies;

requirements for at least one drill per year to be

--

performed on a "backshift" for each brigade; and,

i

,

_

- _ _

_ - _ _ _ _ .

__

._

_ _ _ _

.

34

.

'

requirements for maintenance of training records.

--

No unacceptable conditions were identified.

7.6.2

Records Review

The inspector reviewed training records of fire brigade

i.

members for calendar years 1985 and 1986 to ascertain that

they had attended the required quarterly training and

participated in a quarterly drill, and received the annual

hands-on fire extinguishment practice.

In addition to the

records reviewed, the inspector witnessed a fire drill.

No unacceptable conditions were identified, except as

follows.

7.6.3

Fire Brigade Training Findings

7.6.3.1

Fire Brigade Training Violates T.S. Requirements

The inspector requested to observe a fire brigade drill

,

scheduled to be performed during the inspection.

The

inspector positioned himself by the firefighter's equip-

ment locker expecting that the firefighters would don

their protective gear responding to the drill. The senior

'

resident inspector observed activities at the scene.

>

Upon announcing the drill, only one fire fighter came to

,

the locker. The remainder of the brigade responded to the

scene of the fire and proceeded to simulate fire extin-

l

guishment.

j

'

The inspector noted that no one was wearing respiratory

'

protective equipment. THI-l T.S. 6.4.2 requires that the

training of the brigade shall meet or exceed NFPA

Standard No. 27(1976 edition) training requirements.

,

!

This standard requires the use of respiratory protective

equipment during drills.

j

'

A review of the licensee's procedures for fire emergencies

and drills identified that these procedures do not have

the requirements to respond to drills wearing respiratory

protection.

This is an apparent violation of the training requirements

identified in NFPA 27 included in T.S. 6.4.2

,

(289/86-01-07).

.

,

__

- _ _ _ _ _ _ . _

_ _ . _ _ _ _ _ _ _ _ _ . . _ ~ _ _ _ _ _ _ - - - - _ - - _ _ _ _ _ _ _ _ _ _

__

_

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35

.

7.6.3.2

Inadequate Fire Brigade Training Record Keeping

The inspector reviewed the fire brigade training records

to ascertain compliance with licensing conditions set

forth in a letter to NRC, dated January 7,1984 (Hukill to

Stolz).

This letter iterates the revised fire protection

program plan for TMI-1 and is a licensing basis document.

One requirement of the fire protection program is that

fire brigade members should participate in drills quarter-

ly but must participate in at least two drills per year.

The inspector observed that the method used to track the

training given to firefighters is cumbersome and mistake

prone.

In reviewing less than a 10*4 sample of firefighter

training, it was observed that few firefighters had

fulfilled the drill attendance requirement "at regular

intervals" for the year by participating in drills sched-

uled only a month apart. Existing NRC guidance specifies

that drills be scheduled at regular intervals. The same

t

review also identifiec' one firefighter on the brigade

eligibility list who did not have the required number of

drills. The inspector noted that the licensee utilized &n

inefficient record keeping system. The inspector also

noted the large size of the fire brigade. The inspector

questioned the relationship between the cumbersome record

keeping system, the large brigade size and the problems

with attendance at fire drills. The &bove are collec-

tively recognized as an unresolved item pending a detailed

review of the licensee's training procedures in this arei

g

by Region I (289/86-01-08).

7.7 Facility Tour

The inspector examined fire protection water systems, including fire

pumps, fire water piping and distribution systems, post-indicator

valves, hydrants, and contents of hose houses. The inspector toured

accessible vital and non-vital plant areas and Axamined fire detec-

tion and alarm systems, automatic and manual fixed suppression

systems, interior hose stations, fire barrier penetration seals, and

fire doors. The inspector obserted general plant housekseping

conditions and randomly checked tags of portable extinguishers for

evidence of periodic inspections. No deterioration of equiptent was

noted.

The inspection tags attached to extir:gvishers indicated that

monthly inspections were performed.

No unacceptable conditions were identified, e.xcept as follows.

,

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7.7.1

Inoperable Fire Ocors

The inspector observed that a number of doors labeled " fire

doors" would not close automatically. The licensee explained

that this is caused by air pressure differentials.

The lit.enses

committed to identify the doors involved af.d, if these doors

are ih fire walls, they will gither be fixed or other compensa-

tory measures Hill be taken in accardance yith the 10 require-

ments. This is an uaresolved item (289/B6-01 09).

In response to an NRC security inspector' cor/;ern, the licensee

initiated work on security doors that were also fire doofi (see

paragraph 6.8).

Apparently, fire protect.icrz personnel were not

factor'ed i,to the pro-job planning phase and those actions

would have decated the fire door,

Subsecuent to identification

cf the problein by a liSnsee operations engineer, appropriate

corrective action was taken to maintain the door for both fire

and security purposes. The inspector concluded that the

operations engineer was quick to ider.tify the problem, but the

incident showed poor Job planning by the maintenance depart-

ment.

The inspector had no further questions in this area.

7.7.2

Fire Drill and_pg e Systems !_nicerability

For the fire drill observed by the inspector, the licensee

provided the inspector with the drill scenario.

The scenario

involved a fire in the pressurizer heater cabinets switchgear

located on the 322' elevation in tha turbine building.

The inspector was stationed by the fire locker waiting fcr the

drill to start. When the drill was announced, the inspector

was not able to hear the announcement and the fire alarm was

-

barely audible. Because of this system's malfunction, a member

of the fire brigade also did not hear the announcement and did

not respond.

The licensee became aware of the system'.s mal-

function and committed to have the system repaired and en-

hanced. The enhancerrent will include additional speakers to

cover all plant areas and procedures for system surveillance.

This is an unresolved item (289/86-01-10).

7.7.3

Fire Service Water use for__ Utility Purposes

The inspector observed that plant personnel are using water

f rom hose stations to backwash and flush equipment. NFPA does

not recommend tnis practice because prolonged operation of

centrifugal pumps at shut of f pressure or low flow rates may

prove harmful to the pumps.

Using the fire pumps in this

manner will require additional maintenance and surveillance.

Additionally, from a human factors engineering standpoint,

,

a.

..

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.. .. - _. -

..

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37

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the operators may get used to seeing tne pump running; so, if

+

the pyTp starta tacause of either a broken main or due to a

fire, either conditicn reay not be quic9.ly diagaosed.

This is an unresolved item pending eviaw of the licensee's

actions in this area by NRC Region I (789/86-01-11).

.

8.

Licensee Event Report Onsjf.e__ Review

1

The inspector reviewed Licensee Event Report (LER) No. 85-004-0, which

was submitted to the NRC on Decenber 26, 1985, in accordence with 10 CFR 50.73. The LER described a breach of a fire barrier during mcdification

'

work to a makeup pump wall with a sealant or contir,uous fire watch post.ed

as required by TS 3.18,7.

Dueing this inspection period, the inspector reviewed the licensee's

submitted report on the ev6nt.

The report complied wf?.h 10 CFR 50.73 and

accur.ately reported the facts of the event, properly evaluated the event,

and accurately reflected the corrective actions taken. An underlylr.g

cause was that this was the first time in a number of years maintenance

}

personnel did this type of work which is normally performed by contrac-

tors. The event did point out a need for closer supervisory scrutiny by

the maintenance department and better comnunications with fire protection

personnel.

9.

Licensee Action on Previous Inspection Findings

(

The inspector reviewed licensee action on prevfous inspection findings to

ensure that the licensee took appropriate action in response to the

findings or by self-initiative and that the licensee's .acticn was timely.

9.1

THIS PARAGRAPH CONTAINS SAFEGUARDS INFORMATION

f

AND IS NOT TOR PUBLIC DISCLOSURE, IT IS INTENTIONALLY LEFT SLANK.

The inspectors observed the licensee test all zones of the system

and they functioned according to test precedures which confcrmed to

general perf-crmance requirements.

>

9.2 (Closed) Violation (289/85-11-01): Individual not preperly

processed into the protected area at the screenhouse area

'The security officer involved was appropriately disciplined. Ali

+

security of ficers were reinstructed on the correct procedure for

access centrol and signed a statement acknowledging this retraining.

During this inspection, the inspectors obssrved several security

officers process personnel into the PA at the screenhouse area and

all were processed in accordance with the licensee's security plan

and implementing procedures,

s

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8

38

9.3 (Closed) Violation Q69/85-11-02):

Two security officers had not

completed annual physical fitness _ testing.

In January 1986, respon-

__

'sibility for scheduling physical fitness testing was transferred

from the Training Department to the Security Department to provide

better line control. A review by the inspectors on the status of

training disclosed that physical fitness testing was current.

0.4 (Closed) Unresolvsd (289/85-17-01):

Positive control of photo

badges and key cards'.

T W inspector init1.41Ty reviewed the

licensee's control of ptioto badges and key cards in Irispection

Reoort 289/85-17. The item was considered unresolved pending

fu'rther review of the applicable portions of the licensee's security

plan. This review was performed as part of a later inspection

(289/85-27-63). Durit.g this subsequent review, the inspector deter-

rained the unresolved item to te a violation.

This item is being

adr>inistratively closed and will be tracked as part of the noted

violation.

As a result of thi.s review, the inspector concluded that the licensee's

actions were timely and appropriate to adequately resolve these issues,

except as n6ted in paragraph 9 4.

Appropriate enforcement action was

taken in that case.

10. E/it interviey

The ir,spectors discussed f.he inspection scope and findings with the

lir.ensee management at a final exit interview conducted on February 7,

1986.

In addition, an interin exit interview cccurred in the security

area on January 30, 1986. The following licensee personnel attended the

final exit n.eeting:

G. Baker, Hanager, Environmental Controls, THI-I

J. Colitz, Phnt Engineering Director, TMI-1

J. Enders, Lieutenant, TM1-1 Security

C. Incorvati, THI-1 Audit Supervisor, Nuclear Assurance

D. taudermilch, Protection Trair.ing Supervisor, TMI-1

R. Neisiig, TMI-1 Cor.munications

M. Nelson, TMI-1 Review Program Supervisor

1. O'Connor, i.ead Fire Protection Engineer, TMI-1/2

S. Otto, THI$1 Licensing Engineer, Technical Functions

F. Perry, Manager, Support Tralr.ing, TMI-1

L. Ritter, Administrator II, Maintenance, TMI-1

M. Ross, Plant Opef ations Director, TMI-1

9. Sinegar, Administrator II, Maintenance, TMI-1

C. Smyth, Manager of Licensing, Technical Functions

R. Toole, Operations and Maintenance Director, TMI-1

H. Wilson, Preventive Maintenance Supervisor, THI-1

- --

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39

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The inspection results, as discussed at the meeting, are summarized in

the cover page of the inspection report.

Licensee representatives

indicated that other than the security area none of the subjects dis-

cussed contained proprietary or safeguards information.

Unresol"vid Items are matters about which information is required in order

to ascertain whether they are acceptable items, violations, or devia-

tions. Unresolved item (s), discussed during the exit meeting, are

documented in paragraphs 2.2.3, 3.1.4, 3.2.4, 4.1, 4.3, 7.6.3.2, 7.7.2,

7.7.3, and 9.4.

Inspector Follow Items are matters which were established to administra-

tively follow open issues based on inspector judgement or on licensee /

staff commitments prior to the THI-1 restart.

Inspector follow item (s),

discussed during the exit meeting, are documented in paragraphs 6.8 and

9.1,

s

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%

%

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s

%

4

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ATTACHMENT I

ADDITIONAL RESIDENT INSPECTOR COVERAGE

',

The NRC inspectors assessed the adequacy and effectiveness of operating

'

personnel performance based on the inspectors' observations of operating

activities to determine that:

operators are attentive and responsive to plant parameters and condi-

--

tions;

plant evolutions and testing are planned and properly authorized;

--

procedures are used and followed as required by plant policy;

--

equipment status changes are appropriately documented and communicated to

--

appropriate shift personnel;

--

the operating conditions of plant equipment are effectively monitored and

appropriate corrective action is initiated wher required;

backup instrumentation, measurement, and readings are used as appropriate

--

when normal instrumentation is found to be defective or out of tolerance;

logkeeping is timely, accurate, and adequately reflects plant activities

--

and status;

operators follow good operating practices in conducting plant operations;

--

and,

operator actions are consistent with performance-oriented training.

--

The inspectors' observations included, but were not limited to, those reactor

plant operation, maintenance, radiological controls and surveillance test

activities listed below:

Operations

--

Control room observation of Control Room Operators (CRO), Shift Foremen

(SF), and Shif t Supervisors (SS)

Observation of turnover between SFs and auxiliary operators (A0s)

--

Observance of CR0 and SF logs

--

Performance of plant shutdown and startup for bellows replacement ob-

--

served in control room

Operational review of hot spot flush

--

Inspection of plant soaces

--

L

e

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o

Attachment

2

Maintenance

Maintenance associated with extraction steam line bellows replacement

--

Nondestructive examination of bellows

--

Reactor Protection System (RPS) Breaker shunt trip replacement

--

Radiological Controls

Locked high radiation doors

--

Radiation Work Permit posting

--

Weekly survey maps

--

Surveillance

RPS breaker testing and calibration

--

Power Operated Relief Valve surveillance data

--

>

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