| | | Reporting criterion |
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| 05000280/LER-1986-001-01, :on 860107,reactor Trip Occurred Due to Loss of Instrument Air.Caused by Hot Gas Bypass Valve in Dryer Improperly Adjusted to Maintain Air Temp Above Freezing. Operator Attempted to Gain Manual Control |
- on 860107,reactor Trip Occurred Due to Loss of Instrument Air.Caused by Hot Gas Bypass Valve in Dryer Improperly Adjusted to Maintain Air Temp Above Freezing. Operator Attempted to Gain Manual Control
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| 05000280/LER-1986-002, :on 860108,unit Tripped from 97% Power & Specific Activity Sample of Reactor Coolant Exceeded Tech Spec Dose Equivalent I-131 Limit.Caused by Iodine Spike. Level Monitored Every 4 H |
- on 860108,unit Tripped from 97% Power & Specific Activity Sample of Reactor Coolant Exceeded Tech Spec Dose Equivalent I-131 Limit.Caused by Iodine Spike. Level Monitored Every 4 H
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| 05000280/LER-1986-002-01, :on 860119,at 100% Power,Excess Leakage of RCS Noted.Caused by Failed motor-operated Valve Packing & Failed Diesel Generator Diaphragm.Valve Will Be Repacked & Diaphragm Replaced During Next Suitable Outage |
- on 860119,at 100% Power,Excess Leakage of RCS Noted.Caused by Failed motor-operated Valve Packing & Failed Diesel Generator Diaphragm.Valve Will Be Repacked & Diaphragm Replaced During Next Suitable Outage
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| 05000281/LER-1986-003-03, :on 860216,turbine Tripped Due to High Level in Steam Generator B.Caused When Main Feedwater Bypass Valve B Failed to Close on Demand.Valve Failure Caused by Blockage in Air Pilot Relay.Blockage Dislodged |
- on 860216,turbine Tripped Due to High Level in Steam Generator B.Caused When Main Feedwater Bypass Valve B Failed to Close on Demand.Valve Failure Caused by Blockage in Air Pilot Relay.Blockage Dislodged
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| 05000280/LER-1986-003, :on 860119,at 97% Power,Reactor Tripped Manually Following Drop of Four Fuel Rods Into Core & Turbine Runback.Caused by Control Rod Logic Cabinet Jump Short.Abnormal Procedure 1.4 Changed |
- on 860119,at 97% Power,Reactor Tripped Manually Following Drop of Four Fuel Rods Into Core & Turbine Runback.Caused by Control Rod Logic Cabinet Jump Short.Abnormal Procedure 1.4 Changed
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| 05000280/LER-1986-004, :on 860119,following Manual Reactor Trip, Specific Activity Sample of Primary Coolant Sys Exceeded Dose Equivalent I-131 Level of 1.0 Uci/Cc.Caused by Fuel Element Defects in Reactor Core |
- on 860119,following Manual Reactor Trip, Specific Activity Sample of Primary Coolant Sys Exceeded Dose Equivalent I-131 Level of 1.0 Uci/Cc.Caused by Fuel Element Defects in Reactor Core
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| 05000281/LER-1986-004-02, :on 860219,during Test of Component Cooling Check Valves in RHR Sys,Operator Made Incorrect Valve Lineup Resulting in Isolation Component Cooling Flow to RHR HX a & B.Event Rept Placed in Operator Reading Manual |
- on 860219,during Test of Component Cooling Check Valves in RHR Sys,Operator Made Incorrect Valve Lineup Resulting in Isolation Component Cooling Flow to RHR HX a & B.Event Rept Placed in Operator Reading Manual
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| 05000281/LER-1986-005-01, :on 860511,overpower Delta T Reactor Trip Occurred When Spurious Rod Signals from Emergency Buses Caused Turbine Runback.Caused by Malfunctioning Auto Load Tap Changer on Transformer.Changer replaced.W/860610 1tr |
- on 860511,overpower Delta T Reactor Trip Occurred When Spurious Rod Signals from Emergency Buses Caused Turbine Runback.Caused by Malfunctioning Auto Load Tap Changer on Transformer.Changer replaced.W/860610 1tr
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| 05000280/LER-1986-005, :on 860124,unit Manually Tripped from 42% Power Due to Arcing on Isolated Phase Bus Duct A.Caused by Corrosion on Contact Surfaces of Lugs of Ground Straps. Damaged Section of Duct Replaced & Welded |
- on 860124,unit Manually Tripped from 42% Power Due to Arcing on Isolated Phase Bus Duct A.Caused by Corrosion on Contact Surfaces of Lugs of Ground Straps. Damaged Section of Duct Replaced & Welded
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| 05000280/LER-1986-006, :on 860124,specific Activity Sample of Reactor Coolant Showed Dose Equivalent I-131 Level of 1.22 Mci/Cc After Manual Reactor Trip from 42% Power.Caused by Fuel Element Defects in Core.Level Monitored Every 4 H |
- on 860124,specific Activity Sample of Reactor Coolant Showed Dose Equivalent I-131 Level of 1.22 Mci/Cc After Manual Reactor Trip from 42% Power.Caused by Fuel Element Defects in Core.Level Monitored Every 4 H
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| 05000281/LER-1986-006-03, :on 860616,svc Water Leak Discovered in Expansion Joint on Svc Water Return Line from Recirculation Spray Hx.Caused by Galvonic Corrosion.Expansion Joints Replaced & Carbon Steel on Joints Coated |
- on 860616,svc Water Leak Discovered in Expansion Joint on Svc Water Return Line from Recirculation Spray Hx.Caused by Galvonic Corrosion.Expansion Joints Replaced & Carbon Steel on Joints Coated
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| 05000281/LER-1986-007-02, :on 860617,reactor Trip Occurred Due to High Level in Steam Generator A.Caused by Failure of Valve FCV-2478 to Close Due to Metal Debris Between Plug & Valve Seat.Metal Debris Removed & Valve Reassembled |
- on 860617,reactor Trip Occurred Due to High Level in Steam Generator A.Caused by Failure of Valve FCV-2478 to Close Due to Metal Debris Between Plug & Valve Seat.Metal Debris Removed & Valve Reassembled
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| 05000280/LER-1986-007, :on 860107,two Bolting Studs in Valve Flange MOV-SI-1890B Failed.Caused by Intergranular Stress Corrosion of Bolting Matl.Insp Conducted & Stud Matl Replaced,As Necessary |
- on 860107,two Bolting Studs in Valve Flange MOV-SI-1890B Failed.Caused by Intergranular Stress Corrosion of Bolting Matl.Insp Conducted & Stud Matl Replaced,As Necessary
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| 05000281/LER-1986-008-03, :on 860706,low Head Safety Injection Pump Discharge Isolation Valve MOV-2890C to Cold Legs Found Energized in Open Position.Human Performance Evaluation Will Be Performed to Determine Cause |
- on 860706,low Head Safety Injection Pump Discharge Isolation Valve MOV-2890C to Cold Legs Found Energized in Open Position.Human Performance Evaluation Will Be Performed to Determine Cause
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| 05000281/LER-1986-008, :on 860706,low Head Safety Injection Pump Discharge Isolation Valve to Cold Leg Found Energized in Open Position.Cause Undetermined.Procedural Changes Will Be Implemented |
- on 860706,low Head Safety Injection Pump Discharge Isolation Valve to Cold Leg Found Energized in Open Position.Cause Undetermined.Procedural Changes Will Be Implemented
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| 05000280/LER-1986-008, :on 860213,unexpected Start of Auxiliary Feed Pump 2-FW-P-3B Occurred.Caused by Open Coil in Bfd Relay AFP-3XB.Relay Replaced & Tested Satisfactorily |
- on 860213,unexpected Start of Auxiliary Feed Pump 2-FW-P-3B Occurred.Caused by Open Coil in Bfd Relay AFP-3XB.Relay Replaced & Tested Satisfactorily
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| 05000280/LER-1986-009, :on 860208,during Startup,Operating Main Feedwater Pump Tripped Due to High Level in Steam Generator C.Caused by Dust Accumulation in Pilot Relay Blocking Air to Valve Operator.Blockage Removed |
- on 860208,during Startup,Operating Main Feedwater Pump Tripped Due to High Level in Steam Generator C.Caused by Dust Accumulation in Pilot Relay Blocking Air to Valve Operator.Blockage Removed
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| 05000281/LER-1986-009-03, :on 860709,reactor Trip Breaker Opened Following Spurious RCS Low Flow Signal.Caused by Personnel Error During Replacement of Failed Reactor Protection Sys Train B Relay.Individual Counseled |
- on 860709,reactor Trip Breaker Opened Following Spurious RCS Low Flow Signal.Caused by Personnel Error During Replacement of Failed Reactor Protection Sys Train B Relay.Individual Counseled
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| 05000281/LER-1986-010-02, :on 860711,pump B Discharge Pressure Dropped to Zero,Causing Inoperability of Both Charging Pumps a & B. Caused by Air Introduced in Sys During Maint on Pump A.Pump Vented.Both Pumps Returned to Svc |
- on 860711,pump B Discharge Pressure Dropped to Zero,Causing Inoperability of Both Charging Pumps a & B. Caused by Air Introduced in Sys During Maint on Pump A.Pump Vented.Both Pumps Returned to Svc
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| 05000280/LER-1986-010, :on 860207,reactor & Turbine Tripped on High Steam Generator Level.Caused by Failure to Adjust Feedback Cam Following Maint.Cam Adjusted & Maint Procedure Revised |
- on 860207,reactor & Turbine Tripped on High Steam Generator Level.Caused by Failure to Adjust Feedback Cam Following Maint.Cam Adjusted & Maint Procedure Revised
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| 05000281/LER-1986-011-02, :on 860720,determined That Svc Water Leaking Into Containment from Recirculation Spray HX (Rshx).Caused by Leaking Tubes in RSHX B.Tubes Plugged.Rshx Successfully Pressure Tested |
- on 860720,determined That Svc Water Leaking Into Containment from Recirculation Spray HX (Rshx).Caused by Leaking Tubes in RSHX B.Tubes Plugged.Rshx Successfully Pressure Tested
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| 05000281/LER-1986-012-03, :on 860821,during Monthly Performance Test, Relay LM-REL-200A1 Found Failed & on 860826 Relay R-LM-REL-200A2 Found Failed.Caused by Intermittent Operation of Comparator.Relays Replaced & Tested |
- on 860821,during Monthly Performance Test, Relay LM-REL-200A1 Found Failed & on 860826 Relay R-LM-REL-200A2 Found Failed.Caused by Intermittent Operation of Comparator.Relays Replaced & Tested
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| 05000280/LER-1986-012, :on 860409,flow Path from Boric Acid Tank to Charging Pump Suction Inadvertently Isolated.Caused by Personnel Error in Isolating Boric Acid Filter.Flow Path Reestablished by Unisolating Filter |
- on 860409,flow Path from Boric Acid Tank to Charging Pump Suction Inadvertently Isolated.Caused by Personnel Error in Isolating Boric Acid Filter.Flow Path Reestablished by Unisolating Filter
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| 05000281/LER-1986-012-02, :on 860821,during Monthly Performance Test, Relay LM-REL-200A1 Found Failed & on 860826,relay LM-REL-200A2 Found Failed.Caused by Intermittent Operation of Comparator.Relays Replaced & Tested |
- on 860821,during Monthly Performance Test, Relay LM-REL-200A1 Found Failed & on 860826,relay LM-REL-200A2 Found Failed.Caused by Intermittent Operation of Comparator.Relays Replaced & Tested
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| 05000280/LER-1986-013, :on 860510,following Shutdown for Refueling Outage,Specific Activity Sample of Reactor Coolant Showed Dose Equivalent of I-131 1.05 Mci/Cc.Caused by Fuel Element Defects in Reactor Core.Level Monitored |
- on 860510,following Shutdown for Refueling Outage,Specific Activity Sample of Reactor Coolant Showed Dose Equivalent of I-131 1.05 Mci/Cc.Caused by Fuel Element Defects in Reactor Core.Level Monitored
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| 05000281/LER-1986-013-02, :on 861005,auxiliary Feedwater Pumps Started & Steam Generator Blowdown Trip Valves Closed.Caused by Cycling of Auxiliary Lube Oil Pump for Main Feed Pump (MFP) & Trip of MFP Breaker.Procedures Changed |
- on 861005,auxiliary Feedwater Pumps Started & Steam Generator Blowdown Trip Valves Closed.Caused by Cycling of Auxiliary Lube Oil Pump for Main Feed Pump (MFP) & Trip of MFP Breaker.Procedures Changed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000280/LER-1986-014, :on 860511,temporary Degradation of Dc Bus Voltage B Experienced,Resulting in ESF Actuation.Caused by Inadequate Procedure in Design Change to Replace Batteries. Procedure Will Be Revised |
- on 860511,temporary Degradation of Dc Bus Voltage B Experienced,Resulting in ESF Actuation.Caused by Inadequate Procedure in Design Change to Replace Batteries. Procedure Will Be Revised
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| 05000281/LER-1986-014-02, :on 861010,results of Type C Containment Leakage Testing Indicated That Inside & Outside Containment Sump Trip Valves Had Leakage Greater than 300 Scfh.Caused by Erosion of Plug & Seat.Valves Will Be Replaced |
- on 861010,results of Type C Containment Leakage Testing Indicated That Inside & Outside Containment Sump Trip Valves Had Leakage Greater than 300 Scfh.Caused by Erosion of Plug & Seat.Valves Will Be Replaced
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| 05000281/LER-1986-015-01, :on 861031,pressurizer Safety Valve Setpoints Found Outside Allowable Limits.Caused by Failure to Compensate for Operating Temp & Valve Wear.Valves Replaced & Setpoints Reset |
- on 861031,pressurizer Safety Valve Setpoints Found Outside Allowable Limits.Caused by Failure to Compensate for Operating Temp & Valve Wear.Valves Replaced & Setpoints Reset
| 10 CFR 50.73(a)(2)(1) |
| 05000281/LER-1986-015-02, :on 861031,pressurizer Safety Valves Had Lift Setpoints Outside Allowable Limits During Refueling Surveillance Testing.Safety Valve Setpoints Reset.Vendor Failure Analysis Underway |
- on 861031,pressurizer Safety Valves Had Lift Setpoints Outside Allowable Limits During Refueling Surveillance Testing.Safety Valve Setpoints Reset.Vendor Failure Analysis Underway
| 10 CFR 50.73(a)(2)(1) |
| 05000280/LER-1986-016, :on 860510,lift Settings for Five Safety Valves on Main Steam Line B Found 3% Greater than Lift Setpoints. Caused by Setpoints Set Too High During 841223 Calibr Due to Unreliable Indication |
- on 860510,lift Settings for Five Safety Valves on Main Steam Line B Found 3% Greater than Lift Setpoints. Caused by Setpoints Set Too High During 841223 Calibr Due to Unreliable Indication
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| 05000281/LER-1986-016-01, :on 861116,containment Radiation Monitor Trip Valves TV-RM-200A,B & C Closed on Safeguards Signal.Caused by Inadequate Procedure.Procedure Will Be Modified |
- on 861116,containment Radiation Monitor Trip Valves TV-RM-200A,B & C Closed on Safeguards Signal.Caused by Inadequate Procedure.Procedure Will Be Modified
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000281/LER-1986-017-02, :on 861121,during Periodic Test 8.5A, Inadvertent Auto Start of Emergency Diesel Generator 3 (EIIS-ER) Occurred.Caused by Personnel Error.Testing Suspended & Diesel Shut Down |
- on 861121,during Periodic Test 8.5A, Inadvertent Auto Start of Emergency Diesel Generator 3 (EIIS-ER) Occurred.Caused by Personnel Error.Testing Suspended & Diesel Shut Down
| 10 CFR 50.73(a)(2) |
| 05000280/LER-1986-017, :on 860524,loss of Operating RHR & Component Cooling Pumps 1B Occurred Due to Undervoltage Transient. Caused by Personnel Error.Forced Coolant Circulation Reestablished |
- on 860524,loss of Operating RHR & Component Cooling Pumps 1B Occurred Due to Undervoltage Transient. Caused by Personnel Error.Forced Coolant Circulation Reestablished
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| 05000281/LER-1986-018-02, :on 861112,environmentally Qualified Components Found Not Installed Per Approved Raychem Guidelines.Caused by Procedures Not Conforming to Raychem Application Guide. Procedures Revised |
- on 861112,environmentally Qualified Components Found Not Installed Per Approved Raychem Guidelines.Caused by Procedures Not Conforming to Raychem Application Guide. Procedures Revised
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| 05000281/LER-1986-018, :on 861112,discovered Environ Qualified Components Not Installed Per Approved Raychem Guidelines. Caused by Inadequate Training of Personnel Installing Matl. Procedures Revised & Addl Training Conducted |
- on 861112,discovered Environ Qualified Components Not Installed Per Approved Raychem Guidelines. Caused by Inadequate Training of Personnel Installing Matl. Procedures Revised & Addl Training Conducted
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| 05000280/LER-1986-018, :on 860528,emergency Diesel Generator 3 Automatically Started.Caused by Inadequate Design Change Procedure Causing Interruption of Dc Power.Procedure Revised |
- on 860528,emergency Diesel Generator 3 Automatically Started.Caused by Inadequate Design Change Procedure Causing Interruption of Dc Power.Procedure Revised
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| 05000281/LER-1986-019-01, :on 861201,individual Rod Position Indicators (Irpi) for Control Rods Out of Calibr.Caused by Instrument Drift.All Inoperable Irpis Recalibr & Returned to Svc |
- on 861201,individual Rod Position Indicators (Irpi) for Control Rods Out of Calibr.Caused by Instrument Drift.All Inoperable Irpis Recalibr & Returned to Svc
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| 05000280/LER-1986-019, :on 860711,automatic Opening of Reactor Trip Breakers Occurred.Caused by Spurious Turbine First Stage Pressure Spike That Unblocked Permissive P.7 |
- on 860711,automatic Opening of Reactor Trip Breakers Occurred.Caused by Spurious Turbine First Stage Pressure Spike That Unblocked Permissive P.7
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| 05000280/LER-1986-020, :on 860609,during Environ Qualification Insp, Limitorque Motor Valve Operator Wiring Found Questionable. Unidentifiable Wiring Introduced Through Plant Field Changes.Wiring Replaced |
- on 860609,during Environ Qualification Insp, Limitorque Motor Valve Operator Wiring Found Questionable. Unidentifiable Wiring Introduced Through Plant Field Changes.Wiring Replaced
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| 05000281/LER-1986-020, :on 861209,reactor Tripped Due to Low Water Level in Steam Generator C (EIIS-SG).Caused by Improper Reassembly of Valve Following Maint.Unit Inspected & Tested Prior to Startup |
- on 861209,reactor Tripped Due to Low Water Level in Steam Generator C (EIIS-SG).Caused by Improper Reassembly of Valve Following Maint.Unit Inspected & Tested Prior to Startup
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| 05000281/LER-1986-020-01, Forwards LER 86-020-01 & Reactor Trip & Feedwater Pipe Failure Rept | Forwards LER 86-020-01 & Reactor Trip & Feedwater Pipe Failure Rept | |
| 05000281/LER-1986-020-02, Forwards LER 86-020-02 & Surry Unit 2 Reactor Trip & Feedwater Pipe Failure Rept | Forwards LER 86-020-02 & Surry Unit 2 Reactor Trip & Feedwater Pipe Failure Rept | |
| 05000280/LER-1986-021, :on 860713,individual Rod Position Indicators (Irpi) Declared Inoperable,Per Tech Spec 3.12.E.Caused by Instrumentation Drift Affected by Primary Coolant Temp & Control Rod Movement.Irpis Recalibr |
- on 860713,individual Rod Position Indicators (Irpi) Declared Inoperable,Per Tech Spec 3.12.E.Caused by Instrumentation Drift Affected by Primary Coolant Temp & Control Rod Movement.Irpis Recalibr
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| 05000280/LER-1986-022, :on 860916 & 20,partial Train B ESF Actuations Occurred Due to Reactor Protection Sys Relay Failures.Caused by Coil Failure.Coil Replaced & Relay Reinstalled & Tested |
- on 860916 & 20,partial Train B ESF Actuations Occurred Due to Reactor Protection Sys Relay Failures.Caused by Coil Failure.Coil Replaced & Relay Reinstalled & Tested
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| 05000280/LER-1986-023-01, :on 860820,containment Sump Trip Valve Found Leaking from Inside Containment Isolation Valve.Caused by Loose Valve Position Indication Arm.Valve Manually Isolated & Screw Set Tightened in Indication Arm |
- on 860820,containment Sump Trip Valve Found Leaking from Inside Containment Isolation Valve.Caused by Loose Valve Position Indication Arm.Valve Manually Isolated & Screw Set Tightened in Indication Arm
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| 05000280/LER-1986-024, :on 860813 & 14,at 100% Power,Control Room Chillers Failed to Operate.Caused by Clogged Chillers Due to Unfiltered River Water Flowing Through Tubes.Chillers Unclogged & Strainer Returned to Svc |
- on 860813 & 14,at 100% Power,Control Room Chillers Failed to Operate.Caused by Clogged Chillers Due to Unfiltered River Water Flowing Through Tubes.Chillers Unclogged & Strainer Returned to Svc
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| 05000280/LER-1986-025, :on 860918 & 19,control Rods P-6 & P-10 Dropped Into Core,Respectively & Reactor Manually Tripped.Caused by Failed Stationary Gripper Coil & Loose Female Connector Pin. Parts Replaced & Control Rods Tested |
- on 860918 & 19,control Rods P-6 & P-10 Dropped Into Core,Respectively & Reactor Manually Tripped.Caused by Failed Stationary Gripper Coil & Loose Female Connector Pin. Parts Replaced & Control Rods Tested
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| 05000280/LER-1986-026, :on 860919,quadrant-to-average-power-tilt Ratio Exceeded 2% Tech Spec Limit.Caused by Dropped Control Rod P-6 Due to Failed Stationary Gripper Coil in CRD Mechanism. Coil Replaced |
- on 860919,quadrant-to-average-power-tilt Ratio Exceeded 2% Tech Spec Limit.Caused by Dropped Control Rod P-6 Due to Failed Stationary Gripper Coil in CRD Mechanism. Coil Replaced
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| 05000280/LER-1986-027, :on 861009,two of Three Control Room Air Conditioning Chillers Found Inoperable.Caused by One Chiller Out for Maint & Other Inoperable Due to Failed Relay.Failed Relay Jumpered & Replaced |
- on 861009,two of Three Control Room Air Conditioning Chillers Found Inoperable.Caused by One Chiller Out for Maint & Other Inoperable Due to Failed Relay.Failed Relay Jumpered & Replaced
| 10 CFR 50.73(a)(2)(i) |