ML20138Q432

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Part 21 & Third Interim Deficiency Rept NCR 85-391,Item 209 Re Size Variation of Siemens-Allis Secondary Disconnect Fingers.Initially Reported on 850301.Acceptable Fingers Installed.Final Rept Will Be Submitted by 860228
ML20138Q432
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 12/13/1985
From: Watson R
CAROLINA POWER & LIGHT CO.
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
CON-NRC-407, REF-PT21-85, REF-PT21-86-018-000 209, HO-850481-(), HO-850481-(O), NCR-85-391, NRC-85-391, PT21-86-018-000, PT21-86-18, NUDOCS 8512270216
Download: ML20138Q432 (4)


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s Cp&L Carolina Power & Light Company Y U E C 1 7 p 3,. 5 SHEARON HARRIS NUCLEAR PROJECT P.O. Box 101 New Hill, North Carolina 27562

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M fe l s 9 5 60-7v File Number: SHF/10-13510E Letter Number: HO-850481 (0)

Dr. J. Nelson Crace NRC-407 United States Nuclear Regulatory Commission Region II 101 Marietta Street, Northwest (Suite 2900)

Atlanta, Georgia 30323 CAROLINA POWER & LIGHT COMPANY SHEARON HARRIS NUCLEAR POWER PLANT 1986 - 900,000 KW - UNIT 1 6.9 KV SWITCHCEAR CIRCUIT BREAKERS -

SECONDARY DISCONNECT FINGERS, ITEN 209

Dear Dr. Grace:

Attached is our third interim report on the subject item which was deemed reportable per the provisions of 10CFR50.55 (e) and 10CFR, Part 21, on March 1, 1985. CP&L is pursuing this matter, and it is currently projected that corrective action and submission of the final report will be accomplished by February 28, 1986.

Thank you for your consideration la this matter.

Your very truly, k

R. A. Watson Vice President Shearon Harris Nuclear Power Plant RAW:jsb Attachment cc: Messrs. C. Maxwell (NRC-SHNPP)

J. M. Taylor (NRC)

NBI-OS1 8512270216 851213 DR ADOCK 05000400 PDR I \\

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CAROLINA POWER & LIGHT COMPANY SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 THIRD INTERIM REPORT SECONDARY DISCONNECT FINGERS 6.9 KV CIRCUIT BREAKERS NCR 85-391 ITEM 209 DECEMBER 11, 1985 REPORTABLE UNDER 10CFR 50.55(e) AND 10CFR PART 21 IBMD-WKCB02-OS4

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SUBJECT:

Shearon Harris Nuclear Power Plant Unit No. 1 i

10CFR50.55(e) and 10CFR Part 21 reportable deficiency. Non-uniform sized secondary disconnect fingers on 6.9 KV Class IE switchgear breakers Purchase Orders NY-435112 and NY-435113 from Siemens Allis, Inc.

ITEM:

6.9 KV circuit breaker secondary disconnects.

SUPPLIED BY:

Siemens-Allis, Sanford, North Carolina.

NATURE OF DEFICIENCY:

Due to variations in manufacturing process and material, the secondary disconnect fingers are of varying length. The varying length af fects the quality of the connections at the secondary disconnect. These connections are an integral part of the breaker control circuitry.

DATE PROBLEM IDENTIFIED:

Shearon Harris parsonnel identified this problem via NCR 85-391 on February 13, 1985.

DATE PROBLEM REPORTED:

On March 1, 1985, CP&L (Mr. N.J. Chiangi) notified the NRC (Mr. A. Hardin) that the item was reportable under the provisions of 10CFR50.55(e) and 10CFR Part 21.

SCOPE OF PROBLEM:

The deficiency involves the twenty five Unit 1 Class 1E 6.9 KV switchgear breakers.

SAFETY IMPLICATIONS: When contacts are made with insufficient wipe and pressure to ensure adequate and reliable trip and reclose control circuits, the ability of the breaker to operate during emergency events is adversely affected.

REASON DEFICIENCY IS REPORT-ABLE:

As redundancy is compromised due to a generic deficiency, the availability of electric power from either offsite or onsite sources needed to operate ESF Systems is compromised. This reduces the degree of protection to plant systems and to public health.

CORRECTIVE:

ACTION:

Siemens-Allis has partially supplied new fingers to Shearon Harris. These fingers were subjected to a 100% conventional and compression inspection to assure conformance by Siemens-Allis. The Siemens-Allis Quality Assurance unit is pursuing IBHD-WKCB02-OS4 i

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corrective action through their subvendor via appropriate changes in the subvendors QA program and acceptance criteria. The Shearon Harris site is currently inspecting secondary disconnect fingers at the site. From initial inspections it has been determined that existing fingers do not conform to the length of the new fingers. The original fingers will be replaced with the new fingers. Completion of the installation of the new fingers will commence once Siemens Allis supplies the balance of the disconnect fingers to the Harris site.

FINAL REPORT:

Completion of the installation of the new secondary disconnect fingers for 6.9 KV switchgear is scheduled for completion on February 28, 1986.

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