ML20140C553

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Insp Rept 50-416/85-45 on 851116-1220.Violation Noted: Failure to Close Local Leak Rate Test Valves by Normal Means,Failure to Train Personnel Performing QA Activities & Failure to Follow Diesel Generator Maint Procedures
ML20140C553
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 01/10/1986
From: Butcher R, Caldwell J, Panciera V
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20140C540 List:
References
50-416-85-45, NUDOCS 8601280339
Download: ML20140C553 (14)


See also: IR 05000416/1985045

Text

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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ATLANT A, GEORGt A 30323

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Report No.:

50-416/85-45

Licensee:

Mississippi Power And Light Company

Jackson, MS 39205

,

Docket No.:

50-416

License No.:

NPF-29

Facility Name:

Grand Gulf 1

Inspection Conducted : November 16 thru December 20,1985

Inspectors: [

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H.~C. sur.cner, Sen;#F

idenEinspector

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Approvedby:\\>{},1. n , aMJf,&

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W W. PanWeFa', Chief, Project Section 28

Aat4 Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine inspection entailed 202 resident inspector-hours at the

site in the areas of Operational Safety Verification, Maintenance Observation,

Surveillance Observation, ESF System Walkdown, Reportable Occurrences, Operating

Reactor Events, Inspector Followup and Unresolved Items, and License Conditions.

Results:

Violations - failure to close LLRT valves by normal means, failure

to adequately train personnel performing activities affecting quality, and

failure to follow procedures when performing diesel generator maintenance.

Deviation - failure to incorporate periodic test of ESF room coolers.

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ADOCK 05000416

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REPORT DETAILS

a

1.

Licensee Employees Contacted

J. E. Cross, Site Director

  • C. R. Hutchinson, General Manager

R. F. Rogers, Technical Assistant

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  • J. D. Bailey, Compliance Coordinator

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M. J. Wright, Manager, Plant Operations

L. F. Daughtery, Compliance Superintendent

D. Cupstid, Start-up Supervisor

R. H. McAnulty, Electrical Superintendent

  • R. V. Moomaw, Manager, Plant Maintenance
  • B. Harris, Compliance Coordinator

J. L. Robertson, Operations Superintendent

L. Temple, I & C Superintendent

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Other licensee employees contacted included technicians, operators, security

force members, and office personnel.

  • Attended exit interview.

2.

Exit Interview

The inspection scope and findings were summarized on December 20, 1985, with

those persons indicated in paragraph 1 above.

The licensee did not identify

as proprietary any of the materials provided to or reviewed by the

inspectors during this inspection.

The licensee had no comment on the

following inspection findings:

a.

Unresolved Item 85-45-01; Significance of Plugging of ESF Room Coolers.

(Paragraph 5.a)

b.

Deviation 85-45-02; Failure to Incorporate Periodic Test of ESF Room

,

Coolers to Ensure System Operation.

(Paragraph 5.a)

c.

Unresolved Item 85-45-03; Unusable Fuel Oil Tank Volume.

(Paragraph

5.b)

d.

Unresolved Item 85-45-04; I;SIV Accumulator Check Valves Not Addressed

in the IST Program.

(Paragraph 5.c)

e.

Inspector Followup Item (IFI) 85-45-05; Permissible Leakage Rate for

LLRTs.

(Paragraph 7)

f.

Violation 85-45-06; Failure to Close LLRT Valves by Normal Means.

(Paragraph 7)

g.

Violation 85-45-07; Failure to Adequately Train Personnel Performing

Activities Affecting Quality.

(Paragraph 9.a)

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h.

IFI 85-45-08; TDI Diesel Generator Intake & Exhaust Valve Spring

Inspection.

(Paragraph 9.c)

i.

IFI 85-45-09; TDI Diesel Generator Air Intake Silencer Defect

Inspection.

(Paragraph 9.d)

j.

Unresolved Item 85-45-10; Licensee Identified Discrepancies in

Environmental Qualification Program.

(Paragraph 9.e)

k.

Violation 85-45-11; Failure to Follow Procedures when Performing Diesel

Generator Maintenance.

(Paragraph 10)

1.

IFI 85-45-12; Excessive Oil Around Diesel Generators and Existence of

Two Valves with Same Identification Number.

(Paragraph 8)

3.

Licensee Action on Previous Enforcement Matters (92702)

Not Inspected.

4.

Unresolved Items

An Unresolved Item is a matter about which more information is required to

determine whether it is acceptable or may involve a violation or deviation.

New Unresolved Items are discussed in Paragraph 5.a, 5.b, 5.c, and 9.f.

5.

Operational Safety Verification (71707)

The inspectors kept themselves informed on a daily basis of the overall

plant status and any significant safety matters related to plant operations.

Daily discussions were held with plant management and various members of the

plant operating staff.

The inspectors made frequent visits to the control

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room such that it was visited at least daily when an inspector was on site.

Observations included instrument readings, setpoints and recordings status

of operating systems; tags and clearances on equipment controls and

switches; annunciator alarms; adherence to limiting conditions for opera-

tion; temporary alterations in effect; daily journals and data sheet

entries; control room manning; and access controls.

This inspection

activity included numerous informal discussions with operators and their

supervisors.

Weekly, when onsite, a selected ESF system is confirmed operable.

The

confirmation is made by verifying the following:

accessible valve flow path

alignment; power supply breaker and fuse status; major component leakage,

lubrication, cooling and general condition; and instrumentation.

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General plant tours were conducted on at least a biweekly basis.

Portions

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of the control building, turbine building, auxiliary building and outside

areas were visited.

Observations included safety related tagout verifica-

tions; shift turnover; sampling program; housekeeping and general plant

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conditions; fire protection equipment; control of activities in progress;

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radiation protection controls; physical security; problem identification

systems; and containment isolation.

The following comments were noted:

a.

It came to the inspectors attention that during the performance of flow

balancing testing of the new Standby Service Water (SSW) B pump the

licensee discovered several Engineered Safety Feature (ESF) room

coolers plugged with sand.

The inspectors questioned the licensee

about the safety significance and reportability of plugged ESF room

coolers.

The licensee responded that they would have the Nuclear Plant

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Engineering (NPE) Department evaluate the flow through the coolers to

determine if flow was sufficient to ensure operation of the associated

ESF equipment during an accident and verify that the plant was not in

an unanalyzed condition.

Pending NPE's evaluation the question of

safety significance and reportability will be identified as an

Unresolved Item.

(50-416/85-45-01).

Further review by the inspectors revealed a commitment in the FSAR,

paragraph 9.4.5.4, that the ESF room coolers be periodically inspected

,

to ensure that all normally operating equipment is functioning properly

'

and standby components are periodically tested to ensure system

operation.

From a discussion with the licensee, the inspectors

discovered that no program existed to inspect and test the ESF room

coolers as required by the FSAR.

In fact, the only reason the B train

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of ESF room coolers were discovered to be plugged with sand was due to

the testing of a new SSW pump.

The licensee has replaced the plugged

coolers and is in the process of testing the A train of the ESF room

coolers.

The failure of the licensee to have a program to inspect and

test the ESF room coolers as committed to in the FSAR will be identified

as a Deviation (50-416/85-45-02).

b.

During a review of one of the plant's Incident Reports (irs), the

inspectors discovered that the minimum level for the Emergency Diesel

Generator (EDG) storage tank appeared to be in error in the

non-conservative direction.

Consequently, the possibility existed that

the plant could have operated with the EDG fuel tank levels below the

limits allowed in Technical Specifications (TS).

This discovery by the

licensee resulted from a review of a TS change that was being imple-

mented ir.to a surveillance procedure to raise the minimum fuel storage

tank level to compensate for new larger Standby Service Water (SSW)

pump motors being placed on the EDGs' busses.

This review revealed a

Bechtel drawing (JK-M-2003) of the fuel oil tanks showing an unusable

fuel oil volume to be approximately 8,200 gallons.

This 8,200 gallons

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was used to compute the new minimum fuel oil tank levels corresponding

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to 57,200 gallons needed to support the new SSW pump motors.

However

the figure of 8,200 gallons was not used to determine the level which

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corresponded to the previous TS limit of 48,000 gallons.

An unusable

volume of 3,400 gallons was used to determine the minimum level for the

TS limit.

The licensee has stated that conversations with the diesel

fuel transfer pump vendor, some informal calculations and statements in

the FSAR indicate that the value used for the unusable volume. (3,400

gallons) to determine the minimum EDG fuel oil tank level corresponding

to the 48,000 gallon TS requirement is appropriate for this applica-

tion.

The only documentation other than the FSAR which the licensee

can provide is the Bechtel drawing of the tank supplied to MP&L showing

the unusable volume to be 8,200 gallons.

The inspectors asked the licensee if the tank levels had ever dropped

to a level below 48,000 gallons when using 8,200 gallons as unusable

volume.

The assistant to the Operations Superintendent informed the

inspectors that a review of the EDG operations log revealed that the

only times the fuel oil levels were below 48,000 gallons, using 8,200

gallons as an unusable volume, were when the corresponding EDG was

declared inoperable for other reasons.

The licensee has been requested

to provide written documentation from the fuel pump vendor and MP&L's

Engineering organization to support their contention that 3,400 gallons

unusable volume is appropriate for this application.

Since the

possibility existed that the previous surveillance procedures would

have allowed the EDGs to be operated with fuel oil tank level below the

limit of ' Technical Specifications, this will be identified as an

Unresolved Item (50-416/85-45-03) pending the written documentation

supporting the licensee's previous values.

'

c.

A situation similar to that described in IE Information Notice 85-84,

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Inadequate Inservice Testing of Main Steam Isolation Valves, existed at

GGNS.

The instrument air system is a non-safety-related system which

normally supplies operating air for the Main Steam Isolation Valves

(MSIVs).

There are safety related accumulators which provide stored

air for MSIV operation in the event the instrument air system is lost

(i.e. isolated, etc).

Each MSIV has an accumulator with an in-line

check valve from the instrument air system.

The check valves B21F024A,

F0248, F024C,

F024D, F029A, F029B, F029C, and F029D, do not appear to

have been included in the licensee's Inservice Testing (IST) program,

nor in the licensee's type C testing per Appendix J of 10 CFR 50.

The

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instrument air lines just upstream of the noted check valves are

non-seismic piping.

T.S. table 3.6.4-1 requires a maximum isolation

time of 5 seconds for the MSIVs.

The licensee conducted testing with

the instrument air line isolated, the accumulators charged with instru-

2

ment air and no steam flow. The MSIV closure times were within the 5

second requirement.

The licensee is

investigating to determine the

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reason the accumulator check valves were not included in the IST

program or IST program relief request.

This will be an Unresolved Item (50-416/85-45-04).

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6.

Maintenance Observation (62703)

During the raport period, the inspector observed selected maintenance

activities:

The observations included a review of the work documents for

adequacy, adherence to procedure, proper tagouts, adherence to Technical

Specifications, radiological controls, observation of all or part of the

actual work and/or retesting in progress, specified retest requirements, and

adherence to the appropriate quality controls.

In the areas inspected, no violations or deviations were identified.

7.

Surveillance Testing Observation (61726)

The inspector observed the performance of selected surveillances.

The

2

observation included a review of the procedure for technical adequacy,

conformance to Technical Specifications, verificat. ion of test instrument

calibration, observation of all or part of the actual surveillances, removal

from service and return to service of the system or components affected, and

review of the data for acceptability based upon the acceptance criteria.

Technical Specifications (TS) 3.6.1.2 states that containment leakage rates

shall be limited to an overall integrated leakage rate of less than or equal

to L where L equals 0.437 percent by weight of the containment air per 24

hourd at P , 71.5 psig.

The Final Safety Analysis Report (FSAR), paragraph

15.6.5.5, ftates that the design basis leak rate of the primary containment

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and its penetrations (excluding the main steam lines) is 0.35 percent per

day.

The Main Steam Line Isolation Valves (MSLIVs) are assumed to leak at

25 SCFH per valve.

The proposed TS for containment leak rate was discussed

in a letter dated December 31, 1981 from Mr. L. Dale, MP&L to Mr. H. Denton,

NRC (AECM-81/510).

Attachment 1 to the letter presented a summary of the

method used to calculate an overall integrated leak rate.

A review of

calculations by a Region II inspector indicated that the TS allowable of

0.60 La for all penetrations and all valves subject to type B and C tests

would equal approximately 325.25 SCFH.

The Licensee's Surveillance

Procedure, 06-ME-1M61-V-0001, Rev 26, Local Leak Rate Test, paragraph 5.11.2

states the overall allowable leakage limit of all type B & type C tests

shall not exceed 0.60 La or 182.5 SCFH.

A review of the licensee's letter

of December 31, 1981 indicates an error in attachment 1, step 1, in that the

204.20 is titled "SCFH" while in fact the 204.20 is "CFH" at accident

pressure, not standard pressure.

Since the licensee's error appears to be

in the conservative direction, the licensee was notified of the error and is

presently reviewing the FSAR to determine the basis for allowable leakages.

The licensee was informed that any change to the 0.437 % per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

presently specified would require a TS amendment.

This will be an

Inspector Followup Item (50-416/85-45-05).

During the performance of the Integrated Leak Rate Test (ILRT) in early

November 1985, the licensee discovered that valve C41F150, the outboard

isolation for penetration 61, was not fully closed.

In order to complete

the ILRT the licensee closed the vent valve down stream of C41F150.

Subsequent to the ILRT the licensee performed a Local Leak Rate Test (LLRT)

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on the two isolation valves associated with penetration 61, C41F150, the

outboard isolation valve and C41F151, the inboard isolation valve.

The

resulting leakage for each valve was so excessive that test pressure could

not be reached.

The inboard isolation valve C41F151 is a stop check valve

and the required position of the handwheel for the ILRT is to be in the open

direction. With the handwheel in the open direction.C41F151 acts as a check

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valve preventing flow in the outboard direction.

The previous LLRT of

C41F151, performed on June 18,1985, indicated zero leakage.

The only

operation connected with this valve since the LLRT was the reclosure of the

handwheel after the June LLRT and the opening of the handwheel in prepara-

tion for the ILRT.

This movement of the handwheel should not have any

affect on the position of the disk.

The licensee has disassembled valve

C41F151 and lapped the disk and seat.

During the disassembly it was

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observed that the packing was loose and the seat was dirty.

The subsequent

LLRT performed in November was satisfactorily.

Af ter the unsuccessful LLRT of C41F150, following the ILRT, the licensee

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attempted to shut the valve.

The operator was able to get approximately one

(1) more turn by hand but the valve still would not pass the LLRT.

Finally

the licensee placed a valve wrench on the valve and was able to get another

one quarter (1/4) of a turn in the closed directi.on.

This time the LLRT was

performed satisfactorily but the zero leakage rate achieved in June 1985 was

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not reproduced.

Since the successful LLRT on June 18, 1985, C41F150 had

only been repositioned one time and that was to perform the LLRT on C41F151

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also performed on June 18,1985.

C41F150 had been closed or verified closed

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on at least six (6) different occasions, including the valve lineup in

preparation for the ILRT, since the repositioning in June 1985.

The

inspectors questioned the licensee personnel, who perform an LLRTs, on the

requirement in Appendix J of 10 CFR 50, that a valve shall be closed by

normal operation prior to the performance of the LLRT.

The licensee

informed the inspectors that they considered the use of excessive force and

valve wrenches to close manual isolation valves for the purpose of passing

the LLRT to be normal operation.

The inspectors informed the licensee that

the use of excessive force and valve wrenches did not constitute normal

operation as required by Appendix J of 10 CFR 50, and requested a list of

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any other valves requiring abnormal operation to pass their respective

LLRTs.

The Mechanical Maintenance Superintendent notified the inspectors

that there were no other valves requiring excessive force or valve wrenches

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to pass their LLRTs.

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It is important to note that the piping associated with penetration 61 does

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nnt connect to any system in the plant.

The piping is capped at both ends,

inside and outside the containment.

Consequently operation of the isolation

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valves is not required except for the performance of their LLRTs.

The

licensee however does not know if excessive measures were taken to get

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C41F150 and C41F151 to pass their respective LLRTs with zero leakage in June

of 1985.

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Subsequent to conversations with the inspectors the licensee performed

maintenance on C41F150 and reperformed the LLRT successfully.

The failure

of the licensee to meet the requirement of 10 CFR 50, appendix J to shut

valve C41F150 using normal operation in order to achieve a successful LLRT

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following the ILRT will be identified as a Violation (50-416/85-45-06).

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8.

ESF System Walkdown (71710)

A complete walkdown was conducted on the accessible por tions of the Division

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1 Emergency Diesel Generator.

The walkdown consisted of an inspection and

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verification, where possible, of the required system valve alignment,

including valve power available and valve locking, where required; instru-

mentation valved in and functioning; electrical and instrumentation cabinets

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free from debris, loose materials, jumpers and evidence of rodents; and

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system free from other degrading conditions.

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During the walkdown of the Division 1 Emergency Diesel Generator (EDG), the

inspectors observed several items of concern. One item deals with a condi-

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tion where several areas on and around the the EDG contained pools of lube

oil which appear to be more than just normal amounts. Another item deals

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with the discovery of two valves on the valve lineup sheet and existing in

the plant with the same identification number. The valve lineup sheet

Attachment 1A of System Operating Instruction (S0I) 04-1-01-P75-1 contains

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two valves with the same identification number of F112A. Even though these

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valves appear on the same lineup sheet there was no mention by the operators

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of this problem in the comments section of the completed lineup sheet.

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quick look at Division 2 EDG valves revealed that the same condition exists

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there also. The inspectors have notified the licensee of their concerns and

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will be following up these items to ensure proper resolution. This will be

identified as Inspector Followup Item (50-416/85-45-12).

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In the areas inspected, no violations or deviations were identified.

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9.

Reportable Occurrences (90712 & 92700)

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The below listed Event Reports were reviewed to determine if the information

provided met NRC reporting requirements.

The determination included

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adequacy of event description and corrective action taken or planned,

exirtence of potential generic problems and the relative safety significance

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of each event. Additional inplant reviews and discussions with plant

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personnel as appropriate were conducted for the reports indicated by an

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asterisk. The Event Reports were reviewed using the guidance of the general

policy and procedure for NRC enforcement actions.

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The following License Event Report (LERs) are closed.

LER No.

Event Date

Event

  • 85-039

October 10, 1985

Personnel Error

Causing Loss Of

Power To ESF Bus 12.

  • 85-042

November 2, 1985

Incorrect Wiring

Configuration

Caused the Loss of

ESF Transformer 11.

a.

LER 85-039. On October 17, 1985 while moving a relay from a tagged out

feeder breaker to the Engineered Safety Feature (ESF) Division 2

electrical bus for the purpose of calibration, a personnel error caused

the other feeder breaker to trip deenergizing the entire bus.

At the

time of the event the plant was in mode 4 with the safety and shutdown

cooling systems associated with the Division 2 ESF bus declared

inoperable for various reasons.

However as a direct result of the

event the operable mode of

shutdown cooling, Residual Heat Removal

(RHR) system A, was isolated from the vessel. Shut down cooling was

restored and since the reactor had been in cold shutdown since October

13, 1985 the impact on the reactor was minimal.

The personnel error

consisted of an electrician removing a relay from ESF Division 2 feeder

breaker 152-1601 and placing the relay connection plug back in the

empty relay case.

This plug caused the bus lockout relay to sense a

trip signal tripping the other feeder breaker 152-1601 causing a total

loss of power to the Division 11 ESF electrical bus.

The electrician

did understand that the connection plug should not be placed back into

the empty relay case but he did not understand that the protective

relay circuits remained energized even though the breaker was tagged

out.

He, therefore, was not knowledgeable in the protection circuits

relationship between the feeder breakers.

10 CFR 50, Appendix B, Criterion II states in part that the Quality

Assurance Program shall take into account the need for special

controls, processes, test equipment, tools and skills to attain the

required quality, and the program shall provide for indoctrination and

training of personnel performing activities affecting quality as

necessary to assure that suitable proficiency is achieved and main-

tained.

The failure of the licensee to ensure that the electrician was

trained in the protection characteristics and ir.terfaces of feeder

breakers resulting in the loss of power to an ESF electrical bus and

subsequent loss of the shutdown cooling operation of the RHR A system

will be identified as a Violation (50-416/85-45-07).

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b.

LER 85-042.

The event associated with this LER consisted of ESF

transformer 11 output breakers tripping due to a differential protec-

tion relay signal on two different occasions, resulting in loss of

power to

ESF electrical buses.

These two events appear to have

resulted from wiring errors made some years back.

The licensee stated

!

that back in 1979 Bechtel personnel discovered that the differential

relays for each of the ESF transformers were wired backwards.

This

wiring error was corrected on the transformers but the General Electric

(GE) drawing showing this wiring error was not corrected.

Also unknown

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to the licensee another wiring error existed on a secondary side

current transformer to ESF transformer 11.

The licensee speculates

that this wiring error caused ESF transformer 11 to trip on a

protection

relay signal sometime during the startup or preoperational

testing of Division 3 High Pressure Core Spray (HPCS) Pumps.

Since the,

General Electric drawing had not been corrected and the differential

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relay would be suspected, the engineers probably discovered that the

differential relay was wired differently than the General Electric

drawing had specified and, therefore, changed the relay to be consist-

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ent with the drawing.

The relay and current transformer, each being

wired backwards, cancelled each other therefore the starting of the

HPCS pump on ESF transformer 11 would not have tripped the transformer

indicating the problem had been solved.

On November 2, 1985, the first trip of ESF transformer 11 occurred

resulting in a loss of power to the Division 2 ESF electrical bus. This

started Diesel Generator 12, and caused several isolations and secured

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RHR B shutdown cooling.

This trip uncovered the problem of the

differential relay being wired backwards and the fact that the General

Electric drawing had not been corrected.

However, it did not disclose

the reason why the relay had been changed back to the incorrect GE

drawing configuration.

The reason this wiring error had gone unde-

tected until November 2,

1985, was the current needed for normal

operation of equipment connected to ESF transforn.er 11 was just under

the trip threshold of the differential relay.

However, the licensee

had just replaced the B Standby Service Water (SSW) Pump motor with a

larger one and this was the first time this equipment had been started

and operated off of ESF transformer 11.

This new larger SSW pump motor

caused the current load requirement to just exceed the trip threshold

of the differential relay and tripped the transformer.

The second trip of ESF transformer 11 occurred on November 23, 1985,

when both Division 1 and Division 3 ESF electrical buses were being

supplied off of ESF transformer 11. The trip was caused by starting the

HPCS pump for testing and resulted in the loss of power to both ESF bus

1 and 3. The loss of power started division 3 diesel generator and

caused numerous isolations, one of which was instrument air that

eventually resulted in a reactor scram signal due to a scram discharge

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instrument volume high water level trip signal.

The plant was shutdown

in mode 4 at the time of the event.

The investigation by the licensee

discovered the secondary current transformer wiring problem which had

been masked by the previous differential relay wiring problem.

The

current transformer being wired backwards only became a problem when

the ESF transformer 11 differential relay wiring was corrected after

the trip on November 2,1985, and then only when the secondary side of

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ESF transformer 11 associated exclusively with the Division' 3'ESF bus,

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is lined up to Division 3 and the HPCS pump is started. 'It is

important to note that the Division 3 electrical bus can be lined up to

any of the three ESF transformers and the secondary side of ESF 11

associated with Division 3 can only supply power to Division 3 on

Unit 1.

Therefore, the improperly wired current transformer only comes

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into play when ESF transformer 11 is supplying power to the Division 3

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ESF bus.

The licensee has corrected the current transformer wiring

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problem and the GE drawings were corrected earlier.

The other ESF

transformer differential relays have been verified to be hooked up

properly.

c.

By letter dated November 6,1985, Transamerica DeLaval, Inc.

(TDI)

notified the NRC of a potential 10 CFR Part 21 defect in the TDI Diesel

Generators (DGs).

The defect concerned recently experienced isolated

failures of the intake and exhaust valve springs.

TDI stated that all

springs failed after an extensive operating experience of approximately

5,000 to 7,000 operating hours.

The suspect valve springs are

,

manufactured by Betts Spring Co. , San Leandro, California and are

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identified by a white stripe painted on the spring.

TDI is requesting

all users report the results of their inspection to determine if

corrective action is required.

No action was recommended other than

inspection.

The licensee's inspection of the Division 1 DG indicated

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that all valve springs had a white stripe on the side.

The Division 2

DG will be inspected during the first refueling outage.

No broken

valve springs have been identified at Grand Gulf and the DGs have less

,

than 2,000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> operating time.

This will be an Inspector Followup

,

Item (50-416/85-45-08).

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d.

By letter dated September 3, 1985, American Air Filter (AAF) notified

the NRC of a 10 CFR Part 21 defect in the Division 1 and 2 Diesel

Generator (DG) air intake silencers, model TDM or FTDM.

The defect was

a possibility of an internal part not being welded in place.

On a

commercial diesel engine installation identical in most respects to

standby diesel generator nuclear installations, a turbocharger and

diesel engine failure was experienced when an internal part of an AAF

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intake silencer was ingested into the turbocharger shortly af ter

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startup.

The ingested part was found not to have been welded in place

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per design.

Air pressures and vibration existing during engine

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operations were sufficient to dislodge the part and convey it down-

stream into the engine turbocharger.

AAF stated that if the DG has

been in service, the likelihood of the weld not being in place is much

lower and the licensee should schedule an inspection for verification.

The licensee inspected the DGs and visual inspection revealed that the

welds had been made.

This will be an Inspector Followup Item for record purposes

(50-416/85-45-09).

e.

On December 5,1985, Mississippi Power and Light (MP&L) notified the

NRC that they had discovered equipment installed in the plant which

appeared to be in violation

of 10 CFR 50.49 " Environmental Qualifi-

cation of Electric Equipment Important to Safety for Nuclear Power

Plants." This equipment consisted of 17 limit switches, 8 of which had

not been environmentally sealed and 9 had date codes missing.

The

plant was in cold shutdown at the time of the notification and the ,

licensee corrected all of the identified discrepancies prior to

startup.

The investigation by the licensee to determine if these limit switches

are in fact required to be environmentally qualified and if there are

any other discrepant equipment is continuing.

Pending the licensee's

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final resolution of the scope and extent of the problem this will be

identified as an Unresolved Item (50-416/85-45-10).

10.

Operating Reactor Events (93702)

The inspectors reviewed activities associated with the below listed reactor

events.

The review included determination of cause, safety significance,

.

performance of, personnel and systems and corrective action.

The inspectors

examined instrument recordings, computer printouts, operations journal

entries, scram reports and had discussions with operations, maintenance and

engineering support personnel as appropriate.

The licensee's investigation

into the Diesel Generator (DG) overspeed that occurred on November 6,1985,

has been completed and the DG has been reassembled.

The cracks in the main

generator base were evaluated by a consulting group, Failure Analysis

Associates, and it was determined that continued use of the existing base

was permissible.

Two meetings were held at the Grand Gulf Plant with NRC

representatives to explain what the licensee's investigation had shown.

On

November 14, 1985, Mr. Carl Berlinger and Mr. Emmett Murphy from NRR were

present and on November 21, Mr. Carl Berlinger, NRR and Mr. Paul Louzecky,

NRC consultant, were on site.

The Division 1 DG was completely disassembled

and the results of nondestructive examinations were available for review.

It appears the DG overspeed was the result of the inadequate refilling and

venting of the Woodward Governor following maintenance that required the

removal and draining of the Woodward Governor (including the booster and

cooler).

This overspeed condition resulted in substantial damage to the DG.

A description of the damage, inspection and repair is provided in the

summary of the meetings noted above.

Also, a meeting was held in the NRC

Region II office on December 13, 1985, where the licensee presented the

results of their investigation.

.

12

T.S.6.8.1 requires written procedures be established, implemented and

maintained covering activities recommended in Appendix A of R.G.1.33. R.G.

1.33 requires written procedures for performing maintenance that can effect

performance of Safety related equipment.

The Division 1 DG retest was

performed by Maintenance Work Order (MWO) M57687 dated November 6,1985.

A

review of the MWO indicated the following discrepancies.

(a) Maintenance Section Procedure (MSP) 07-5-09-40, revision 1, Control of

Retest Requirements, Paragraph 6.3.2.d. (1) states" when maintenance

retest (Special Instructions) are required that do not exist, and are

subsequently developed by a Maintenance Planner, an Engineer will

review the maintenance retest and approve, disapprove, or modify

accordingly."

Contrary to the above, the special instruction included

in the MWO does not have the approval signature of the Responsible

Maintenance Engineer (RME).

(b) MSP-07-5-09-40, Revision 1, Paragraph 6.3.2 requires the RME/Respon-

sible Field Engineer (RFE) specify maintenance retests.

Contrary to

the above, maintenance retests were specified by a Mechanical

Supervisor.

(c) Preventive Maintenance Instruction 07-5-24-P75-E001AB-5, Revision 0,

Periodic Oil Change of the Standby Emergency Diesel Woodward Governor

Model #EGB-35-C, paragraph 7.10.1 states "Run engine 15 minutes, stop

engine and drain governor oil and fill with fresh oil."

Contrary to

the above, the retest specified by MWO M57687 did not specify the

draining of governor oil & refill with fresh oil following a 15 minute

run.

The failure to follow procedures as noted above is a violation

(50-416/85-45-11).

The Woodward Governor manual for the EG-B35 and EG-B50 hydraulic actuators,

Grand Gulf (GG) TDI diesels use EG-B35C governors, has a warning that the

engine should be equipped with separate overspeed shutdown devices to

protect against runaway or damage to the engine should the mechanical-

hydraulic governor, or electric controls, the actuators, fuel control, the

driving mechanism, the linkages or the controlled devices fail.

The GG

diesels have a separate overspeed device manufactured by the Woodward

Governor Company. The overspeed trip is set at 15% over the normal governor

speed of 450 rpm (or 517 rpm).

During tests following the overspeed event

the licensee measured the response time of their overspeed trip and found a

2.25 second time delay.

This was on Unit 2.

Also, TDI has stated that the

DGs on an unloaded start from rest will be accelerating at approximately 50

rpm /sec at 350 rpm and accelerating at approximately 100 rpm /sec at 517 rpm.

It can be surmised then that a DG without the benefit of a governor would

probably be damaged to some extent by the time the overspeed trip would take

effect.

The Woodward Booster and Cooler are part of the Woodward Governor

. -- -- - _ ~

- . _ - - - . - - _ _ _ _ - - . - - - . -

. - - - . . _ _ - = - .

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assembly used on the Division 1 & 2 DGs.

The Booster Servomotor Bulletin,

.

36684 B, the latest vendor document that the licensee had available on site,

{

does not have any cautions or warnings about purging air.

However, Bulletin

36684 J, which is a later issue, contains a caution regarding prcper purging

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of air to prevent possible sluggish governor response.

The licensee

returned the Woodward governor to the manufacturer for testing, and when

tested with an equal amount of oil as found following the overspeed event,

,

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the governor was erratic in operation which would probably explain the loss

]

of governor control.

The licensee's procedure for changing oil in the

Woodward governor is Preventive Maintenance Instruction (PMI) 07-5-24-P75-

E001AB-5, Periodic Oil Change of the STBY.

EMER. Diesel Woodward Governor

3

Model #EGB-35-C. Paragraph 7.9 fills the governor with new clean oil to the

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top of the gauge glass and then paragraph 7.10 has the operator turn the

governor speed control down to idle speed (300 rpm approximately) and start

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the engine (DG) unexcited.

The procedure does not require purging air from

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the governor prior to start. It is not clear that the licensee had adequate

warning that starting the DG and then venting the Woodard Governor could

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result in an overspeed event.

This appears to be a generic issue which the

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licensee has initiated action to inform other DG users of the potential for

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damage.

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11.

IFI & Unresolved Items (92701)

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a.

(Closed) IFI 50-416/85-39-02.

The licensee has completed the investi-

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gation into the DG overspeed event.

This item is discussed in para-

graph 10 of this report.

This item is closed.

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b.

(Closed) IFI 50-416/85-06-05.

The inspector has received a response

l

regarding the adequacy of Technical Specifications.

This item is

4

closed.

c.

(Closed) IFI 50-416/85-14-01.

The licensee has submitted an updated

FSAR.

This item is closed.

d.

(Closed) IFI 50-416/85-14-02.

The inspectors have reviewed the

,

licensee's actions addressing the concerns associated with this

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followup item.

Reviews of subsequent post trip analysis indicate that

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these actions were adequate to prevent further occurrence.

This item

is closed.

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12.

License Condition

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The Grand Gulf operating license, NPF-29, paragraph 2.C. (9) requires that

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prior to startup following the first refueling outage, MP&L shall complete

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structural modifications, if required, as a result of the NRC staff's

completion of its review of the licensee's response to IE Bulletin 80-11.

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By letter dated November 4,1985, from Mr. T. Novak, NRC to Mr. J. Richard,

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MP&L, the NRC stated that the GGNS submittals were acceptable and license

condition 2.C.(9) has been fulfilled.

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In the areas Inspected, no violations or deviations were identified.

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